ML20205N966

From kanterella
Jump to navigation Jump to search
Insp Repts 50-424/86-09 & 50-425/86-04 on 860201-0331. Violation Noted:Failure to Perform Adequate Sys Walkdown During Turnover of safety-related Sys for Unit 1
ML20205N966
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 04/17/1986
From: Livermore H, Rogge J, Schepens R, Sinkule M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20205N947 List:
References
50-424-86-09, 50-424-86-9, 50-425-86-04, 50-425-86-4, NUDOCS 8605210030
Download: ML20205N966 (26)


See also: IR 05000424/1986009

Text

i

.

'

UNITED STATES

[pKfooq'o,

NUCLEAR REGULATORY COMMISSION

['

'n

REGION 11

i

.

g

,j

101 MARIETTA STREET.N.W.

j

's

ATLANTA. GEORGI A 30323

\\m.+/

.

'

Report Nos.:

50-424/86-09 and 50-425/86-04

Licensee: Georgia Power Company

P. O. Box 4545

.

Atlanta, GA 30302

Docket Nos.: 50-424 and 50-425

- License Nos.: CPPR-108 and CPPR-109

Facility Name:

Vogtle 1 and 2

Inspection Conducted:

February 1 - March 31,1986

L

Inspectors: _

Y

[wWI

/

6

H. H. Livermore, Senior Resident. Inspector

Date Signed

-I "p

9

l

Construction

j

f

h

-(N.k

A}r 7/96

pn J. F. Rogge, Senior Resident lyspector, Operations

Date Signed

'

f J & !

z ~ (-

n/o/os

'

fet R. J. 'Schepens, R sident Inspector, Construction

Date Signed

'b b

Approved by:

/7

i

j

M. V. Sinkule, Section Chief

Date Signed

Division of Reactor Projects

i

SUMMARY

Scope: This routine, unannounced inspection entailed 457 Resident inspection-

hours on site (133 hours0.00154 days <br />0.0369 hours <br />2.199074e-4 weeks <br />5.06065e-5 months <br /> were on backshifts) inspecting: containment and safety

,

l

related structures, piping systems and supports, safety related components,

auxiliary systems, electrical equipment and cables, instrumentation, preopera-

tional test program, quality programs and administrative controls affecting

quality, and follow-up on previous inspection identified items.

The second

corporate management meeting was conducted during this period and the Atomic

Safety and Licensing Board hearings were attended.

i

Results: One violation was identified

" Failure to Perform an Adequate System

Walkdown During the Turnover of Safety-Related Systems" - Paragraph 11.

!

t

8605210030 860418

PDR

ADOCK 05000424

G

PDR

,

,e

- . - -

.,

y-

,,-.., -,+<_ ,- .,.-,,

.-

.-sy--c-,4m---

  • . - , .

, , . _ ,

_

-~%

-~ r vv.-

m

y-

,-r

w--

,. --

--

..

. _. . _

. . ..

. _

.

. _ .

4

'

e

4

.

l

.

DETAILS

'

1.

Persons Contacted

Licensee Employees

R. E. Conway, Senior Vice-President, Vogtle Project Director

D. O. Foster, Vice-President, Project Support

  • R. H. Pinson, Vice-President, Project Construction

P. D. Rice, Vice-President, Engineering

W. T. Nickerson, Assistant to the Project Director

W. C. Ramsey, Readiness Review Manager

R. W. McManus, Readiness Review

"M. H. Googe, Project Construction Manager

  • G. Bockhold, Jr., General Manager Nuclear Operations
  • H. P. Walker, Manager, Unit Operations

C. W. Hayes, Vogtle Quality Assurance Manager

  • C. E. Belflower, Quality Assurance Site Manager - Operations
  • E. D. Groover, Quality Assurance Site Manager - Construction

S. D. Haltom, Quality Assurance Engineering Support Supervisor

W. E. Mundy, Quality Assurance" Audit Supervisor

D. M. Fiquett, Project Construction Manager - Unit 2

  • B. C. Harbin, Manager Quality Control

'

G. A. McCarley, Project Compliance Coordinator

'

"W. C. Gabbard, Regulatory Specialist

,

W. F. Kitchens, Operations Superintendent

'

T. Dannemiller, Senior QA Engineer

  • J. F. D' Amico, Regulatory Compliance Superintendent

C. L. Coursey, Maintenance Superintendent

M. A. Griffis, Superintendent-Maintenance

N. R. Harris, Quality Control Assistant Manager

i

W. R. Duncan, Readiness Review

i

R. M. Bellamy, Initial Test Manager

i

'

Other licensee employees contacted included craftsmen, technicians, super '

vision, engineers, inspectors, and office personnel.

,

,

Other Organizations

,

  • F. B. Marsh, Project Engineering Manager - Bechtel

H. M. Handfinger, Preoperational Test Superintendent - Bechtel

B. F. Hurless, QA Surveillance Specialist - Bechtel

G. F. Trudeau, Readiness Review - Bechtel

W. F. Hindle, Engineer - Bechtel

  • Attended Exit Interview

i

a

i

4

3

-,

--,,_.,,.,.-,>-.-.=m-

--r,..-n-

er -

., ,-- - , - , ,

,e.,

,-..---e--.,

-m,.,

- . ,

w---u-.y.*

-.,.-r,--m--

-

,-

..r,.

- - - - - , .-

e--,,ee..-

-

.

.

2.

a

-

2.

Exit Interview (30703C)

The inspection scope and findings were summarized on March 31, 1986, with

those persons indicated in paragraph 1 above.

The inspector described the

areas inspected and discussed in detail the inspection finding listed below.

No dissentirg comments were received from the licensee.

The licensee did

'

not identify as proprietary any of the materials provided to or reviewed by

the inspector during this inspection.

(0 pen) Violation, 50-424/86-09-01 " Failure to Perform an Adequate System

Walkdown During the Turnover of Safety Related Systems" - Paragraph Ell.

(0 pen) Inspector Followup Item, 50-424/86-09-02 " Review Licensee Action

Pertaining to the Restoration of Safety Related Equipment" -Paragraph 11.

t

!

I

(0 pen) Inspector Followup Item, 50-424/86-09-03 " Review Licensee Resolution

,

of Instrumentation Documentation Forwarding to the Vault During Turnover" -

4

Paragraph 11.

)

(0 pen) Inspector Followup Item, 50-424/86-09-04 " Review Projects Revised

]

Response to Quality Concern No. 85V0582" - Paragraph 5.

.

1

(0 pen) Inspector Followup Item, 50-424/86-09-05 "Reviev Licensee Action to

j

Resolve HVAC Handswitch Nomenclature" - Paragraph 11.

