ML20205A029

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Insp Repts 50-413/86-27 & 50-414/86-30 on 860626-0725. Violations Noted:Failure to Follow Procedure for Corrective Maint & Failure to Provide Adequate Procedure for Valve Operator Maint
ML20205A029
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 08/01/1986
From: Lesser M, Peebles T, Skinner P, Van Doorn P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20205A014 List:
References
50-413-86-27, 50-414-86-30, CAL, NUDOCS 8608110289
Download: ML20205A029 (8)


See also: IR 05000413/1986027

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UNITE 3 STATES

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NUCLEAR REGULATORY COMMISSION

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101 MARIETTA STREET, N.W.

ATI.ANTA, GEORGI A 30323

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Report Nos.

50-413/86-27 and 50-414/86-30

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Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.:

50-413 and 50-414

License Nos.: NPF-35 and NPF-52

Facility Name: Catawba 1 and 2

Inspection Conducted: June 26 - July 251986

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Approved by:

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T. Peeb~les, 5ection Chief

Dat.e Signed

Projects Branch 3

Division of Reactor Projects

SUMMARY

Scope: This routine, unannounced inspection was conducted on site inspecting in

the areas of, review of plant operations (Units 1 & 2); surveillance observation

(Units 1 & 2); maintenance observation (Units 1 & 2); review of licensee

nonroutine event reports (Unit 2); and followup of confirmation of Action Letter

commitments (Units 1 & 2).

Results:

Of the five (5) areas inspected, two (2) apparent violations were

identified, (Failure to follow procedure for corrective maintenance, paragraph

7.b. and Failure to provide adequate procedure for valve operator maintenance,

paragraph 7.c.)

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REPORT DETAIiS

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1.

Licensee Employees Contacted

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J. W. Hampton, Station Manager

H. B. Barron, Operations Superintendent

A. S. Bhatnager, Performance Engineer

  • W. H. Bradley, Quality Assurance

M. J. Brady, Asst. Operating Engineer

S. Brown, Reactor Engineer

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F. Caldwell, Station Services Superintendent

  • J. W. Cox, Superintendent, Technical Services

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T. E. Crawford, Operations Engineer

L. R. Davison, QA Manager Technical Services

B. East, I. & E. Engineer

C. S. Gregory, I. & E. Support Engineer

  • C. L. Hartzell, Compliance Engineer

J. A. Kammer, Performance Test Engineer

.

J. Knuti, Operating Engineer

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  • P. G. LeRoy, Licensing Engineer

W. W. McCollough, Mechanical Maintenance Supervisor

.W. R. McCullum, Superintendent, Integrated Scheduling

C. E. Muse, Operating Engineer

F. P. Schiffley, II, Licensino Engineer

  • G. T. Smith, Maintenance Superintendent
  • J. Stackley, I. & E. Engineer

D. Tower, Operating Engineer

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

  • Attended exit interview.

2.

Exit Interview

The inspection scope and findings were summarized on July 25, 1986, with

those persons indicated in paragraph 1 above. The inspector described the

areas inspected and discussed in detail the inspection findings. 4 No

dissenting comments were received from the licensee. The licensee did not

identify as proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

3.

Licensee Action on Previous Enforcement Matters

(Units 1 & 2) (92701)

(92702)

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This area was not inspected.

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4.

Unresolved Items *

A new unresolved item is identified in paragraph 5.c.

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5.a Plant Operations Review (Units 1 & 2) (71707 and 71710)

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a.

The inspectors ieviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements. Technical

Specifications (TS), and administrative controls. Control room logs,

danger tag logs, Technical Specification Action Item Log, and the

removal and restoration log were routinely reviewed.

Shift turnovers

were observed to verify that they were conducted in accordance with

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approved procedures.

The , inspectors verified by observation and interviews, the measures

taken to assure physical protection of the facility met current

requirements.- Areas inspected included the security organization, the

estab1fshment and maintenances of gates, doors, and isolation zones in

the proper condition, that access control and badging were proper and

procedures followed.

