ML20147A965
ML20147A965 | |
Person / Time | |
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Site: | Byron ![]() |
Issue date: | 01/10/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20147A958 | List: |
References | |
50-454-96-09, 50-454-96-9, 50-455-96-09, 50-455-96-9, NUDOCS 9701280378 | |
Download: ML20147A965 (23) | |
See also: IR 05000454/1996009
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U. S. !10 CLEAR REGULATORY COMMISSION
REGI0t1 III
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Docket Nos: 50-454, 50-455
Report flo: 50-454/96009, 50-455/96009
Licensee: Commonwealth Edison Company
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Facility: Byron Generating Station, Units 1 & 2
Location: 4450 N. German Church Road
Byron, IL 61010
Dates: September 27 - December 17, 1996 i
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Inspectors: S. D. Burgess Senior Resident Inspector
N. D. Hilton, Resident Inspector
M. J. Farber. Regional Inspector, DRS
T. M. Tongue, Project Engineer, DRP
C. K. Thompson, Illinois Department of Nuclear Safety !
Approved by: R. D. Lanksbury Chief,
Reactor Projects. Branch 3 i
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9701280378 970110
PDR ADOCK 05000454
G PDR
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EXECUTIVE SUMMARY
Byron Generating Station. Units 1 & 2
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NRC Inspection Report 50-454/96009. 50-455/96009
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-This inspection included aspects of lite..see operations, engineering.
maintenance, and plant support. The report covers a resident inspection ;
conducted from September 27 through December 17. 1996.
Operations
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The station auxiliary transformer (SAT) switching and restoration
operations were carefully planned and professionally executed. -
(Section 01.3) .
Maintenance
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Maintenance and surveillance activities were completed thoroughly and
professionally. (Section M1.1)
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Surveillance test OBVS SX-5 contained inadequate acceptance criteria to
determine SX system operability. (Section M1.2)
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System engineering failed to appreciate or understand the importance of the
surveillance test with respect to SX system operability. Previous
surveillances documented silt accumulation outside the acceptance criteria
and degraded trash racks since 1993 with no operability assessments
performed. (Section M1.3)
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Heat exchanger inspections and cleaning found minimal silt. (Section M1.6)
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Comprehensive maintenance activities significantly improved the weather
protection of the Unit 2 SAT. (Section M1.7)
Engineerinq
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Based on excessive silt found in the essential service water (SX) cooling
towers on October 15, 1996, engineering determined that the SX system was
inoperable when the plant relied on the deep well pumps for makeup
capability. (Section El.1)
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The design input used in calculating the ultimate heat sink cooling tower
basin makeup did not reflect the SX system design features since initial
plant operation. The 1991-1992 design-basis reconstitution failed to
identify this error. (Section E1.2)
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Engineering did not ap] ear to be knowledgeable of the SX system design as
it was documr ed in tle UFSAR. (Section E1.3)
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The license submittal regarding spent fuel pool (SFP) Boraflex degradation
and the decision to checkerboard the SFP was not pursued in a timely manner
until after discussions with the NRC. (Section E2.1)
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Engineering aggressively pursued the motor control center spacer issue with
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Westinghouse. The operability assessment and corrective actions to install
the spacers was timely and thorough. (Section E2.2)
Plant Sunnort -
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The inspectors identified a worker lying in the Unit 1 positive
displacement charging pump room. During an approximate 25-minute stay. the
individual received undetectable radiation exposure. (Section R1.1)
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The inspectors identified a containment 9 ray fire door blocked open
without a fire barrier impairment pert: A violation was issued.
(Section F1.1)
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REPORT DETAILS
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Summary of Plant Status
Unit 1 operated at power levels up to 97 percent during this inspection
period.
Unit 2 was in a refueling outage (B2R06) until October 4.1996, when the unit
went critical and was placed on the grid October 5. 1996. Subsequently, the
unit operated at power levels up to 100 percent. i
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I. Doerations
01 Conduct of Operations
01.1 General Comments (71707).
- Using Inspection Procedure 71707, the inspectors conducted frequent
reviews of ongoing plant operations. In general, the conduct of
operations was professional and safety-conscious. Specific events and
noteworthy observations are detailed in the sections below.
01.2 Unit 2 Startuo (71707)
The licensee shutdown Unit 2 on August 8. 1996, due to a 120 gallons per
day steam generator tube leak. After approximately 1 week, the licensee
transitioned to the refueling outage, originally scheduled to start
September 7. 1996. During the outage, the licensee completed steam
generator inspections and repairs and a reactor coolant system
resistance temperature detector (RTD) bypass loop elimination
modification. On October 4,1996, at approximately 12:30 a.m. (CDT).