(0 pen) CDR 86-93 "Procass and Root Valvac" - Paragraph 4

'

(Closed) Violation, 50-424/85-37-01 " Failure to- Prescribe Appropriate

Procedures to Control Area Cleanliness" - Paragraph 3.

(Closed) C0R 86-92 and Inspector Followup Item, 50-424/85-63-01 "Trans-

america Delaval

Inc.

(TDI) Diesel

Generator Jacket Water Pump" -

i

!

Paragraph 4.

(Closed) Unresolved Item, 50-424/84-32-01 " Evaluation of Failure to Report a

Potential Significant Deficiency" - Paragraph 4.

,

The following NRC exit interviews were attended during the inspection period

by a resident inspector:

t

Date

Name

February 14

G. A. Schnebli, L. E. Nicholson

J. R. Harris, J. J. Lenahan

i

F. R. McCoy, W. K. Poertner

S. J. Vias

'

G. A. Hallstrom

February 28

G. R. Wiseman

,

~

E. H. Girard

T. D. Gibbons

'

. ---

.

-

.

3

Date

Name

!

(Continued)

March 5

F. R. McCoy

March 17

G. A. Schnebli

March 21

S. J. Vias

W. Kleinsorge

"

R. W. Newsome

'

M. D. Hunt

T. F. McElhinney

"

!

A. L. Cunningham, et. al.

!

March 27

R. W. Wright, R. A. Moore

l

L. H. Jackson, J. H. Moorman

March 28

L. E. Nicholson

3.

Licensee Action on Previous Enforcement Matters (92702)

(Closed) Violation 50-424/85-37-01, " Failure to Prescribe Appropriate

Procedures to Control Area Cleanliness". The Inspector has reviewed Georgia

]

Power Company's (GPC) response dated October 23, 1985, and the revised GPC

'

Field Procedure GD-T-17 which incorporated the zone designation requirements

of ANSI N45.2.3.

In addition, since the initial occurrence, the Inspector

'

'

has observed the implementation of zone cleanliness by GPC in various areas.

1

Based on the above reviews and field observation of controlled zone

postings, the inspector has determined that the corrective actions have been

acceptably addressed and are complete.

3

,

4.

Followup on Previous Inspection Items (92701)

i

(Closed) CDR 86-92 and Inspector Followup Item 50-424/85-63-01.

Trans-

,

l

america Delaval, Inc. (TDI) Diesel Generator Jacket Water Pump.

The

licensee's evaluation and corrective action as documented in letters dated

February 14, 1986 and March 10, 1986, was reviewed.

The TDI letter dated

,

January 22, 1986, to the NRC was also reviewed.

During this inspection

period the Resident Inspector notified the NRC Vendor Branch that only two

.

of the three faulty pump - impellers were onsite.

Followup by the Vendor

!

Branch with TDI resulted in further vendor review and final location of the

third impeller in Saudi Arabia.

i

(0 pen) CDR 86-93 Process and Root Valve.

The licensee informed the

residents on the progress toward resolution for this item. The licensee has

performed field walkdowns to determine if the hardware has been affected.

j

The problem, with a few exceptions, was presented as being limited to the

Valve Designation List and the Quantity Tracking System data differences.

This item continues to remain open until final corrective action is

implemented.

,

,

9

--.-,-----oe,,--,w--.

- - . , , , - .

.,-r.-,y.7-..,---.s-~v._,e-,-_e-ey.-,.r.-

,

,ey. . .

- - - - - -

..-.,-,.7,.,y-

,-,---%. , .

.-y---

,

--

. . . ,

-

-

. - .

.-.

. .,.

-.

-

'$.

4

,

,

4

-

I

(Closed) ' Unresolved Item 50-424/84-32-01, "Fai' .re to Report a Potential

Significant Deficiency". This item was reviewed and the Inspector concluded

that the licensee had performed timely identification and reporting of the

Cable Separation issue.

5.

Construction Inspection - Units 1 & 2

2

1

'

I

Periodic inspections were made throughout this reporting period in the form.

j

of general type inspections in different areas of both facilities. The

<

areas were selected on the basis of the scheduled activities and were varied

d

to provide wide coverage. Observations were made of activities in progress

to note defective items or items of noncompliance with the required codes

a

!

and regulatory requirements. On these inspections, particular note was made

!

of the presence of quality control inspectors, supervisors, and quality

control evidence in the form of available process sheets, drawings, material

identification, material protection, performance of tests, and housekeeping.

I

Interviews were made with craft personnel, supervisors, coordinators,

quality control inspectors, and others as they were available in the work

areas.

!

'

The inspector reviewed nu'mbrous construction deviation reports to determine

if requirements were met in the areas of documentation, action to resolve,

justification, and approval signatures in accordance with GPC Field Proce-

'

,

cure No. GO-T-01.

I

i

-l

The inspector cnnducted a review of the licensee's Quality Concern package

l

identified as 85V0582.

During the review the inspector questioned the

"

4

!

project's response in several areas and conducted a meeting on Monday,

March 17, 1986, with the licensee to address the Inspector's questions. The

e

"

licensee committed to address the Inspector's questions via a revised

I

l

project response. The inspector advised the licensee that, pending review

i

'

of the project's revised response, this matter will be identified as

Inspector Followup Item 50-424/86-09-04, " Review Project's revised response

!

to Quality Concern No. 85V0582.

t

Readiness Review Module No.

7,

" Plant Operations and Support", and

1

l

Appendix G, " Measuring and Test Equipment," were reviewed during this

l

inspection period.

!

l

No violations or deviations were identified.

i

'

4

f

i

>

r

!

E

i

+

"

t

h

2

'

,

>

a

+

-

2-n

e

a-

-

h:

-

r+-

w-m

1

.-

5

-

i

l

i

j

6.

Fire Prevention / Protection and Housekeeping Measures - Units 1 & 2 (42051C)

The inspector reviewed and examined portions of the following procedures

1

pertaining to the fire prevention / protection measures and housekeeping

measures to determine whether they comply with applicable codes, standards,

4

"

NRC Regulatory Guides and licensee commitments.

!

!

- SD-T-05, Rev. 6 Fire-Protection Equipment Inspection and Testing

I

GD-T-15, Rev. 5 Welding and Cutting

-

GD-T-17, Rev. 4 Housekeeping

-

i

The inspector observed fire prevention / protection measures in work areas

j

containing safety related equipment during the inspection period to verify

,

the following:

1

i

Combustible waste material and rubbish was removed from the work areas

-

l

as rapialy as practicable to avoid unnecessary accumulation of

j

combustibles

j

-

Flammable liquids are stored in appropriate containers and in

j

designated areas throughout tSe plant

.

4

-

Cutting and welding operations in progress have been authorized by an

appropriate permit, combustibles have been moved away or safely

i

covered, and a fire watch and extinguisher was posted as required

j

-

Fire protection / suppression equipment was provided and controlled in

j

accordance with applicable requirements

j

4

No violations or deviations were identified.

