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- g Pw. aqs u.s. NUCLEAA REGULATORY -
APMIOVEO Oma NO. 3198 4104 i
LICENSEE EVENT REPORT (LER) 8xma's: 8'8U8' PACILITV NARAE 11, DOCKET NutABER (2)
PAGE(31 Nine Mile Point Unit 2 o 15 t o Io I o I 41110 1 lOFl 013 TITLE 144 Standby Gas Initiation - High Radiation Signal EVENT OATE Ill LER seveABER 181 REPORT OATE (71 OTHER PACILITIES INVOLVED 10)
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y N/A o 15101010 1 I I 1l1 2! 7 86 8l6 0l 1l 1 0l1 0l3 1l 8 8l 7 N/A oi 5 1 0 1 0 loi l I OPERATisse TMa$ REPORT IS BusaniTTED PURSUANT TO THE REQUIREMENTS OF 10 CPR 9: tChac* oao or ore e, er,e,os,ourmet 111)
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NAME TELEPHONE NUMSER AREA CODE Robert G. Randall. Supervisor Technical Support 3l 11 5 a 419l -l 21 4 1 45 1
CAAPLETE ONE LINE POR EACH COMPONENT P AILURE DESCE.*EO IN TMit REPORT (13)
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..- - n.,,n Automatic initiation of the Standby Gas Treatment System divisions I & II occurred on November 27,1986 at 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br /> and on December 8,1986 at 1442 hours0.0167 days <br />0.401 hours <br />0.00238 weeks <br />5.48681e-4 months <br />.
Initiation was caused by spurious Reactor Building exhaust ventilation duct high radiation signals. A root cause analysis has been completed per procedure S-SUP-1, " Root Cause Analysis Program".
Testing and investigations have isolated the following design deficiencies of electrical and mechanical components in the process radiation monitoring cabinets:
1.
A high frequency pressure variation in the sample lines.
2.
A low set point for the differential pressure switches.
3.
Ground Ioops.
4.
Externally mounted power transistors picking up electrical noise.
The corrective actions taken are as follows:
1.
Addition of accumulator in the sample lines.
2.
The set point for the dif ferential pressure switches was increased.
3.
thdesirable grounds were removed.
4.
A modification request has been initiated to shield the externally mounted transistors.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION maovEo ove =o uso-oio4 umRes; eesim FACluTY NAME (1)
DOCKET NUMBER (2)
LER NUMGER lel PAGE133 MN, ' '
.(Ejgh" vEAR Nine Mile Point Unit 2 o l5 lo lo lo l4 l 110
$6 01111 Q1 Q2 0F 0l3 TEXT (# mswo ansce e segurent war admeener MC Form Jme's1(17)
I.
DESCRIPTION OF EVENT
On Novenber 27,1986 at 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br /> and on December 8,1986 at 1442 hours0.0167 days <br />0.401 hours <br />0.00238 weeks <br />5.48681e-4 months <br /> with the mode switch in the shutdown position, the Nine Mile Point NJclear Station #2 experienced automatic initiation of the Standby Gas Treatment System divisions I and II.
These initiations were caused by spurious high radiation signals being transmitted from Radiation Monitoring Sample Cabinets 2HVR*328 (below refueling floor monitor) and 2HVR*148 (above refueling floor monitor).
II.
CAUSE OF EVENT
A root cause tnalysis has been completed per procedure S-SUP-1, ' Root Cause Analys is Program".
Testing and investigations have isolated the following design deficiencies of electrical and mechanical components in the process radiation monitoring cabinets:
1.
A high frequency pressure variation in the sample lines due to pump design was causing degradation of the charcoal filters.
2.
The set point for the pressure differential switches was too low resulting in frequent occurrences where the switch would hum or chatter as the set point was being approached introducing significant noise levels on the power supply of the microprocessor. The noise was resulting in spurious high radiation signals.
3.
Oscilloscope readings revealed die presence of significant ground loops which induce noise into process signal cabling typically resulting in spurious high radiation signals.
4.
Externally mounted power transistors on the microprocessors were picking up electrical noise and contaminating the power supply.
III.
ANALYSIS OF EVENT
This event is reportable per 10 CFR 50.73 part (a) (2) (iv) automatic actuation l
of any B1gineered Safety Feature.