In addition to the areas discussed above, the areas toured were observed

for fire prevention and protection activities.

These included such

things as combustible material control, fire protection systems and

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materials, and fire protection associated with maintenance activities.

Detailed inspections were accomplished for reactor trips occurring on

July 8, 1986 (Unit 2) and July 17, 1986 (Unit 1). The inspectors also

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witnessed startup testing activities associated with Unit 2 including

observation of Loss of Control Room test (TP/2/A/2650/03) on June 27,

1986 and July 11, 1986 and Turbine Trip Test (TP/2/A/2650/07) on

July 23, 1986. The inspectors participated in a special inspection of

the safety injection incident which resulted from the Loss of Control

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test conducted on June 27, 1986.

This inspection is documented in

NRC/RII Report No. 50-413/86-25, 414/86-27. Documentation of followup

of corrective actions related to this incident is contained in

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paragraph 9 below,

b.

On July 9,

1986, the licensee requested a temporary waiver of

compliance with Technical Specifications (TS) which involved an

extension until 8:00 a.m. on July 12, 1986 for the time allowed by TS

Action statement 3/4.6.3 " Containment Isolation Valves".

This waiver

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was made in order to preclude an unnecessary thermal cycle on the

reactor and associated systems.

Following discussions between NRR,

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Region II, the Resident Inspector and the licensee, the waiver was

granted. The licensee subsequently went into the ACTION statement on

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July 12, repaired the valve and returned the valve to operable status

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within the ACTION statement time requirements.

The licensee has

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addressed this issue in a letter to Region II dated July 10, 1986.

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  • An -Unresolved Item is a matter about which more information is required to

determine whether it is acceptabale or may involve a violation.

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c.

On June 22, 1986, an Engineering Safeguards Features (ESF) actuation

occurred.

This ESF actuation was the automatic startup of the

Auxiliary Feedwater (CA) pumps caused by a loss of ' normal feedwater.

During this actuation, CA Train A (CA pump) failed to start, several

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Nuclear Sampling (NM) and Steam Generator Blowdown (BB) valves failed

to close, and valve ICA-46 B in CA Train B failed to close completely.

The licensee identified that the failure of CA Pump to start and the NM

and BB valves to not operate was due to a failure of a Bussman type FNA

fuse. This type of fuse had been identified at McGuire Nuclear Station

(MNS) as a potential problem. A review of this area by the inspector

identified that several failures also had occurred at Catawba. As of

June 26, 1986 a total of twenty (20) fuses were identified as having

failed, e'aven (11) of which were found in the warehouse stock.

These

failures were di gussed with Region II, NRR and the MNS Senior Resident

Inspector in detail. As a result, Region II requested that Duke Power

Company (DPC) perform a more detailed investigation of the reliability

of Bussman FNA type fuses at all their nuclear generating plants. The

Cunfirmation of Action Letter dated July 3,

1986, for Catawba as

discussed in paragraph 9, addresses this issue.

DPC has initiated

discussions with the manufacturer and has commenced a test program to

determine reliability.

In addition, Catawba has commenced performing

weekly visual surveillances to obtain data on failure rates. Pending

the completion of data collection and analysis and review of the

conclusions reached by the licensee and review by the inspector, this

item

is

identified

as

an

Unresolved

Item

413-50/86-27-01,

414-50/86-30-01, Followup of analysis of Bussman type FNA fuses for

reliability.

No violations or deviations were identified.

6.

Surveillance Observation (Units 1 & 2) (61726)

During the inspection period, the inspector verified plant operations were

in compliance with various TS requirements.

Typical of these requirements

were confirmation of compliance with the TS for reactor coolant chemistry,

refueling water tank, emergency power systems, safety injection, emergency

safeguards systems, control room ventilation, and direct current electrical

power sources.