4

7.

Structural Concrete - Unit 2 (47053C)

.!

>

a.

Procedure and Document Review

,

The inspector reviewed and examined portions of tFe following proce-

,

l

dures pertaining to the placement of concrete to determine whether they

comply with applicable codes, standards, NRC Regulatory Guides and

j

licensee commitments:

CD-T-02, Rev. 17

Concrete Quality Control

-

- CD-T-06, Rev. 9

Rebar and Cadweld Quality Control

- CD-T-07, Rev. 8

Embed Installation and. Inspection

CD-T-EO, Rev. 6

Installation and Inspection of Trumpets,

-

,

Rigid Extensions, and Duct Sheathing

'

i

!

'

,I

i

.

. . - - . .

.

-.

.

._.

..

_ . .

-

3

l

6

j

-

i

b.

Installation Activities

,

j

- The inspector witnessed portions of the concrete placement indicated

below to verify the following:

)

(1) Forms, Embedment, and Reinforcing Steel Installation

-

Forms were properly placed, secure, leak tight and clean.

Rebar and other embedment installation was installed in

-

accordance with construction specifications < and drawings,

secured, free of concrete and excessive . rust, specified

j

distance from . forms, proper onsite rebar bending (where

j

applicable) and clearances consistent with aggregate size.

(2) Delivery, Placement and Curing

)

-

Preplacement inspection was completed and approved prior to

placement utilizing

a

Pour Card (Procedure

Exhibit

!-

CD-T-02*18).

-

Construction joints were prepared as specified.

i

-

Proper mix was specified and delivered.

)

-

Temperatura control of the mix, mating surfaces,'and ambient

j

were monitored.

Consolidation was performed correctly.

-

Testing at placement location was properly performed in

-

accordance with .the acceptance criteria and recorded on a

Concrete Placement Pour Log (Procedure Exhibit CD-T-02*20).

Adequate crew, equipment and techniques were utilized.

-

.

1

j

-

Inspections during placements were conducted effectively by a

j

sufficient number of qualified personnel.

I

j

-

Curing methods and temperatures were monitored.

1

1

i

)

I

!

I

<

]!

!

!

-

4

,

4

4

--,_

. . . . , , , _ . _ , . _ - _ _ . . . - - - . .

-__--_._-,,-_---,_-_,-...,,m.--,.,

_.-_.-4._,-..

_

.

.

-

.

.. .

.-

.

.

.-

-

.

.

'

7

.

4

(3) Installation of Tendon Sheaths for Containment Pours Only

-

Tendon Sheaths were oriented properly, installed within

specified tolerances, clear and free of damage.

4

Pour No.

Location

Inspection Activity

4

2-072-001.002

Diesel Generator Building-

Placement

!

Level 2 Slab

1

2-301-001 A,

Condensate Storage Tanks-

Preplacement, Place-

B&C

Base Slab

ment & Curing

2-010-024A

Construction Opening-

Preplacement &

i

Elevation 214'-7" to

Placement

224'-7"

2-051-005 A&B

NSCW Beam & Cross Wall

Preplacement &

Placement

!

c.

Rebar Splici,ng

.-

The Inspector witnessed cadwelding operations for the cadwelds indi-

l

cated below to verify the following:

-

Inspections are performed during and after splicing by qualified

j

QC inspection personnel,

i

Each splice was defined by a unique number consisting of the bar

-

size, splice type, the position, the operator's symbol, and a

>

sequential number.

<

Process and crews are qualified.

-

.

The sequential number and the operator's symbol are marked on all

-

,

completed cadwelds.

'

Operator's Symbol /

,

Pour No.

Location

Sequential Number

2-010-024

Construction Opening

CR 329

2-010-024

Construction Opening

CR 330

.,

A-111-01B

Control Building Opening

EA 35

A-111-01B

Control Building Opening

EA 36

A-111-01B

Control Building Opening

EA 37

A-111-01B

Control Building Opening

EA 39

,

m.-

-,nw.w

- ,

,w

,,--,m-


,--,,--m

w,,,,,,,n,.

..m..,,-,

.',n,w.,

,-,,,s.

--w,-n-,,p---,.myr-4-m,,,,--

-,.wm-pa

mm---,

- , , ,

_ __

. .

_

.. - .

.

-

__

_

..

.

.

8

i

-

i

i

The inspector also conducted random inspections of completed cadwelds

at the locations noted below to verify the following:

'

-

Tap hole does not contain slag, blow out, or porous metal.

)

-

Filler metal was visible at both ends of the splice sleeve and at

the tap hole in the center of the sleeve. No voids were detected

at the ends of the :leeves.

,

.

The sequential number and the operator's symbol are marked on all

-

completed cadwelds.

,

Pour No.

Location

Inspection Activity

[

2-301-001 A,8&C

Condensate Storage Tanks

Anchor Cadwelds

2-01C-45

Reactor Vessel Pourback

Rebar Splice Cadwelds

'!

No violations or deviations were identified.

4

8.

Containment (Prestressing) - Unit 1 (47063C)

j

a.

Procedure end Document Review

4

The inspector reviewed and examined portions of the following speci-

!

fication, procedure, and drawings pertaining to the installation of

vertical ter. dons, to determine whether they comply with applicable

codes, standards, NRC Regulatory Guides and licensee commitments.

I

X2AF04

Technical Provisions for Containment

-

Post-Tensioning System

t

-

AX2AF04-100-12

Field Instruction Manual for Installation

of VSL E5-55 Post-Tensioning System Within

.

i

Nuclear Containment Structures, Rev. 9.

!

b.

Installation Activities

1

The inspector witnessed portions of the installation activities indi-

l

cated below to verify the following:

.

,

4

The latest i ssue (revision) of applicable drawings or procedures

-

i

are available to the installers and were being used.

4

4

-

Tendons were free of nicks, kinks, corrosion; were it. stalled in

designated locations; and that the installation sequence and

.

technique was per specified requirements.

-

Installation crew was properly trained and qualified.

-

,

j

QC inspection was properly performed by qualified personnel in

-

accordance with applicable requirements.

l

l

4

-,.--.-r4.--c..w---.--,,,-.,%,ec,--.-w..--.ge-.-,,,

-,

w - -,

-7,-,r-,

m.,,.ww.

,_+,.v,--,-,-,.,e.,

enew.~-..

.y.#..

, ,

.-,-..,--,,w

.- -

..

.

.

-

.

-.

..

.

t

9

-

1

-

Adequate protective measures were being taken to ensure. mechanical

and corrosion protection during storage, handling, installation,

,

and post installation.

The following tendons were observed:

,

Vertical

i

Tendon No.