The design basis of the Standby Gas Treatment System is to limit the release of radioactive gases from the reactor building to the environment within the guidelines of 10 CFR 100 in the event of a Loss of Cooling Accident (LOCA) and to maintain a negative pressure in the Reactor Building under accident conditions.
Since the Engineered Safety Feature initiated and functioned per design, there were no adverse safety consequences and would not have been even in a design basis accident circumstance.
The Secondary Containment Veltilation System was in normal operating condition within five hours for the 11/27/86 event and within two hours for the 12/8/86 event.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AP,Rovfo OuS mo. siso-em f.XPtRES: 8/31/m F ACILITV NAast Itl DOCKET NUMSER G3 LgR NUMSER ($1 PAGE(33 SE N,{,... "8y 18,y,"
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I V.
CORRECTIVE ACTION
1.
Modification PN2Y86MX153 has been completed which adds a transient pressure accumulator between the sample pump and the charcoal filters (reference Sketch #1) for six category I process radiation monitor cabinets (2HVR* CAB 14A, B, 32A, B, and 2 CMS
- CAB 10A, B). This has greatly reduced charcoal filter degradation. A modification request (Issue
- I20045) has been initiated for the balance of the cabinets.
2.
The alarm set point for the filter differential pressure switches was increased on all cabinets experiencing " chattering" to mitigate the effects of noise level produced by the switch on the power supply of the microprocessor.
3.
The undesirable grounds from the shield on process signal cables for all category I process radiation monitor cabinets have been removed per modification PN2Y86MX145.
4.
A modification request (Issue #I20046) has been initiated to shield the externally mounted power transistors on the microprocessors.
V.
ADDITIONAL INFORMATION
Identification of Components Referred to in this LER IEEE 803 IEEE 805 Component EIIS Funct System ID Standby Gas Treatment Systems N/A BH Sample Cabinet CAB IL Radiation Monitors MON IL Filter (on cabinet)
FLT IL Accumulator ACC IL Secondary Containment Ventilation System N/A VA Pressure differential switch PDS IL Power Supply RJX IL There are no previous similar events.
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g IMP 23836 NAGARA MOH AWK POWER CORPORATION
^ NIAGARA MOHAWK SYRACUSE,NY 13212
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March 18,'1987'
- - thited States telear Regulatory Commission Document Control Desk Washington, DC 20555 RE:
- - Docket No. 50-410 LER 86-11 Supplement 1 Gen tlemen:
In_ accordance.with 10 CFR 50.73, we hereby submit the following Licensee Event Report:
LER 86-11 Which is being submitted in accordance with 10 CFR 50.73 Supplement 1 (a) (2) (iv), "Any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS).
However, actuation of an ESF, including the RPS, that:
resulted from and was part of the preplanned sequence during
' testing or reactor operation need not be' reported."
A telephone notification was made at 0700 hours on Noverrber 27,1986, and at 1442 on December 8,1986 per'10 CFR 50.72 part -(b) (2) (iv).
This report was completed in the format designated in NtRES-1022, Supplement No. 2, dated September 1985.