The inspector verified that surveillance testing was

performed in accordance with the approved written procedures, test instru-

mentation was calibrated, limiting conditions for operation were met,

appropriate removal and restoration of the affected equipment was

accomplished, test results met requirements and were reviewed by personrel

other than the individual directing the test, and that any deficiencies

4dentified during the testing were properly reviewed and resolved by

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appropriate management personnel.

No violations or deviations were identified.

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7.

Maintenance Observations (Units 1& 2) (62703)

a.

Station maintenance activities of selected systems and components were

observed / reviewed to ascertain that they were conducted in accordance

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with requirements. The inspector verified licensee conformance to the

requirements in the following areas of inspection: the activities were

accomplished using approved procedures, and functional testing and/or

calibrations were performed prior to returning components or systems to

service; quality control records were maintained; activities performed

were accomplished by qualified personnel; and materials used were

properly certified. Work requests were reviewed to determine status of

outstanding jobs and to assure that priority is assigned to

safety-related equipment maintenance which may effect

system

performance.

b.

During review of Work Requests (WR) the inspector noted that WR No.

21552-OPS was signed off as complete on June 23, 1986.

This WR was

initiated to perform corrective maintenance on Auxiliary Feedwater

Systems (CA) valve ICA46B which had not closed fully as required to

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provide CA pump runout protection on June 22, 1986 during an ESF

actuation (see paragraph 5.c.).

The WR documented that a blown fuse

had been replaced correcting the condition which prevented the valve

from closing. A review of the electrical schematic by the inspector

disclosed that the electrical design of the valve included a lock-in

circuit which should have allowed the valve to go full closed once the

close signal had been received. The licensee was requested to review

this problem further and discovered that the valve operator did not

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have the torque setting required by design.

Licensee Maintenance

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Management Procedure

1.0,

Work Request Preparation Section 4.10

requires the job supervisor to sign approval of a WR if the problem

identified has been resolved and expected results are produced.

Therefore, this item is a violation of TS 6.8.1 which requires licensee

procedures to be followed. This is Violation 413/86-27-02: Failure to

follow procedure for corrective maintenance.

e.

Further review of the problem identified in paragraph 7.b. above was

conducted by the licensee at the request of the inspector. This review

disclosed that the licensee procedure for maintenance of Rotork valve

actuators, Ip/0/A/3820/11, Certification of Rotork Valve Actuators, was

inadequate in that it referenced rated torque valves for valve

actuators rather than required torque valves for the individual

applications. This resulted in certain actuators which were required

to have torque settings greater than the rated value being replaced

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without proper recertification of torque settings.

This further

resulted in Valve Nos. ICA46B, CA pump runout protection valve and

INV158, Chemical

and Volume Control System letdown containment

isolation valve being undertorqued and not being able to close under

all postulated conditions.

Licensee evaluation of these conditions

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indicated that these problems did not represent a serious safety

concern.

These evaluations are documented in licensee memoranda

H. E. Edwards to A. P. Cobb dated July 18, 1986 and July 16, 1986.

This item violates 10 CFR 50, Appendix B, Criterion V which requires

procedures to include appropriate quantitative acceptance criteria.

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This 1, violation 413/86-27-03: Failure t.o provide adequate procedure

for valve operator maintenance.

Two violations were identified as described in paragraphs 7.b. and 7.c.

No

deviations were identified.

8.

Review of Licensee Nonroutine Event Reports (Unit 2) (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine if

the information provided met NRC requirements. The determination included:

adequacy of description, verification of compliance with Technical

Specifications and regulatory requirements, corrective action taken,

existence of potential generic problems, reporting requirements satisfied,

and the relative safety significance of each event.

Additional inplant

reviews and discussion with plant personnel, as appropriate, were conducted

for those reports indicated by an (*).