Length

Seq. No.

_ Activity

29-83*

557'

23

Tendon Installation

31-81*

549'

24

Tendon Installation

  • Surveillance Tendon

No violations or deviations were identified.

i

9.

Containment (Steel Structures and Supports) - Units 1 & 2 (48053C)

i

Periodic inspections were conducted to observe containment steel and support

installation activities in progress, to veri #y the following:

Components were being

properly

handled (included bending

or

-

straightening).

'

!

-

Specified clearances were being maintained.

,

Edge finishes and hole sizes were within tolerances.

-

l

Control, marking, protection and segregation were maintained during

-

l

storage.

-

Fit-up/ alignment meets the tolerances in the specifications and

j

drawings.

Some of the more specific structural steel installation activities inspected

i

were in the Unit 2 containment building area on A level (elevation 220') and

the pipe racks on C' level (elevation 143').

}

j

No violations or deviations were identified.

10.

Safety-Related Structures (Structural Steel and Supports) - Units 1 & 2

l

(48063C)

1

Periodic inspections were conducted to observe construction activities of

4

safety-related structures / equipment supports for major equipment outside the

containment to verify that:

4

Materials and components were being properly handled to prevent damage.

-

i

l

.

-3

,, - . - ~

i.e.,,..

--.,w_m..w,c..w-ww.,,,,..,,,,-va-

_e-,,.m_.

__..w.-,-,

,

_.--,-,,c4

,v-,.-.-,--m-

,,---,,#-,,,.m

._.,+._,,6

. . ,-

_ _ _ . , , , _ . .

-

_

_

o

4

10

'

-

1

-

Fit-up/ alignment were within tolerances in specifications and drawing

requirements.

-

Bolting was in accordance with specifications and procedures.

i

-

Specified clearances from adjacent components were being met.

One of the more specific safety-related structure installation activities

inspected was the Unit 2 refueling water storage tank liner plate erection

'

to verify the following:

-

Plate and other materials are controlled in accordance with specifi-

cations, codes, drawings, and procedures.

,

,

-

Fitting and aligning are properly controlled as required.

1

-

Welding is in accordance with approved procedures by qualified welders,

i

1

-

Examination and testing are in accordance with the specification,

j

codes, drawings, and procedures.

j

No violations'or deviations were identified.

l

11.

Reactor Coolant Pressure Boundary and Safety Related Pining - Observation of

Work and Work Activities - Unit 1 (49053C) (49063C) (37301)

i

1

During the inspection period, pipe run walkdowns were performed to determine

whether the piping run was installed as shown on approved drawings and in

accordance with applicable construction specifications.

Specific pipe run

walkdowns included a walkdown of the following ASME B&PVC,Section III,

Class I, II & III Piping as listed below:

P&ID NO. REVISION

PIPE RUN INSPECTED

1X4DB122, Rev. 17

Residual Heat Removal (RHR) System Trains A&B

Suction and Discharge Piping in the Auxiliary

Building.

(Line No's. 003-12", 003-14", 028-14",.

J

013-3", 039-12", 003-14", 005-8", 007-8", 012-2",

004-14", 027-14", 014-3", 040-12", 006-8",

008-2", 008-8", & 009-8").

4

1X4DB133-1, Rev. 15

Nuclear Service Cooling Water (NSCW) System

'

Train A Supply and Return Header' Piping in NSCW

Tower, and Supply and. Return Piping to the

Component Cooling Water Pump Motor Coolers.

(Line No's. 023-18", 031-18", 033-18", 004-24",

416-1/2", 417-1/2", 419-1/2", 418-1/2", 420-1/2",

4

'

421-1/2", 045-3", 047-3", 007-12", 008-12",

009-12", 010-12", 181-24", 004-16", 471-2",

390-18", 049-3", 077-2", 063-2", 049-2", 079-2",

067-2", 053-2", 053-3", 005-1", 006-1", & 003-16").

l

r

.

.

u .

.-

.

.--

.

-

a- .

.

---

- .

.

-2---.m-

.- -

--ia--

--


m-

.

ms---u-

.

11

-

1X4DB133-2, Rev. 17

NSCW Train B Inlet and Outlet Piping to the

Auxiliary Component Cooling Water Heat Exchanger.

,

(Line No's. 084-18", 086-18", & 241-2").

1X4DB134, Rev. 14

NSCW Train A Supply and Return Header to CVCS,

SI, CS, and RHR Motor Coolers (Line No's. 004-16",

004-4", 003-4", & 003-16").

1X4DB135-1, Rev. 17

NSCW Train A Inlet and Outlet Piping to the

Auxiliary Component Cooling Water Heat Exchanger

and Supply and Return Header Piping to the

,

Containment Coolers.

(Line No's. 390-18",

175-18", 174-18", 174-14", 179-14", 176-2",

177-2", 178-2", 062-2", 028-2", 182-2", 348-2",

187-14", 222-8", 187-10", 187-8", 195-8", 002-8",

194-8",226-8",002-10",002-14").

IX4DB161-2, Rev. 15

Auxiliary Feedwater (AFW) System Train A&B

Suction and Discharge Piping.

(Line No's.

016-8", 024-8", 046-4", 054-2-1/2", 020-4",

,

025-8", 017-8", 045-4", 042-2-1/2", 003-1/2",

091-1/2",062-2",037-2",063-2").

.

Inspections were performed on a rancom daily basis.

!

)

Specific areas examined during the pipe run walkdown for compliance with the

applicable piping & instrumentation drawings and the Plant Design and

!

Instrumentation Construction Specification No. X4AZ01, were as follows:

Vent and Drain Connections and Locations

Instrumentation Connections and Locations

Valve Installation and Orientation

Line Size and Location

Fittings Type and Location

Pipe / Valve / Fitting End Connections

Hanger Locations and Types

The Inspector reviewed and examined portions of the following procedures

pertaining to system turnover:

GD-T-31, Rev. 1

System and Area Turnover Verification

GD-A-48, Rev. 1

Nuclear Construction System Turnover

GD-A-49, Rev. O

System Walkdown and Master Tracking System

Punchlist Input.

SUM-9, Rev. 6

System Turnover

'

SUM-17, Rev. 6

System Punchlist

- .. _. -. - - -.

-

. - . . - . - . .

-.- - --..- - -.

. . . - - .

.

.

- - -

-

-

-

-

-

.

.

.

12

-

<

During the inspection, the Inspector identified the following discrepancies

regarding the as-built configuration as compared to the P&ID:

-

RHR Train B Valve No. 1-1205-X-403 was found not to be installed

1

l

RHR Trains A&B Valve No's. 1-1205-U4-120 and 1-1205-U4-121 were found

-

to be installed in the incorrect flow direction (i.e., flow is over

seat).