Very truly yours,,
+744_.-
Thomas E. Lempges Vice President mclear Generation TEL/DRG/mjd
- Attachments cc:
Regional Administrator, Region 1 Senior Resident Inspector, W. A. Cook i
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| 05000220/LER-1986-001, :on 860118,original Calculations for Jet Impingement Loading on ECCS Isolation Valves Found in Noncompliance W/Fsar.Caused by Break Inside Guard Pipe. Isolation Valves Will Be Replaced |
- on 860118,original Calculations for Jet Impingement Loading on ECCS Isolation Valves Found in Noncompliance W/Fsar.Caused by Break Inside Guard Pipe. Isolation Valves Will Be Replaced
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i) | | 05000410/LER-1986-001-01, :on 861105,two Reactor Scrams Occurred During Initial Fuel Loading.Caused by Spike on Intermediate Range Monitor D & High Level Scram Discharge Trip.Operator Training Mod Submitted |
- on 861105,two Reactor Scrams Occurred During Initial Fuel Loading.Caused by Spike on Intermediate Range Monitor D & High Level Scram Discharge Trip.Operator Training Mod Submitted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-002-01, :on 861104,four Source Range Monitors (Srms) Downscale Channels Placed in Bypassed State When Jumpers Installed to Clear SRM Downscale Rod Blocks.Caused by Human Error & Procedure Deficiency.Procedure Revised |
- on 861104,four Source Range Monitors (Srms) Downscale Channels Placed in Bypassed State When Jumpers Installed to Clear SRM Downscale Rod Blocks.Caused by Human Error & Procedure Deficiency.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-002, :on 860201,radioactive Gaseous Effluent Monitoring Sys Stack Gas Sample Pump 1 Tripped.Caused by Failed Board in Microprocessing Unit.Board Replaced |
- on 860201,radioactive Gaseous Effluent Monitoring Sys Stack Gas Sample Pump 1 Tripped.Caused by Failed Board in Microprocessing Unit.Board Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-003, :on 860308,attempt to Reset HPCI Following Manual Trip of Turbine Failed Because Contacts for Emergency Governor Limit Switch Did Not Change State.Caused by Stuck Plunger Assembly.Work Request Initiated |
- on 860308,attempt to Reset HPCI Following Manual Trip of Turbine Failed Because Contacts for Emergency Governor Limit Switch Did Not Change State.Caused by Stuck Plunger Assembly.Work Request Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-003-01, :on 861108,partial Loss of Secondary Containment Isolation Actuation Instrumentation Occurred. Caused by Personnel Error.Training Mod Recommendation Initiated |
- on 861108,partial Loss of Secondary Containment Isolation Actuation Instrumentation Occurred. Caused by Personnel Error.Training Mod Recommendation Initiated
| | | 05000220/LER-1986-004, :on 860308,w/unit Shut Down for Refueling,High Reactor Water Level Signal Resulted in Turbine Trip Signal, Causing Feedwater Control Sys Transfer to HPCI Mode. Procedural/Hardware Changes Being Considered |
- on 860308,w/unit Shut Down for Refueling,High Reactor Water Level Signal Resulted in Turbine Trip Signal, Causing Feedwater Control Sys Transfer to HPCI Mode. Procedural/Hardware Changes Being Considered
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-004-01, :on 861109,unit Experienced Two Full Scrams W/Mode Switch in Refuel.Caused by Faulty Circuit Card.Root Cause Unknown But Random Infant Mortality Suspected.Circuit Card Replaced |
- on 861109,unit Experienced Two Full Scrams W/Mode Switch in Refuel.Caused by Faulty Circuit Card.Root Cause Unknown But Random Infant Mortality Suspected.Circuit Card Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-005, :on 860402,during Shutdown for Refueling,Full Scram Experienced.Caused by Loss of Power to Reactor Protection Sys Bus II Due to Deenergization of Brown Boveri ITE-27 Relay.Relay Repaired or Replaced |
- on 860402,during Shutdown for Refueling,Full Scram Experienced.Caused by Loss of Power to Reactor Protection Sys Bus II Due to Deenergization of Brown Boveri ITE-27 Relay.Relay Repaired or Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-005-01, :on 861105,source Range Monitor Channel C Erroneously Left in Bypass Position Following Surveillance Check.Caused by Failure of Operator to Adhere to Procedure. Procedure Revised & Staff Counseled |