Unit 2 criticality was achieved by diluting the reactor coolant system
baron concentration. Following the performance of low power physics
testing, the unit was placed on the grid on October 5,1996, at
1:56 p.m. (CDT).
01.3 Station Auxiliary Transformer Outage Operations
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a. Inspection Scone
The licensee performed a Unit 2 Station Auxiliary Transformer (SAT) bus
duct inspection as part of the corrective actions from the Unit 1 loss
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of offsite power on May 23, 1996. The inspectors observed portions of
the electrical operations required to restore SAT 242-1 and place SAT
242-2 out of service and to restore Unit 2 to a normal off-site power
electrical lineup after inspection completion. The inspectors also
observed portions of the maintenance inspections performed on the bus
ducts (see Section M1.7).
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b. Observations and findings
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On October 26 and November 2. 1996, the inspectors. observed the SAT
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pre-job briefings. Both briefings were attended by all operators
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involved in the SAT outege and -the planned evolutions were discussed in
L detail. Contingency plans were discussed with dedicated operators
L assigned to complete any.. required actions. Extra operators and shift
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management were available to support the evolutions. . Communications
were clear and concise with questions and answers. The significance of
the evolution and management expectations were discussed.
The inspector also observed emergency diesel generator runs, electrical
bus switching evolutions, breaker manipulations, and out of. service -
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activities. The inspector observed consistent application of three-way
l communications, procedure use and place keeping, and peer checking.
c. Conclusions
The inspector concluded that the SAT switching and r'estoration
operations were carefully planned and professionally exec.uted. l
08 Miscellaneous Operations Issues (92901) ~
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08.1 (Closed) Violation 50/454-94022-02: Station procedure BAP 300-1. !
" Conduct of Operations " and BAP 330-1. " Station Equipment '
Out-Of-Service Procedure." did not properly verify that the C steam '
generator (SG) was ready for service prior to refilling it. When the
licensee placed the C SG into wet layup after contractor maintenance,
approximately 3600 gallons of secondary side water drained onto the
containment floor. The inspectors reviewed the licensee's corrective ;
actions that consisted of creating a SG secondary side close-out '
checklist in procedures BMP 3300-14. " Steam Generator Primary Manway
Closure Removal and Installation." Revision 14. and BMP 3300-18. " Steam
7 Generator Secondary Manway/Shell Opening Closure Removal and .
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Installation." Revision 12. The inspectors concluded that the checklist
contained appropriate activities that were required to be performed ,
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prior to returning the SG secondary side to the operations department
for normal system fill or testing following maintenance. The checklist
also established better control of contractor activities. During the
recent Unit 2 outage (B2R06), the checklist was included in the SG work
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request packages with no concerns noted. This item is closed.
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II. Maintenance
M1 Conduct of Maintenance
M1.1 Maintenance Observations (62703)
The inspectors observed all or portions of the following work
activities:
. WR 960094288 Troubleshoot oscillations from 2AF005A.
. WR 960002499 Replacement of RWST access cover gaskets
. WR-960002500 Replacement of RWST access cover gaskets
^ . WR 960101104 Silt removal in SX cooling tower basins A and B
. WR 960108241 Inspect / Clean Unit 1 SI lube oil cooler
The inspectors found that the maintenance activities were conducted in
accordance with approved procedures and were in conformance with
technical specifications. The inspectors observed maintenance
supervisors and system engineers monitoring job progress. Quality
control personnel were also present. When a]plicable, appropriate
radiation control measures were in place. T1e inspectors identified no
concerns as a result of these maintenance observations.
M1.2 Inadeouate Surveillance Test Acceptance Criteria and Test Control
a. Inspection Scope
On October 1.5. 1996, during the performance of surveillance OBVS SX-5.
" Inspection of River Screen House (RSH) and Essential Service Water
Cooling Tower." the licensee identified that silt levels in the
essential service water (SX) cooling tower basins were greater than the
acceptance criteria. The inspectors reviewed surveillance procedure
OPVS SX-5 for technical adequacy and also discussed the results of the
diver's inspection on October 15. 1996. with licensee personnel.