-

NSCW Trains A&B Valve No's. 1HV-11707 and 1HV-11621 were found to be

l

installed in the incorrect flow direction.

-

NSCW Trains A&B Valve No's. IPSV1718 and IPSV1719 were found to be

I

installed on the outlet side of the auxiliary component cooling water

(ACCW) heat exchanger. The piping and instrumentation diagram (P&ID)

shows it to be installed on the inlet side.

,

-

NSCW Train A temperature element No's. 1TE-11641, 1TE-11642, ITE-11643,

and 1TE-11644 were found to be installed in reverse order to what the

P&ID shows.

-

NSCW Train A Valve No's. 1-1202-X-312 and 1-1202-X-313 were found to be

in reverse locations from what the P&ID shows.

The above discrepancies are examples of the licensee's failure to perform an

,

adequate system walkdown during the turnover of safety-related systems.

l

Several meetings were held with the licensee to fully discuss NRC concerns

in this area.

The NRC concern centers on the fact that the above discrep-

ancies were not identified nor documented during' the construction walkdown

per Field Procedure GD-A-49. Also, the fact that these systems (i .e. , RHR &

,

NSCW) have been turned over to Operations for pre-operational testing since

September 18, 1985 and September 14, 1985, respectively and the above

!

discrepancies were not identified on the system punchlist as required by

SUM-17. Also, there does not appear to be any requirement in the Startup

.

Manual for the test supervisor or test engineers to conduct periodic system

walkdowns and to what attributes to inspect so as to ascertain the current

'

system status.

l

The foregoing is considered to be in violation of 10 CFR Part 50,

f

Appendix B, Criterion V and will be identified as Violation 50-424/86-09-01

'

" Failure to Perform an Adequate System Walkdown During the Turnover of

'

l

Safety-Related Systems."

l

'

During the above system walkdowns, the Inspector also noted the Limitorque

h

covers on Valves 1HV-8804B, 1HV-8812A, 1HV-8812B, and 1HV-2138 were not

'

properly secured after maintenance.

The inspector informed the licensee

that, pending review of the licensee's action pertaining to the restoration

of safety-related equipment, this matter will be identified as Inspector

'

Followup Item 50-424/86-09-02 " Review Licensee Action Pertaining to the

I

Restoration of Safety-Related Equipment."

!

_ , - .

,

,_,,._y__,., _ , _ .

_.,,,m___.,.-c_

-.,._,,-~.,y--.

_ . . . . - -

.,-o

, - ,

_-.-,_e.

__

-.r_

. , . . ~

_ , _ , ,_,

.. .r

-

. .

1

.

t

13

.

During the above-noted meetings, the licensee identified a problem in the

instrumentation documentation area.

Their investigation into the tempera-

ture elements revealed a problem in the documentation review process and

with it getting to the vault. The Inspector informed the licensee that,

pending review of the licensee action to resolve the problem of instrumen-

tation documentation not - getting to the vault, this matter will be

identified as Inspector Followup Item 50-424/86-09-03, " Review Licensee

Resolution of Instrumentation Documentation Forwarding to the Vault During

>

Turnover".

Selected portions of the Diesel Generator Building Ventilation system and

the Auxiliary Feedwater Pumphouse Ventilation System were inspected for

as-built configuration as compared to FSAR Sections 9.4.7.5 and 9.4.8.5.

The inspector reviewed the following documents and drawings:

FSAR Section 9.4.7 Diesel Generator Building Ventilation System

-

FSAR Section 9.4.8 Auxiliary Feedsater. Pumphouse Ventilation System

-

'

-

P&ID 1X408217, Rev. 8 Diesel Generator Building HVAC System

P&ID 1X4DB227, Rev. 7 Auxiliary Feedwater Pumphouse HVAC System

'

-

OP's Procedure No.11325, Rev. O AFW Pumphouse and DG Bldg HVAC Normal

-

Alignment

During the inspection, the Inspector noted that the following hand switches

on the Control Room HVAC Control Panel QHVC were labeled as " exhaust" fan

j

whereas the P&ID and the Operations Procedure states " supply" fan.

1-HS-12004

AFW Pumphouse Turbine Driven Pump Rm Supply Fan

-

.

1-1492-B7-003-M01

1

- 1-HS-12050A

D.G. Bldg HVAC Train A Rm Supply Fan 001 1-1566-B7-001-M01

!

- 1-HS-12051A

D.G. Bldg HVAC Train A Rm Supply Fan 003 1-1566-B7-003-M01

!

%

i

1-HS-12053A

D.G. Bldg HVAC Train B Rm Supply Fan 002 1-1566-B7-002-M01-

-

,.<:

- 1-HS-12054A

D.G. Bldg HVAC Train B Rm Supply Fan 004 1-1566-B7-004-M01

This matter will be identified as Inspector Followup Item 50-424/86-09-05,

" Review Licensee Action to Resolve HVAC Handswitch Nomenclature".

1

12.

Reactor Coolant Pressure Boundary and Safety Related Piping Welding -

Unit I and 2 (55073C) (55083C)

!

a.

Welding

Periodic inspections were conducted during daily plant surveillances on

l

safety-related pipe welding at various stages of weld completion. The

i

purpose of the inspection was to determine whether the requirements of.

applicable specifications, codes, standards, work procedures and QC

'

procedures are being met as follows:

1

I

i

'

_ _ _ _ _ _ , _ _ _ , _ _ _ - , _ _ , . _ _ _ _ _ ______--_~.

,

. .-~ . , - - _ . - - - ,

_ ,,

{

.

1.

,

,

14

-

Work was conducted in accordance with a process sheet which

-

identifies the weld and its location by system, references

procedures or instructions, and provides for production and QC

signoffs.

Welding procedures, detailed drawings and instructions, were

-

readily available and technically adequate for the welds being

~

s

made.

Welding procedure specification (WPS) were in accordance with the

'

-

applicable ASME Code requirements and that a Procedure Qualifica-

tion Record (PQR) is referenced and exists for the type of weld

being made.

That the base metals, welding filler materials, flu ~es, gases, and

-

insert materials were of the specified type and grade, have been

properly inspected, tested and were traceable to test reports or

certifications.

That the purge and/or shielding gas flow and composition were as

-

.

specified in the welding procedure specification and that

protection was provided to shield the welding operation from

adverse environmental conditions.

That the weld joint geometry including pipe wall thickness was

-

specified and that surfaces to be welded have been prepared,

cleaned and inspected in accordance with applicable procedures or

instructions.

-

That a sufficient number of adequately qualified QA and QC

inspection personnel were present at the work site, commensurate

with the work in progress.

-

That the weld area cleanliness was maintained and that pipe

N

alignment and fit-up tolerances were within specified units.