- on 861105,source Range Monitor Channel C Erroneously Left in Bypass Position Following Surveillance Check.Caused by Failure of Operator to Adhere to Procedure. Procedure Revised & Staff Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-006, :on 860409,discovered That One of four-inch Sample Lines to Header Completely Plugged.Caused by Pebbles Washed Off Reactor Bldg Into Roof Drains.Roof Drain Screens Will Be Installed |
- on 860409,discovered That One of four-inch Sample Lines to Header Completely Plugged.Caused by Pebbles Washed Off Reactor Bldg Into Roof Drains.Roof Drain Screens Will Be Installed
| | | 05000410/LER-1986-006-01, :on 861112,Tech Spec Hourly Fire Watch Patrol Surveillance Requirements Exceeded Twice.Caused by Cognitive Personnel Errors.Fire Dept Personnel Trained in Tech Spec Requirements & Patrol Methods Revised |
- on 861112,Tech Spec Hourly Fire Watch Patrol Surveillance Requirements Exceeded Twice.Caused by Cognitive Personnel Errors.Fire Dept Personnel Trained in Tech Spec Requirements & Patrol Methods Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000410/LER-1986-007-01, :on 861120,two Electrical Protection Assemblies Spuriously Tripped,Resulting in Loss of Power to safety- Related Control Circuit.Root Cause Evaluation Will Be Performed |
- on 861120,two Electrical Protection Assemblies Spuriously Tripped,Resulting in Loss of Power to safety- Related Control Circuit.Root Cause Evaluation Will Be Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-007, :on 861120,ESF Actuation Occurred.Caused by Two Electrical Protection Assemblies (Epas) Tripping Twice in 2 H Causing Loss of Power to Circuit Bus Due to Personnel Error During MSIV Testing.Epas Reset |
- on 861120,ESF Actuation Occurred.Caused by Two Electrical Protection Assemblies (Epas) Tripping Twice in 2 H Causing Loss of Power to Circuit Bus Due to Personnel Error During MSIV Testing.Epas Reset
| | | 05000220/LER-1986-007, :on 860415,during Refueling Outage Acurex Fuel Zone Level Indication Instrumentation Found Inaccurate by 15 to 20 Inches in Nonconservative Direction.Ge to Correct Software & Acurex Instrumentation Recalibr |
- on 860415,during Refueling Outage Acurex Fuel Zone Level Indication Instrumentation Found Inaccurate by 15 to 20 Inches in Nonconservative Direction.Ge to Correct Software & Acurex Instrumentation Recalibr
| 10 CFR 50.73(a)(2)(1) | | 05000220/LER-1986-008, :on 860422,reactor Bldg Emergency Ventilation Sys Initiated Due to Undervoltage Condition on Instrument & Control Bus 30.Caused by Loss of Backfeed from Plant Switchyard.Investigation Continuing |
- on 860422,reactor Bldg Emergency Ventilation Sys Initiated Due to Undervoltage Condition on Instrument & Control Bus 30.Caused by Loss of Backfeed from Plant Switchyard.Investigation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-008-01, :on 861117,discovered Potential Breaches in Fire Barriers During Control Rod Testing.Caused by Failure to Seal Penetrations.Fire Watches Established & Penetrations Sealed |
- on 861117,discovered Potential Breaches in Fire Barriers During Control Rod Testing.Caused by Failure to Seal Penetrations.Fire Watches Established & Penetrations Sealed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000410/LER-1986-008, :on 861117,discovered Potential Breaches in safety-related Fire Barriers.Caused by Contractor Failure to Follow Established Procedures for Identifying Incomplete Const Work.Breaches Sealed |
- on 861117,discovered Potential Breaches in safety-related Fire Barriers.Caused by Contractor Failure to Follow Established Procedures for Identifying Incomplete Const Work.Breaches Sealed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000410/LER-1986-009, :on 861124,reactor Bldg Ventilation Exhaust Damper 2HVR*AOD9B Closed Initiating Standby Gas Treatment Train A.Caused by Jumper Which Fell & Shorted to Ground. Alternate Installation Methods Under Review |
- on 861124,reactor Bldg Ventilation Exhaust Damper 2HVR*AOD9B Closed Initiating Standby Gas Treatment Train A.Caused by Jumper Which Fell & Shorted to Ground. Alternate Installation Methods Under Review
| | | 05000410/LER-1986-010-01, :on 861123,25% of Control Rods Received Full Scram Signal When All Group 2 Control Rod Solenoid Valves de-energized.Cause Undetermined.Investigation in Form of Supervisory Procedure S-SUP-1 Begun |