Additional observations and issues related to the silt problem are
discussed in other sections of this report under II. Maintenance and
III. Engineering.
b. Observation and Findings
Inadeouate Acceptance Criteria
The inspectors questioned the validity of the SX cooling tower basin
acceptance criteria listed in surveillance OBVS SX-5. The acceptance
criteria stated that the silt buildup in the SX cooling tower basins ,
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shall not exceed 12 inches at two or more points shown on OBVS SX-5.
Attachment E. Attachment E. which was an illegible diagram of the SX
basins. showed 30 sample locations. The inspectors questioned the
operability of the SX system if all 30 silt sample points were measured
within the acceptance criteria at 11 inches. The licensee agreed that
the procedure was inadequate and could not provide justification for the
surveillance acceptance criteria. The inspectors determined that the
procedure failed to have sufficient quantitative acceptance criteria to
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determine SX system operability based on silt levels in the SX cooling
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tower basins. This is an apparent violation of 10 CFR Part 50, '
Alpendix B, Criterion V. " Instructions. Procedures, and Drawings," ,
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Inadeauate Test Control .
The inspectors were told that the October 15, 1996, silt measurements in
the SX cooling tower basins were taken with reference to the diver's
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boot and arm. The inspectors questioned the appropriateness of this !
practice since surveillance procedure OBVS SX-5 referenced test
equipment such as underwater cameras and depth gages that may be used -
during test performance. Since the silt measurements wete-used to
determine SX system operability, the inspectors considered the iiver's
boot and arm to be inappropriate measuring devices for measuring the
silt height in the SX cooling tower basins. Failure to use adequate
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test instrumentation to measure the amount of silt in the SX cooling i
' tower basins is an apparent violation of 10 CFR Part 50 Appendix B, i
Criterion XI, " Test Control." (EEI 454/455/96009-02(DRP)). ,
c. Conclusions -
Inadequate acceptance criteria in surveillance OBVS SX-5 could have
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resulted in meeting the stated acceptance criteria for silt levels in
the SX cooling tower basins even though the SX system would not have
been able to meet its design function.
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M1.3 Inadeouate Evaluation and Corrective Action of Past Surveillances
a. Insoection Stone
The inspectors reviewed past OBVS SX-5 surveillance test results for
1993 through 1995 to detennine previous SX basin silting conditions.
b. Observations and Findinas
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Excessive Silt Accumulation
The acceptance criteria for the amount of silt allowed in surveillance
OBVS SX-5 was as follows:
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l * The RSH intake and forebay shall not exceed 9 inches at two points
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along the width of the intake channel.
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. The RSH SX pump sumps shall not exceed 6 inches sediment accumulation
in sumps.
. The SX cooling tower basin shall not exceed 12 inches at two or more
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points.
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The inspectors reviewed the 1993 tL mugh 1996 completed OBVS SX-5
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surveillance tests and identified the following issues:
. On July 26. 1993, the diver recorded 14 areas where silt levels were
12 inches to 24 inches in the SX basin. silt accumulations in one of
the sumps was 10 inches, and RSH intake and forebay silt
accumulations were 24 to 36 inches. Corrective actions consisted of
the diver " distributing" the silt to levels that met the surveillance
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acceptance criteria. No operability assessment for the SX system was !
performed on the as found silt condition.
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The silt buildup in the SX cooling tower basin changed the volume of
water as analyzed in the UFSAR and therefore could change the
consequences of the design-basis accident bounded in the UFSAR.
Failure to take a)propriate corrective action to the silt 1
accumulation in t1e SX cooling tower basins is an apparent violation
of 10 CFR Part 50. Appendix B. Criterion XVI. " Corrective Action."
. On July 26,199S. the diver recorded silt accumulations of 30 inches
to 4 feet in the RSH intake and forebay area. Silt accumulation in
the SX makeup pump sump measured 12 to 18 inches. The silt was
removed via a vacuum pump. Engineering evaluated the test results on
June 17, 1996. No operability assessment for the SX system was
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performed on the as found silt condition.
Based on previous surveillance results, the inspectors questioned SX
system operability since 1993. The licensee initiated a root cause
investigation into the SX silting issue and planned to address past SX
system operability.
Degraded Trash Rack Gratina
The inspectors also identified that the completed surveillance tests for
1.993, 1994, and 1995 documented that several portions of the trash rack
grating had fallen away from up)er lateral supports or were lying in the
bottom of the SX cooling tower Jasins or leaning against the basin
support columns. The trash rack grating was attached to the anti-vortex
drainage duct located at each end of basin A and B. The trash racks
provided a 4 inch by 1-3/16 inch screen for large debris before entering
the drainage duct and eventually the SX pump suction. The ins)ectors
also noted that UFSAR Section 3.8.4.1.6. Figure 3.8-66, descri)ed the
trash rack grating.