The following LERs are closed:

  • LER 414/86-13, Rev.1

Rx Trip due to Failure of Reverse

Purge Flow Valve

  • LER 414/86-14

Manual Rx Trip due to Turbine

Trip on Hi-Hi S/G Level

  • LER 414/86-15

R Trip due to S/G Level Control

Instability

  • LER 414/86-16

Main Feedwater Isolation due to

Overfeed of Steam Generator

  • LER 414/86-18

Main Feedwater Isolation due to

Steam

Generator

Level

Control

Instability

LER 414/86-19

Main Feedwater Isolation due to

Overfeeding of a Steam Generator

No violations or deviations were identified.

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9.

Confirmation of Action Letter Followup (Units 1 & 2) (92703)

A Confirmation of Action Letter (CAL) was issued July 3,1986 concerning the

transient which occurred at Catawba Unit 2 on June 27, 1986 (see Inspection

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Report 50-413/86-25, 50-414/86-27). All actions associated with item 1 of

this CAL were to be completed prior to proceeding above Mode 3 for Units 1

and 2, as applicable.

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Action 1.a. required the licensee to review and understand the root cause

and sequence of events associated with the transient.

The licensee

completed an in depth review of this event.

This was documented in a

" transient cycle" report written on July 6, 1986.

The inspectors reviewed

this report in detail and also discussed the event with licensee management.

The inspectors concluded that the licensee has completed this action item.

Action item 1.b. required the licensee to review functional controllers on

the main control panels (MCP), Auxiliary Shutdown Panels (ASP), and the

Turbine Driven Auxiliary Feedwater Pump Control Panel (TDAFWPCP) with

respect to valve position, nomenclature, units of measure and correct

labeling and that changes made would be incorporated into procedures and

training.

This review was conducted for Units 1 and 2 and various changes

made to the panels. The inspectors reviewed these changes, the procedures

affected and training.

The inspectors concluded that the licensee has

completed this action item.

Action 1.c. required the licensee to conduct a review of all safety-related

circuits where Bussman FNA type fuses are used and where the failure of the

fuse would result in an undetected component malfunction such that the

components safety-related function would not be performed. The licensee was

allowed to perform a weekly visual surveillance on these fuses until

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sufficient data could be obtained and analyzed. The inspector reviewed the

licensees program to accomplish this data collection and participated in the

surveillance process.

Also the results of the initial inspection was

reviewed by the inspectors. This action was taken for both units 1 and 2.

The inspectors concluded that the licensee has conducted the initial review

and is performing weekly surveillances as specified by this action item.

Action item 1.d. was a requirement to train all licensed operators and Shirt

Technical Advisors on this event and the changes to procedures and panels as

a result of this CAL.

The inspectors reviewed the training plan and

witnessed several sessions of the training presentations.

Based on this

review, the inspectors concluded that the licensce has satisfied this action

item.

Action item 1.c.

specified that the licensee would correct all hardware

malfunctions that occurred during this event.

The hardware malfunctions

were corrected and appropriate retesting performed. The inspectors reviewed

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the documentation associated with this work and considered this item to be

complete.

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Action item 1.f. required changes to procedures for initiation of a safety

Jnjection during operation from the ASP.

The inspectors reviewed these

procedures for Units 1 and 2 and consider this action to De complete.

Action item 1.g. required the licensee to provide additional controls over

startup activities, to include additional prior review of test procedures

and additional personnel training.

The licensee implemented additienal

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controls and training.

These controls and the associated training were

reviewed by the inspectors and discussed v.ith Region II management. The

action taken by the licensee .is considered acceptable and this item is

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complete.

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Action item 2 was to satisfactorily complete the Loss of Control Room Test

prior to Unit 2 exceeding 30% power. This test was performed on July 11,

1986 with no abnormal problems.

Prior to proceeding above Mode 3, the actions taken by the licensee in

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response to the CAL and the reviews conducted by the inspectors were

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discussed in detail with Regien II management.

No violations or deviations were identified.

10.

Previously Identified Inspector Findings (Unit 2) (92701)

(CLOSED) Inspector Followup Item 414/84-08-02: Evaluate Feedback from TSC to

Control Room and OSC.

This item is closed based on previous inspections

documented in Report No. 50-414/86-10.

No violations or deviations were identified.

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