- on 861123,25% of Control Rods Received Full Scram Signal When All Group 2 Control Rod Solenoid Valves de-energized.Cause Undetermined.Investigation in Form of Supervisory Procedure S-SUP-1 Begun
| | | 05000410/LER-1986-010, :on 861123,25% of Control Rods Received Full Scram Signal When Group 2 Control Rod Scram Solenoid Valves Deenergized.Cause Not Positively Determined.Training Mod Request Will Be Issued.Procedures Revised |
- on 861123,25% of Control Rods Received Full Scram Signal When Group 2 Control Rod Scram Solenoid Valves Deenergized.Cause Not Positively Determined.Training Mod Request Will Be Issued.Procedures Revised
| | | 05000220/LER-1986-010, :on 860505,reactor Bldg Emergency Ventilation Sys Initiation & Isolation of Normal Reactor Bldg Ventilation Occurred.Caused by Blown Fuse in Control Circuit in Reactor Protection Sys Bus 11 |
- on 860505,reactor Bldg Emergency Ventilation Sys Initiation & Isolation of Normal Reactor Bldg Ventilation Occurred.Caused by Blown Fuse in Control Circuit in Reactor Protection Sys Bus 11
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-011, :on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Divs I & II Occurred.Caused by Spurious Reactor Bldg Exhaust Ventilation Duct High Radiation Signals.Accumulator Added to Lines |
- on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Divs I & II Occurred.Caused by Spurious Reactor Bldg Exhaust Ventilation Duct High Radiation Signals.Accumulator Added to Lines
| | | 05000220/LER-1986-011, :on 860508,contractor Received Contaminated Injury to Hand from Cut Section of Piping.Caused by Personnel Error.Medical Attention Administered & Radiation Exposure Survey Conducted |
- on 860508,contractor Received Contaminated Injury to Hand from Cut Section of Piping.Caused by Personnel Error.Medical Attention Administered & Radiation Exposure Survey Conducted
| | | 05000410/LER-1986-011-01, :on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Div I & II Occurred.Caused by Reactor Bldg Refuel Area Exhaust Ventilation Duct Radiation High Signal |
- on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Div I & II Occurred.Caused by Reactor Bldg Refuel Area Exhaust Ventilation Duct Radiation High Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-012, :on 860516,both Fire Pumps Taken Out of Svc to Allow Diver to Work in Station Svc Water Intake Tunnel. Telephone Notification to Region I Not Made Until 860517. Personnel Counseled |
- on 860516,both Fire Pumps Taken Out of Svc to Allow Diver to Work in Station Svc Water Intake Tunnel. Telephone Notification to Region I Not Made Until 860517. Personnel Counseled
| | | 05000410/LER-1986-012, :on 861128 & 29,series of Related Automatic Initiations of Standby Gas Treatment Sys Occurred.Caused by Clogged Filters & Personnel Error.Approx 50% of First Stage Filters Replaced & Training Mod Initiated |
- on 861128 & 29,series of Related Automatic Initiations of Standby Gas Treatment Sys Occurred.Caused by Clogged Filters & Personnel Error.Approx 50% of First Stage Filters Replaced & Training Mod Initiated
| 10 CFR 50.73(a)(2) | | 05000410/LER-1986-012-01, :on 861128 & 29,automatic Initiation of Standby Gas Treatment Sys Divs I & II & Emergency Recirculation Subsystem of Secondary Containment Ventilation Sys Occurred. Caused by Supply Fan Trip |
- on 861128 & 29,automatic Initiation of Standby Gas Treatment Sys Divs I & II & Emergency Recirculation Subsystem of Secondary Containment Ventilation Sys Occurred. Caused by Supply Fan Trip
| 10 CFR 50.73(a)(2) | | 05000220/LER-1986-013, :on 860518,reactor Bldg Emergency Ventilation Sys Initiated Due to Blown Fuse.Caused by Damaged Timer Relay.Timer Repaired,Fuse Replaced & Sys Returned to Svc.W/ |
- on 860518,reactor Bldg Emergency Ventilation Sys Initiated Due to Blown Fuse.Caused by Damaged Timer Relay.Timer Repaired,Fuse Replaced & Sys Returned to Svc.W/
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-014-01, :on 861203,scram Experienced to one-quarter of Control Rods During Recovery from Earlier Scram & Containment Isolation.Caused by Personnel Error.Addl Licensed Operator Training Requested |
- on 861203,scram Experienced to one-quarter of Control Rods During Recovery from Earlier Scram & Containment Isolation.Caused by Personnel Error.Addl Licensed Operator Training Requested