System engineering concluded after each surveillance test that the trash
rack grating was not part of the test acceptance criteria and that a
work request had been previously written in 1993 to restore the grating
in basin A and in 1994 for the same repairs in basin B. No safety
evaluation or screening for potential unreviewed safety questions had
been performed on this change to the SX system. Since the SX cooling
tower basins are classified Seismic Category I, the inspectors also
questioned the effects the degraded grating potentially had on the UHS
seismic qualifications. The failure to take prompt corrective action to
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repair the trash racks is an apparent violation of 10 CFR Part 50.
Appendix B. Criterion XVI. " Corrective Action." (EEI -
454/455/96009-03B(DRP)).
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In November 1996 the licensee replaced the grating and repaired or- '
replaced the necessary support brackets that were also degraded. During
review of the seismic analysis for the SX cooling tower structure the ,
licensee identified an error in the methodology used to determine
seismic response and member stresses in calculations No. 4.2.3 BY and '
3.4.1 BY. The errors were not significant and the licensee planned to
regenerate the calculations.
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c. Conclusions ,
System . engineering failed to appreciate or understand the importance of
the surveillance test with respect to SX system operability. Previous
surveillances that documented silt accumulations outside the acceptance
criteria brings into question the SX system operability since 1993.
Inadequate corrective action to repair the trash racks since 1993 '
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demonstrated a lack of knowledge of SX system design by the licensee and '
a willingness to operate with a-degraded safety system.
M1.4 River Screen House Insoections
a. Insoection Stone
On December 4,1996, the licensee performed an inspection of the RSH. *
The inspectors discussed the diver's inspecticn with licensee personnel,
b. Observations and Findings
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On December 4.1996, with the use of divers the licensee inspected the
RSH for silt accumulation and found silt levels that exceeded OBVS SX-5 i
surveillance acce)tance criteria at several locations. Through
interviews with t1e diver and licensee Jersonnel the inspectors found
the most significant accumulation was t1e 0A SX makeup pump sump which !
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contained 36 inches of silt where the acceptance criteria was 6 inches. '
The licensee's operability assessment determined that presence of the
silt accumulation did not impede the operability of the pumps to deliver
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the required flow rate. This assessment was based on inservice test t
data (taken every 92 days) that indicated that the pumps were delivering
expected flow rates without exceeding differential pressure
requirements. The data also indicated no signs of pump cavitation. The
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As discussed in Section M1.3. surveillance OBVS SX-5. performed on
July 26, 1995. documented silt levels of 12 to 18 inches. The silt was
removed via a vacuum pump.
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Based on review of the SX makeup pump inservice testing data, the
j inspectors confirmed the licensee assessment that the presence of silt '
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in the sump did not impede the pumps from delivering the required flow
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rate and showed no signs of pump degradation. The excessive silt
accumulation appeared to have taken place over the past 17 months.
M1.5 SX Basin and River Screen House Silt Removal
a. Inspection Scope l
The inspectors observed portions of the silt removal from the SX cooling
tower basins and the RSH. The inspectors discussed the procedure and j
process with licensee personnel and the divers.
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b. Observations and Findings
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To control the cleaning activities in the SX cooling tower basins, the i
licensee wrote procedure SPP 96-067, " Support for Cleaning. Inspection. '
and Repair Activities in the Essential Service Water Cooling Tower
(SXCT) Basins." Revision 0. This special test detailed the system
line-ups needed to support the basin cleaning and also monitored SX
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system parameters before and after the cleaning to detect any effects '
the cleaning might have on the SX system. The silt remov'ed from the ,
towers and the RSH was pumped to tanker trucks, which transported the l
silt to a large earthen basin located just northwest of the plant, j
within the owner controlled area.
c. Conclusions
The inspectors monitored the activities and had no concerns with the
silt removal process. The silt removal activities continued after this
inspection period.
M1.6 Various Heat Exchanger Inspections for Silt
a. Insoection Scone
The inspectors observed portions of small heat exchanger inspections for
silt and discussed the findings with licensee engineering.
b. Observations and Findinas
To ensure that the de-silting activities at the SX cooling tower basins
and the river screen house (RSH) was not adversely affecting plant
equipment, the licensee performed inspections and cleaning of various
heat exchangers cooled by SX water. The inspectors observed minimal
silt in the heat exchangers and agreed with the licensee that heat
exchanger performance was not impaired. The licensee planned to
continue with the inspections on an increased frequency, until the
de-silting was completed and an enhanced inspection schedule was
developed.