That weld filler material being used was in accordance with

-

welding specifications, that unused filler material was separated

from other types of material and was stored in heated cans, and

stubs properly removed from the work location.

,-

That there were no evident signs of cracks, excessive heat input,

sugaring, or excessive crown.

Or.e of the more specific safety-related piping wolding activities

inspected was the Unit 2 Accumulator Tank Loop No. 2 Discharge Valve

(2-HV-88088) weld buildup.

.

. - .

-

-

.-

.

t

15

.

b.

Radiographic Examination

Procedure Review

The inspector reviewed and examined portions of the following procedure

pertaining to radiographic testing to determine that it complies with

'

the applicable codes, standards, NRC Regulatory Guides and licensee-

commitments. The purpose of this review was to determine whether the

radiographic examination procedure contained sufficient information to

-

assure that parameters were specified and controlled within the limits

'

permitted by the applicable code and other additional specification

requirements.

Procedure No,/ Revision

Title

IX-RT-1-W77/5-12-85

Radiographic Procedure IR-192

Butt Welded Pipe Winter 1977

Winter 1977 Addenda

Work Observation

,

!

The inspector observed the performance of radiographic examinations

including processing of the film for the welds listed below.

The

purpose of the inspection was to determine whether the requirements of

applicable

specifications,

codes,

standards,

work

performance

procedures, and QC procedures are being met as follows:

Applicable drawings, instructions, or travelers clearly specify

-

the examination procedure used and that the application of the

technique utilized was appropriate to the circumstance.

Required equipment and materials as specified in the examination

-

procedure was available at the work station.

-

Specific areas, locations and extent of examination was clearly

defined.

-

Examination attributes such as weld surface preparation, density

limitations, film identification, and geometrical unsharpness

limitations were as specified and consistent with the limits or

ranges given in the procedure.

Radiographic film was processed in accordance with the applicable

-

procedure requirements and processed film was free of chemical and

mechanical blemishes which could interfere with interpretation.

,

..

.-.

--- - l- - .-- - -.--

.

-

- - - -

- - - -

- - - - - -

- -

- - -

- .

.

-

.

1

.

16

.

CODE /

ISO NO.

WELD NO. MAT'L.

SIZE

CLASS

STAGE

TECHNIQUE

<

2K3-1208- 491-W-02

SS

4"

ASME/

Final

Doublewall

123-03

Class II

2K3-1208

064-W-03E SS

3"

ASME

Final

Doublewall

064-01

Class II

2K5-1305

055-W-09

CS

16"

ANSI

1/2

Panoramic

-062-01

B31.1

Complete *

2K3-1204

012-W-08R SS

8"

ASME

Final /

Doublewall

-012-01

Class II Repair

  • For information only.

No violations or deviations were identified.

13.

Reactor Vessel and Integrated Head Package - Unit 1 & 2 (50053C)

Periodic Unit 1 inspections consisted of examinations of the Reactor Vessel

installed in containment and the integrated head package stored on the

i

refueling floor in its designated laydown area to determine that proper

storage protection practices were in place, entry of foreign objects and

debris was prevented, and access was controlled.

During the inspection period, the Unit 1 Reactor Vessel Integrated Head

Package was installed on the Reactor Vessel in support of the Reactor

Coolant System Primary Hydrostatic Test.

The Unit 2 inspections consisted of examinations of the Reactor Vessel

installed in containment and the Reactor Vessel head with the installed

control rod drive mechanisms on the refueling floor in its designated

'

laydown area to determine that proper storage protection practices were in

place and that entry of foreign objects and debris was prevented.

Unit 2 Reactor Vessel work inspected consisted of a review of applicable

procedures, drawings, and tre.veler package and observation of work per-

taining to machining the lower radial core supports. The NISCO Traveler

Package (2-42-1, Revision 0, Core Support Machining) which controlled and

documented this work was reviewed by the inspector.

No violations or deviations were identified.

14.

Reactor Vessel Internals - Unit 1 (50063C)

Periodic inspections were conducted during the inspection period of the

upper and lower internals stored in their designated storage areas to

determine that proper storage protection practices were in place, entry of

foreign objects and debris was prevented and access was controlled.

-

_

-

.

_

_ ._

_ _ - _

, _ . - _ .

, _ _ , -

_

.

. _ . _ _

.

_

_.

_ _ _ - . _

.

'

-

,

17

.

During the inspection period the Inspector. observed the installation of the

!

Unit 1 Reactor Vessel Lower Internals in support of the Reactor Coolant

System Primary Hydrostatic Test.

No violations or deviations were identified.

15. Safety Related Components - Units 1 & 2 (50073C)

j

The inspection consisted of plant tours to observe storage, handling, and

protection; installation; and preventive maintenance after installation of

!

safety-related components to determine that work is being performed in

accordance with applicable codes, NRC Regulatory Guides, and licensee

commitments.

During the inspection the below, listed areas were inspected at various

I

times during the inspection period to verify the following as applicable:

Storage, environment, and protection of components were in accordance

-

with manufacturer's instructions and/or established procedures.

-

Implementation of special storage and maintenance requirements such as:

rotation

of

motors,

pumps,

lubrication,

insulation

testing

(electrical), cleanliness,etc.

-

Performance

of

licensee / contractor

surveillance

activities

and

documentation thereof was being accomplished.

-

Installation requirements were met such as: proper location, placement,

orientation, alignment, mounting (torquing of bolts and expansion

anchors), flow direction, tolerances, and expansion clearance.

Appropriate stamps, tags, markings, etc. were in use to prevent

-

oversight of required inspections, completion of tests, acceptance, and

the prevention of inadvertent operation.

Safety-Related piping, valves, pumps, heat exchangers, and instrumentation

were inspected in the following Unit 1 and 2 areas on a random sampling

basis throughout the inspection period:

-

Residual Heat Removal Pump Rooms

-

Diesel Generator Building

-

Containment Spray (CS) Pumps

Auxiliary Feedwater Pumphouse

-

-

Containment Spray Pump Rooms

Pressurizer Rcoms

-

Main Coolant Pump Areas

-

-

Steam Generator Areas

-

Safety Injection Pump Rooms

-

RHR and CS Containment Penetration Encapsulation Vessel Rooms

-

Component Cooling Water (CCW) Heat Exchangers, Surge Tanks and

Pump Rooms

Cable Spreading Rooms

-

-

-

- - .

- ,,

-

-

, . - - . . -

.

- -

.-

--

.

_

- - .

.

.

.

._

.

-

.

r

.