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-014, :on 860603,reactor Scram Occurred During Surveillance Test.Caused by Instantaneous Inlet of Water in Transmitter RE-16B.Surveillance Test Will Be Revised & Technicians Cautioned |
- on 860603,reactor Scram Occurred During Surveillance Test.Caused by Instantaneous Inlet of Water in Transmitter RE-16B.Surveillance Test Will Be Revised & Technicians Cautioned
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-015, :on 860530,reactor Scram Occurred,Initiating Reactor Bldg Emergency Ventilation.Caused by Lifted Neutral Leg of Output Protective Relaying Circuit.Lifted Lead Replaced & Reactor Scram Reset |
- on 860530,reactor Scram Occurred,Initiating Reactor Bldg Emergency Ventilation.Caused by Lifted Neutral Leg of Output Protective Relaying Circuit.Lifted Lead Replaced & Reactor Scram Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-015-01, :on 861203,reactor Scram Occurred While in Shutdown Mode.Caused by Reactor Protection Sys Power Supplies Inadvertently Cross Connected,Resulting in Loss of Power.Design Change Built Into MSIV |
- on 861203,reactor Scram Occurred While in Shutdown Mode.Caused by Reactor Protection Sys Power Supplies Inadvertently Cross Connected,Resulting in Loss of Power.Design Change Built Into MSIV
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-016, Informs That Condition Reported in LER 86-016 Re Incorrect Location of Flow Switches in Standby Gas Treatment Sys Could Create Substantial Safety Hazard & Also Reportable Per 10CFR21 | Informs That Condition Reported in LER 86-016 Re Incorrect Location of Flow Switches in Standby Gas Treatment Sys Could Create Substantial Safety Hazard & Also Reportable Per 10CFR21 | | | 05000410/LER-1986-016-01, :on 861207 & 08,during Surveillance Procedure, Filter Train Heaters Intermittently Deenergized on Low Flow Signal.Caused by Flow Switch Design Deficiency.Sensing Line Relocated |
- on 861207 & 08,during Surveillance Procedure, Filter Train Heaters Intermittently Deenergized on Low Flow Signal.Caused by Flow Switch Design Deficiency.Sensing Line Relocated
| 10 CFR 50.73(a)(2) | | 05000220/LER-1986-016, :on 860523,Channel 11 High Reactor Water Level Feedwater Pump Trip Found Inoperable Until Feedwater Flow Control Valve 11 Opened Approx 50%.Jumpers Installed to Bypass Flow Control Valve Position Contacts |
- on 860523,Channel 11 High Reactor Water Level Feedwater Pump Trip Found Inoperable Until Feedwater Flow Control Valve 11 Opened Approx 50%.Jumpers Installed to Bypass Flow Control Valve Position Contacts
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000220/LER-1986-017, :on 860615,reactor Scram Occurred.Caused by Reactor Low Water Level Setpoint Being Reached During Operator Surveillance Test for Automatic Startup of HPCI Mode of Feedwater Sys |
- on 860615,reactor Scram Occurred.Caused by Reactor Low Water Level Setpoint Being Reached During Operator Surveillance Test for Automatic Startup of HPCI Mode of Feedwater Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-018-01, :on 861216,while Testing Off Normal Status Sys Isolators,Electrician Placed Jumpers from 120-volt Dc Source to 120-volt Ac Line Source,Resulting in Blown Fuse.Caused by Test Engineer Error.Engineer Disciplined |
- on 861216,while Testing Off Normal Status Sys Isolators,Electrician Placed Jumpers from 120-volt Dc Source to 120-volt Ac Line Source,Resulting in Blown Fuse.Caused by Test Engineer Error.Engineer Disciplined
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-018, :on 860618,reactor Scram Occurred Due to Inventory Requirements Exceeding Capability of Condensate & Feedwater Booster Pumps.Caused by Operator Error.Event Reviewed W/Operating Personnel |
- on 860618,reactor Scram Occurred Due to Inventory Requirements Exceeding Capability of Condensate & Feedwater Booster Pumps.Caused by Operator Error.Event Reviewed W/Operating Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-019-01, :on 861215,reactor Scram Signal on Scram Discharge Vol Received Following Preplanned Scram.Caused by Operator Failure to Adhere to Scram Recovery Procedure. Procedure Revised.Training Mod Recommended |
- on 861215,reactor Scram Signal on Scram Discharge Vol Received Following Preplanned Scram.Caused by Operator Failure to Adhere to Scram Recovery Procedure. Procedure Revised.Training Mod Recommended