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c. Conclusions
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The inspectors found that the inspection activities were conducted in
accordance with approved procedures and were in conformance with
technical specifications. The inspectors observed maintenance
supervisors and system engineers monitoring job progress. Quality
control personnel were also'3 resent. The inspectors identified no 1
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concerns as a result of the leat exchanger inspections since minimal
silt was found in SX heat exchangers inspected.
M1.7- Station Auxiliary Transformer Outaae Maintenance
, a. Insoection Scone
The inspectors observed )ortions of.the maintenance inspections
performed on the Unit 2 aus ducts and discussed the overall maintenance
activities with the SAT outage project manager. These activities were
also reviewed against the Updated Final Safety Analysis Report (UF_SAR)
descriptions.
.b. Observations and Findings
The licensee removed the lower covers for the SAT bus ducts to inspect
for water intrusion. The licensee did not identify any significant
degradation of bus duct insulators. The bus duct caulk was also
inspected and found satisfactory; however, the licensee did add caulk in
several areas to provide additional protection. Additional measures
taken to improve the weather protection included supporting rubber seals
on the transformers to enhance water run off and the addition of a
waterproof tape at exterior junctions of the bus duct.
c. Conclusions
The inspector concluded that the licensee significantly improved the
weather protection of the Unit 2 SAT by the comprehensive nature of the
inspection and enhancements.
ML8 Surveillance Observations
a. Insoection Scone (61726)
The inspectors observed all or parts of the following surveillance and
special test procedures. The inspectors also reviewed plant equipment
and surveillance activities against the UFSAR descriptions.
. OBOS 7.5.e.1-1 Essential Service Water Makeup Pump OA Monthly
Operability Surveillance
1BOS 3.1.1-21 Train B Solid State Protection System (SSPS)
Bi-Monthly Surveillance
180S 3.2.1-941 ESFAS Instrumentation Slave Relay Surveillance
1BOS 7.1.2.1.b-1 1A Auxiliary Feedwater Pump Monthly Surveillance
180S 7.1.2.1.b-2 Unit 1 Diesel Driven Auxiliary Feedwater Pump
Monthly Test
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1BOS 8.1.1.2.a-1 Unit 1 1A Diesel Generator Operability Monthly
Surveillance
1BVS 5.2.f.3-2 ASME Surveillance Requirements for Residual Heat
Removal Pump 1RH01PB
-. 2BVS AF-1 Unit 2 2B Diesel Auxiliary Feed Pump Battery
Bank A Capacity Test
2BVS AF-3 Unit 2 Simultaneous Start of Both AF Pumps With
Flow to the Steam Generators
. SPP 96-067 Support for Cleaning, Inspection, and Repair
Activities in the Essential Service Water
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Cooling Tower (SXCT) Basins
b. Observations and. Findings .
During the 1B SSPS surveillance, the licensee failed to complete the
testing within the technical specification (TS) allowed time of 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.
Testing was delayed when an operator failed to latch a relay during the
test. The operator pushed the relay button in far enough to actuate the
relay, but did not latch the relay. Issue resolution delayed the
testing. The inspectors noted that the licensee completed the testing,
but appropriately entered the limiting condition for operation action
requirement. TS 3.3.1 action statement 12.b., for an inoperable reactor
trip breaker. TS 3.3.1 action 12.b required the reactor trip breaker to
be restored in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. the licensee completed the testing in 45 minutes
and exited the action requirement. The inspectors also noted that the
licensee appropriately entered the failure to latch the relay into the
operator workaround program for formal resolution.
c. Conclusions
Observed surveillance activities were completed thoroughly with system
engineers monitoring activities. Difficulties in completing the 1B SSPS
surveillance were appropriately handled with the entry into the TS
action statement.
H8 Miscellaneous Maintenance Issues (92902)
M8.1 (Closed) Inspection Followuo item 50/454-95003-03: Diesel generator
hairline cracks on air intake manifolds were identified during a monthly
surveillance. The licensee's material failure analysis concluded that
the manifolds were overstressed during installation resulting in
material cracks / defects that propagated during engine operation due to
vibration. The licensee installed new intake manifolds on the Unit 1
diesel generator during B1R07. The new manifolds were manufactured to
more stringent fabrication and welding criteria. The manifolds from
i Unit 1 were refurbished by the vendor to the new standards and installed
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on the Unit 2 diesel generators during B2R06. The inspectors noted no
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reoccurrence of the hairline cracks since installation of the
new/ refurbished intake manifolds. This item is closed.