18

-

Accumulator Tank Areas

-

1

Chemical and Volume Control System (CVCS) Letdown Heat Exchanger Rooms

-

Battery & Charger Rooms

-

Nuclear Grade Piping, Valves & Fittings Storage Areas

-

Spent Fuel Pool Heat Exchanger Rooms

>

-

-

Pressurizer Relief Tank Area

CVCS Centrifugal Charging Pumps & Positive Displacement Pump Rooms

-

Bottom Mounted Instrumentation (BMI) Seal Table Area

-

BMI ar.d Supports Under Reactor Vessel

-

-

NSCW Tower Pump Rooms and Pipe Tunnels

No violations or deviations were identified.

16.

Safety Related Pipe Support and Restraint Systems - Units 1 & 2 (50090C)

Periodic random inspections were conducted during the inspection period to

observe construction activities during installation of safety-related pipe

supports to determine that the following work was performed in accordance

'

with applicable codes, NRC Regulatory Guides, and licensee commitments:

Spring hangers were provided with indicators to show the approximate

-

!

" hot" or " cold" position, as appropriate.

'

No deformation or forced bending was evident.

-

Where pipe clamps are used to support vertical lines, shear lugs were

-

,

welded to the pipe (if required by Installation Drawings) to prevent

'

slippage.

-

Sliding or rolling supports were provided with material and/or

lubricants suitable for the environment and compatible with sliding

contact surfaces.

-

Supports are located and installed as specified.

The surface of welds meet applicable code requirements and are free

-

from unacceptable grooves, abrupt ridges, valleys, undercuts, cracks,

discontinuities, or other indications which can be observed on the

welded surface.

-

The inspector conducted a walkdown of the Boron Injection Tank Inlet

and Discharge Piping and the Accumulator Discharge Piping of the Safety

Injection System.

1

.

.

.

.

. .

-

.

.

.

-

.

-

.

-

-

-

-

.

_

_ . . _-

.

.

19

1

-

I

i

,

An inspection of the above attributes was conducted for the following

completed / accepted pipe supports on Unit No. 2:

Pipe Support Dwg No./ Revision

Support Type

!

V2-1208-411-H011, Rev. 4

Pipe Support Assembly

V2-1202-216-H005, Rev. I

Variable Spring

'

V2-1208-411-H014, Rev. 6

Fixed-Pipe Support

V2-1208-095-H019, Rev. 1

Fixed-Pipe Support

V2-1208-411-H019, Rev. 2

Fixed-Pipe Support

No violations or deviations were identified.

17.

Electrical and Instrumentation Components and Systems - Vaits 1 & 2 (51053C)

(52153C)

Periodic inspections were conducted during the inspection period to observe

safety-related electrical equipment in order to verify that the storage,

installation, and preventive maintenance was accomplished in accordance with

applicable codes, NRC Regulatory Guides, and licensee commitments.

During the inspection period an inspection was performed on various pieces

of electrical equipment during storage, installation, ard cable terminating

phase in order to verify the following as applicable:

3

'

Location and alignment

-

i

-

Type and size of anchor bolts

{

-

Identification

l

-

Segregation and identification of nonconforming items

l

-

Location, separation and redundancy requirements

Equipment space heating

-

Cable identification

-

-

Proper lugs used

Condition of wire (not nicked, etc.), tightness of connection

-

Bending radius not exceeded

-

Cable entry to terminal point

-

Separation

-

Unit 1 Electrical Component inspection also consisted of a review of

applicable procedures, drawings, and travel package pertaining to the

Reactor Trip Breaker Replacement Undervoltage Trip Assembly Testing.

The

i

Reactor Trip Breakers are Model No. DS-416.

This modification and testing

-

was conducted by Westinghouse in accordance with their approved QA manual.

.

i

i

'l

4

P

--

- - - - - - - . - ,

.-

.-

- , - - - . .

- - . - -

,m.

-#

3. - - , --- m

-

,-r--

-- , ~ , - +

,

-n

-- , -

- - - .

.

-

-~

_

_

_

e

l

20

-

Procedure and Document Review

The inspector reviewed the following Westinghouse Traveler Package.

-

GAEM-10571-T23, Revision 0

1

Instruction and documentation for the replacement of

Undervoltage Assembly (UV) in the four (4) Reactor Trip

Switchgear Circuit Breakers per drawing IX6A-A19-155

(FCN GAEM-10571) and FEC0 N-68-BF.

Work Observation

The inspector observed the performance of the following steps of the above

procedures on the Train B Rea-tor Trip Breaker Serial No. 02YN0728-4 and the

Train B Reactor Trip Bypass Breaker Serial No. 02YN072B-2:

I

-

Proper interfacing of the UV trip device with the trip bar to ensure

satisfactory trip margin.

-

Breaker closure ard trip by remcving voltage to the UV trip device ten

(10) times to verify satisfactory operation of th: (JV trip device.

-

Trip load check to verify force / load values.

No violations or deviations were identified.

18.

Electrical and Instrumentation Cables and Terminations - Units 1 & 2

(51063C) (52063C)

a.

Raceway / Cable Installation

The inspector reviewed and examined portions of the following

-

procedures pertaining to raceway / cable installation to determine

whether they comply with applicable codes, NRC Regulatory Guices and

licensee commitments.

!

!

-

ED-T-02, Rev. 8 Raceway Installation

[

-

ED-T-07, Rev. 9 Cable Installation

Periodic

inspections

were

conducted to

observe construction

activities of Safety Related Raceway / Cable Installation.

In reference to the raceway installation, the following areas were inspected

to verify compliance with the applicable requirements:

-

Identification

,

-

Alignment

-

Bushings (Conduit)

!

Grounding

-

-

Supports and Anchorages

_

_ __ , - _ _ . _ _ _ _ _ _

_

, _ . - _ .

_-.

.

-

.

.

__

. . . _ _ . . - _

_

-

-

__-

,

-

l

.

21

-

,

In reference to the cable installation the following areas were

inspected to verify compliance with the. applicable requirements:

-

Protection from adjacent construction activities (welding, etc.)

Coiled cable ends properly secured

-

Non-terminated cable ends taped

l

-

i

-

Cable trays, junction boxes, etc., reasonably free of debris

Conduit capped, if no cable installed

-

.

-

Cable supported

Bend radius not exceeded

-

4

-

Separation

b.

Cable Terminations

The inspector reviewed and examined portions of the following proce-

dures pertaining to cable termination to determine whether they comply

with applicable codes,

NRC Regulatory Guides and licensee commit-

ments.

-

ED-T-03, Rev. 7 Cable Termination

In reference to cable terminations the following areas were inspected

to verify compliance with the applicable requirements.

-

Cable identification

-

Proper lugs used

-

Condition of wire (not nicked, etc.), tightness of connection

-

Bending radius not exceeded

-

Cable entry to terminal point

-

Separation

No violations or deviations were identified.