| | | 05000220/LER-1986-019, :on 860618,control Rods Moved While Rod Worth Minimizer Inoperable.Caused by Software Problem in Minimizer Program.Plant Shut Down.Indexing Problem in Computer Software Corrected |
- on 860618,control Rods Moved While Rod Worth Minimizer Inoperable.Caused by Software Problem in Minimizer Program.Plant Shut Down.Indexing Problem in Computer Software Corrected
| | | 05000410/LER-1986-020-01, :on 861218,Div 1 ECCS Initiation Experienced Due to Spurious High Drywell Pressure Signal.Caused by Electricians Replacing Relay.Electrical Maint Training Initiated |
- on 861218,Div 1 ECCS Initiation Experienced Due to Spurious High Drywell Pressure Signal.Caused by Electricians Replacing Relay.Electrical Maint Training Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-020, :on 860618,during Startup from Refueling Outage,Pinhole Leak Discovered in newly-installed 3/4-inch Sample Line Outside Primary Containment.Caused by Flaw in Pipe.Line Disconnected,Capped & Tested |
- on 860618,during Startup from Refueling Outage,Pinhole Leak Discovered in newly-installed 3/4-inch Sample Line Outside Primary Containment.Caused by Flaw in Pipe.Line Disconnected,Capped & Tested
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000220/LER-1986-021, :on 860619,reactor Scram & HPCI Initiation Occurred.Caused by Fuse Pulled During Replacement of Relay for intermediate-range Monitor.Scram & HPCI Initiation Signals Reset |
- on 860619,reactor Scram & HPCI Initiation Occurred.Caused by Fuse Pulled During Replacement of Relay for intermediate-range Monitor.Scram & HPCI Initiation Signals Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-021-01, :on 861210 & 11,HPCS Sys Initiation Experienced Due to lo-lo Water Level Signal.Caused by Inadvertent Movement of 4 Ft Section of Flexible Steel Piping Creating Hydraulic Surges.Steel Plate Removed from Rack |
- on 861210 & 11,HPCS Sys Initiation Experienced Due to lo-lo Water Level Signal.Caused by Inadvertent Movement of 4 Ft Section of Flexible Steel Piping Creating Hydraulic Surges.Steel Plate Removed from Rack
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-022-01, :on 861222,Div I-III Diesel Generators Declared Inoperable During Simultaneous Draining of Day Tank During Chemistry Surveillance Test.Caused by Procedure Deficiency. Procedure Revised.Personnel Counseled |
- on 861222,Div I-III Diesel Generators Declared Inoperable During Simultaneous Draining of Day Tank During Chemistry Surveillance Test.Caused by Procedure Deficiency. Procedure Revised.Personnel Counseled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000410/LER-1986-023-01, :on 861223,inoperable Fire Detector Discovered During Routine Insp.Caused by Personnel Removing Detector from Base Prior to Replacement,Per 861222 Work Request. Surveillance Procedure Will Be Developed |
- on 861223,inoperable Fire Detector Discovered During Routine Insp.Caused by Personnel Removing Detector from Base Prior to Replacement,Per 861222 Work Request. Surveillance Procedure Will Be Developed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-023, :on 860801,discovered Failure to Perform Radiation Protection & Fire Dept Surveillance Tests During 850319-1216.Caused by Personnel Error.Personnel Advised of Tech Spec Requirements & Staff Increased |
- on 860801,discovered Failure to Perform Radiation Protection & Fire Dept Surveillance Tests During 850319-1216.Caused by Personnel Error.Personnel Advised of Tech Spec Requirements & Staff Increased
| 10 CFR 50.73(a)(2) | | 05000220/LER-1986-024, :on 860803,turbine Trip & Subsequent Scram Occurred.Caused by Increase in Reactor Water Level.Hpci Mode of Feedwater Reset,Reactor Water Level Restored & Instrument & Control Personnel Notified to Remove Signal |
- on 860803,turbine Trip & Subsequent Scram Occurred.Caused by Increase in Reactor Water Level.Hpci Mode of Feedwater Reset,Reactor Water Level Restored & Instrument & Control Personnel Notified to Remove Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-024-01, :on 861231,visible Corrosion Observed on Div I & II Battery Bus Bars & Terminals.Caused by Naturally Occurring Leakage from Battery Seals.Corrosion Removed |
- on 861231,visible Corrosion Observed on Div I & II Battery Bus Bars & Terminals.Caused by Naturally Occurring Leakage from Battery Seals.Corrosion Removed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
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