M8.2 (Closed) Insoection Followuo Item 50/454-96003-03: Potential effect of
boric acid corrosion on the carbon steel filtered vent (VF) system due {
to a blocked safety injection (SI) pump drain line. In response to this '
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Concern, system engineering determined that the boric acid corrosion
would be limited to-less than 0.002 inches per year based on boron >
concentrations of 2500 ppm. The VF system is not safety-related and no
operability concerns were noted. The licensee repaired the blocked SI
drain lines This item is closed. ~ '
M8.3 (Closed) Insnection Followun Item 50/454-96007-02: Containment spray
(CS) pump room 1A contaminated due to floor drain plugging. The
inspectors questioned the operability of the safety-related equipment in
the CS and residual heat removal (RHR) rooms with an ' inoperable floor
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drain system, since the UFSAR took credit for the floor drain system to
mitigate the consequences of a flood. In response, the licensee found
only one of two floor drains in the CS and RHR pump rooms plugged.
Based on this configuration, the licensee estimated that during a
design-basis flooding accident, the flood level would be about 5 inches
below the CS and RHR pumps and would be considered operable. The
analysis assumed the flood duration of 30 minutes in accordance with the
UFSAR. Corrective actions included hydrolyzing the floor drains at 4
year intervals and inspect, clean, and test the sump alarms at 5 year
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intervals. This item is closed.
111. Engineerina "
El Conduct of Engineering
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El.1 Excessive' Silting in the Essential Service Water Coolina Towers (37551)
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a. Insoection Scoce
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! The inspectors reviewed the action taken by engineering to determine the
consequences of the silting on the operability of the SX system.
b. Observations and Findings
The licensee identified that silt levels in the SX cooling tower basins
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were greater than the acceptance criteria stated in surveillance OBVS
l SX-5. The acceptance criteria stateu that silt levels were not to
i exceed 12 inches at two or more points. Silt levels at 28 points were
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found to be at 12 to 36 iaches. '
The inspectors review of the licensee's operability assessment found
that the presence of silt in the basin displaced an equivalent volume of
water in the basin. Based on silt measurements taken from both basins,
it was estimated that approximately 48,000 gallons of water were
displaced by the silt. This volume corresponded to a level change of
approximately 15 3ercent on the basin level indicators. The SX cooling
tower serves as tle ultimate heat sink (UHS) for both units and consists
' of two interconnected basins A and B. The water volume in the basin is
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critical as thermal performance of the UHS relies on a specified water
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volume to absorb heat energy from safety-related components cooled by
the SX system. Both thermal and volumetric considerations (which
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include makeup capability) are impacted by the presence of excessive
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silt.
The licensee's o)erability assessment of the thermal performance of the
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UHS determined tlat an adequate volume of water exii.ed in the SX t
cooling tower basin to maintain the SX design temperature below 100 F
for design-basis accident conditions at the TS minimum basin level of
50 percent. <
For makeup capability to the basin, the licensee evaluated the
higher-capacity SX makeup pumps, which corresponded to a TS minimum
water level of 50 percent, and the lower-capacity-deep well pumps, which {
required a TS minimum basin level Qf 82 percent. The makeup capability I
must be sufficient to offset the evaporation rate of the water in the '
cooling tower basin. The analysis concluded that the 15 percent silt
level in the basin had no significant impact on the ability to makeup
the basin with the SX makeup pumps. However, the corresponding
evaluation for the deep well pumps determined that the makeup capability
was inadequate and one basin would run out of water and be incapable of
providing water to the SX system. Therefore, the continued operability
of the UHS and the SX system, when relying on the deep well pumps for 1
makeup capability, would only be assured if SX basin level was
maintained at or above 97 percent to account for the 15 percent silt
accumulation.
1
As compensatory measures the licensee administratively raised the SX
basin levels from 50 percent to 60 percent during normal operations when
both SX makeup pumps were available. The water level limit was raised
from greater than or equal to 82 percent to 97 percent when relying on
the deep well pumps for makeup capability. This reliance occurred when
TS 3.7.5 action statement c, e, f, g, or h were entered. This included
situations when: (1) one or more SX makeup Jumps were inoperable; (2)
when one UHS cooling tower basin level switc1 was inoperable: (3) when
the Rock River water level was forecasted to exceed 702.0 feet: (4) when i
the Rock River water level fell below 664.7 feet or flow was less than !