19. Containment and Safety Related Structural Steel Welding - Units 1 and 2

(55053C) (55063C)

Periodic inspections were conducted during daily plant surveillances on

safety-related steel welding at various stages of weld completion.

The

purpose of the inspection was to determine whether the requirements of

applicable specifications, codes, standards, work performance procedures and

QC procedures are being met as follows:

-

Work was conducted in accordance with a process sheet or drawing which

identifies the weld and its location by system, references procedures

or instructions, and provides for production and or signoffs.

Welding procedures, detailed drawings and instructions, were readily

-

available and technically adequate for the welds being made.

i

-=

,

-

,-

.--

.

.n.

, . -

--

.r..

, ,,

,

-,

, ,

-

.

--

..

.

o

22

Welding procedure specification (WPS) were in accordance with the

-

applicable Code requirements and that a Procedure Qualification Record

.

(PQR) is referenced and exists for the type of weld being made.

-

Base metals and welding filler materials were of the specified type and

grade, were properly inspected, tested, and were traceable.

Protection was provided to shield the welding operation from adverse

-

environmental conditions.

-

Weld joint geometry including thickness was specified and that surfaces

to be welded were prepared, cleaned and inspected in accordance with

applicable procedures or instructions.

-

A sufficient number of adequately qualified QC inspection personnel

commensurate with the work in progress were present at the work site.

-

Weld area cleanliness was maintained and that alignment and fit-up

tolerances were within specified units.

-

Weld filler material being used was in accordance with welding

specifications, unused filler material was separated from other types

of material and was stored and controlled properly, and stubs were

properly removed frcm the work location.

-

That there were no visual signs of cracks, excessive heat input, or

excessive crown on welds.

No violations or deviations were identified.

20.

Preoperational Test Program Implementation / Verification - Unit 1 (70302)

(71302)

The inspector reviewed, in part, the implementation of the preoperational

test program. Test program attributer inspected included review of admin-

istrative requirements, document control, documentation of major test events

and deviations to procedures, operating practices, instrumentation calibra-

tions, and correction of problems revealed by testing.

Periodic facility tours were made to assess equipment and plant conditions,

maintenance and preoperational activities in progress.

Schedules for

program completion and progress reports were

routinely monitored.

Discussions with responsible personnel, as they were available, to determine

their knowledge of preoperational program. The Inspector reviewed numerous

operation deviation reports to determine if requirements were met in the

3

areas of documentation, action to resolve, justification, corrective action

and approvals.

Specific observations made included portions of:

,

,

- , , . , - , , - .

-.

,, -~,

-

.,

. - _ , . . . . , .,

,

~,,s.

.,n

,

v.

,,m>

.,a

.,

,,e-

,

, , , _

.

, _ _ - -

-

,

.

.

'

23

,

a.

Flushing Program

System

Auxiliary Feedwater System - Trains A&B Pump Suction Lines

b.

Preoperational Tests

Pre-op Test Procedure

Activity Observed

1-300-03

Primary Hydro Prerequisites

- Internals Installation

- Reactor Coolant System Venting

- Reactor Coolant Pump Start

1-3BC-01

Residual Heat Removal

- Integrated SI (RHR, SI, & CVCS

Pumps) Recirc. Test Briefing

- Integrated SI Injection Into

Cold Leg

Diesel SOI

Train B Diesel Loading to Verify

Governor Operation

No violations or deviations were identified.

21.

Second Corporate Management Meeting - Units 1 & 2 (303018)

On February 13, 1986, a meeting was held onsite with the persons listed

below to further discuss the change in emphasis from construction to the

operations phases. This meeting was conducted as a followup to the first

meeting conducted on August 27, 1985; see NRC Report 50-424/85-37 and

50-425/85-29.

Topics discussed at the meeting included the status and

handling of construction ana preoperational problems prior to unit

licensing, an update on the regulatory process steps in obtaining a license

recommendation from Region II, the regional inspection activity with

emphasis on the preoperational program the startup test, health physics and

emergency preparedness programs. An overview of the NRC Region II organiza-

tion and responsibilities was presented.

l

3

l

[

.

24

.

Attendees

GPC & SCS

A. H. Pinson, Vice President, Vogtle Construction

H. P. Walker, Manager, Unit Operations

A. L. Mosbaugh, Initial Test Program Manager

D. S. Read, Manager, Quality Assurance

A. E. Desrosiers, Superintendent of Health Physics

C. S. Hayes, Vogtle Quality Assurance Manager

C. E. Belflower, Quality Assurance Site Manager - Operations

J. A. Bailey, Project Licensing Manager, Southern Company Services (SCS)

J. L. Leamon, Licensing, SCS

NRC

A. R. Herdt, Branch Chief, Division of Reactor Safety (DRS)

D. M. Collins, Branch Chief, Division of Radiation Safety and Safeguards

F. Jape, Section Chief, Test Program Section (TPS), DRS

M. V. Sinkule, Section Chief, Division of Reactor Projects

J. F. Rogge, Senior Resident Inspector - Operations

H. H. Livermore, Senior Resident Inspector - Construction

G. A. Schnebli, Reactor Inspector, TPS

L. E. Nicholson, Reactor Inspector, TPS

22.

Followup On Headquarters Requests (25014) Units 1 & 2

TI2500/14 (Closed) Solid State Protection System (SSPS) Manual Trip Circuit.

This inspection was performed to determine the electrical location of the

manual trip circuit in relation to output transistors Q3 and Q4. A short-

circuit failure of the output transistors would prevent the automatic

tripping of the associated reactor trip breaker. In this case, the manual trip would have to be utilized to trip the breaker.

By design the manual trip switches should be located between the transistors output and the

undervoltage trip devi:e in the breaker. A recent NRC review indicated that

erroneous controlled schematics showing the manual trip switches before the

transistors could lead to possible wiring errors.

This inspection completes the followup activities as addressed in inspection

report 50-424/85-37 and 50-424/85-29. The inspector observed the licensee

conduct a continuity check of the SSPS vendor wiring to verify proper

circuit configuration for both Train A and B Unit 1 SSPS equipment. The

inspector concluded besed on this demonstration that wiring errors do not

exist for this site.

No violations or deviations were identified.

i

)

)

, _ .

. .

,_ _ . . _ . - - - _ - - _ , _ . _ _ .

._

.. __

.

I'

9

25

23. Atomic Safety and Licensing Board Hearings - Units 1 & 2 (940108)

On March 11 thru 14, 1986, the ASLB conducted hearings on the following

issues:

Contention 7, Groundwater Contamination

Contention 10.1, Dose Rate Effects

Contention 10.5, ASCO Solenoid Valves

The hearings were held at the Burke County Auditorium and were periodically

attended by the following Region II personnel and the resident inspectors:

M. V. Sinkule, Chief, Projects Section 3C

P. W. Jones, Regional Counsel