700 cfm: .and (5) when a tornado watch was issued for the Byron site. I
The inspectors reviewed maintenance records and operator logs and
determined that the plant relied on the deep well pumps for makeup
capability on July 7 - 12, 1996, during SX makeup Jump, OSX02PB,
maintenance and July 23, 1996, when a tornado watc1 was issued for the
Byron area. Based on the licensee *s analysis, the UHS and the SX system
was considered inoperable at these times.
l
c. Conclusions '
The licensee's operability assessment concluded that the SX system was
inoperable, when relying on the deep well pumps for makeup capability, i
since the basin water volume corresponding to an indicated water level
of 82 percent, reduced by 15 percent due to the presence of silt, was an
inadequate volume of water to support SX operation.
14
.
.
\
l
El.2 Inadequate SX Makeun Calculation !
.
a. Inspection Scnne
During subsequent evaluations, the licensee identified errors in the UHS 1
cooling tower basin makeup calculation. The inspectors discussed the i
,
error with the licensee to determine the error consequences on SX system !
operability. '
b. Observations and Findings
!
The inspectors reviewed the licensee's determination that the VHS
cooling tower basin makeup calculation. NED-M-MSD-14. Re. vision 0 3
'
(performed in February 1992) and Revision 1 (performed in August 1992). !
was based on a usable basin water volume calct 'ated from the bottom of I
the basin. The inspectors found that the actual usable volume for water
1
was limited by the anti-vortex drainage duct that enclosed the SX pump !
suction pipe. The anti-vortex drainage duct openings were 8 inches
above the basin slab and the makeup calculation did not account for this
8 inches of unusable water volume. The calculation also did not account I
for any silt accumulation. These calculations were performed during the ' '
SX/ UHS design-basis reconstitution effort in 1991 and 1992.
l
With the usable volume reduced 8 inches by the anti-vortex drainage
duct, the licensee determined that the deep well makeup pump would not
have adequate makeup capability when the VHS basin water level was at
82 percent per TS 3.7.5 action statements c. e. f, g. or h.
,
The TS l
water level of 82 percent was an inadequate water volume to ensure UHS i
and SX system operability. The licensee stated that the calculational '
error had existed since initial plant operation. Failure to have
adequate design control measures in place to ensure that the
design-basis of the SX system was correctly translated into
specifications is an apparent violation of 10 CFR Part 50. Appendix B.
Criterion III (EEI 454/455/96009-04(DRP)). ,
I
c. Conclusions
The inspectors concluded that the licensee's design input used in
calculating the UHS cooling tower basin makeup did not reflect the SX
system design features since initial plant operation. The design-basis
reconstitution performed in 1991 and 1992 failed to identify this error. l
E1.3 UFSAR Discrepancies on SX Coolina Tower Desian Features
a. Inspection Scone
The inspectors reviewed applicable sections of the UFSAR to determine if
the SX system was accurately reflected.
b. Observations and Findings
The inspectors identified discrepancies between UFSAR Figure 3.8-66 and
UFSAR Figures 9.2-25, 9.2-26. and 9.2-27. Figure 3.8-66 showed a small
15
-- - . - .-- - - - - - . _ . .-- - .- .- . - . - - . - - -
.
box-shaped screen (trash rack) over the SX pump suction in the cooling
.
tower basin and the other figures showed a large anti-vortex drainage
duct. The licensee investigated the discrepancy and determined that the
box-shaped trash rack was part of the initial SX cooling tower basin
design. The box-shaped trash rack was designed to both prevent trash
from entering the SX pump suction piping and to eliminate vortex ;
formation at the suction piping. Testing, performed at the University l
of Iowa in 1980, demonstrated that the box-shaped trash rack neither
effectively prevented vortex formation nor provided adequate capacity as
a trash rack. As a result, prior to receiving an operating license, a
design change installed an anti-vortex drainage duct with an attached
trash rack that ran the width of each basin and enclosed the SX pump
suction. The UFSAR drawings had never been updated to show the current '
dssign. Failure to update the UFSAR to assure that the information
1
included in the UFSAR contains the latest material developed is an.
apparent violation of 10 CFR 50.71, " Maintenance of records, making of
reports," (EEI 454/455/96009-050RP)).
c. Conclusions
,
Licensee personnel did not appear to be knowledgeable that a portion of
the as-built SX system design deviated from design as it was documented
in the UFSAR.
E1.4 Additional SX Basin inspections
7
a. Insnection Stone
On November 5 and 6,1996, the inspectors monitored the licensee's
performance of additional SX basin inspections to facilitate the trash
rack grating replacement and repairs.
- b. Observations and Findinas
A diver entered SX basin B to better inspect and identify the necessary
l repairs to the trash rack. During the inspection, the diver identified
and removed a 4 foot by 20 foot piece of plastic and tw hard hats.
Based on interviews of the divers the inspectors dete" mined that the
plastic was found crumpled against the anti-vortex drainage duct and the
i
l l
hard hats were found on the basin floor. Because of the uncertainty of i
I
similar material being in the A basin, the licensee declared the SX '
pumps in A train on both units inoperable until an ins)ection could be
performed. On November 6,1996, the diver inspected t1e A basin and
i
found a 4 foot by 20 foot piece of plastic and one hard hat. Based on
the observed condition of the materials found in both basins, the
'
inspectors concluded that the items had been in the basin for quite some
time however, the ins 9ectors noted that the SX cooling tower basin
inspections performed in 1993, 1994, 1995, and on October 15. 1996, did
not identify these items.
i
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16
1
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. - - - ,- . - . - - - - - . - - . - . - . - - .-
..
i
c. Conclusions
.
.
Based on the additional inspections, the licensee concluded that both SX
cooling tower basins were free from large foreign material that could
potentially block the SX pump suction. The inspectors concluded that
the age of the foreign material found in the basins called into question
the thoroughness of the previous inspections.
E2 Engineering Support of Facilities and Equipment
E2.1 Soent Fuel Pool Boraflex Dearadation
.
a. Insoection Scone ,
,
Boraflex degradation was first discussed in inspection re) ort 95-09
after the licensee identified elevated silica levels in t1e spent fuel
pool (SFP). Blackness testing, to verify the presence of a neutron
absorber, was performed during June 1996. The licensee received the
test results on September 3. 1996. The in.cpector reviewed the blackness
test results, the licensee's LER, the licensee's response to NRC Generic
Letter 96-04 "Boraflex Degradation on Spent Fuel Pool Racks." and the
licensee's license amendment submittal.
b. Observations and Findings
t
During 1995, the licensee identified elevated levels of silica in the
SFP which was an indicator of Boraflex degradation. Boraflex was
constructed of an organic polymer with a silica filler and neutron
i
absorbing boron carbide interspersed within the silica filler. Boraflex
degradation consisted of cracks and gaps forming in the Boraflex panels
with the Boraflex eventually becoming susceptible to dissolution in the
SFP water. The licensee took interim actions to limit the rate of
degradation, including not reducing silica levels in the SFP. The
i
licensee also established an administrative limit of greater than 1000
l parts per million (ppm) soluble boron in the SFP. The licensee
calculated the 1000 p)m boron would be adequate to maintain k,r, less
than 0.95 if all of t1e Boraflex was removed.
Blackness testing performed on approximately 300 storage cells during l
' June 1996, indicated three panels where Boraflex gaps exceeded 4 inches.
The design criticality analysis assumed any Boraflex gaps to be less
than 4 inches. TS 5.6.1.1 required the SFP racks to maintain k
! than or equal to 0.95 when flooded with unborated water. With he trrgaps,
less
the calculation that demonstrated TS compliance was invalid and the
licensee declared the SFP racks inoperable.
The licensee reviewed the acti;ns taken during the fall of 1995 when the
degradation was identified and determined the actions to be adequate
interim measures. The licensee originally planned to submit a TS
i amendment in early 1997 requesting approval to include soluble boron in
!
the criticality analysis. However, after discussions with the NRC, the
.
4 licensee accelerated the amendment submittal and submitted a license
amendment on November 12. 1996.
1
17
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_ . . _
_ . _ _ _ _ _ . _ . _ _ . _ _ _ _ _ - . . . _ . _ . _ . _ _ _ . . _ . . _ . _
!
- .
.
l'
i
- in addition to the amendment sabmittal, the licensee planned to arrange
'
the fuel in a checkerboard pattern in the SFP to ensure the SFP remained
subcritical with no Boraflex or soluble boron. Checkerboarding placed
fuel in the SFP such that either one or two cells out of every four
.
4
'
would be empty. A criticality analysis indicated that some - '
checkerboarding was required to demonstrate k,,,
- would be less than 1.0
a with no Boraflex and flooded with unborated water.
'
- LER 96-014-00. " Failure to Comply with Design Basis Due to Degradation
.
of.Boraflex in Spent Fuel Racks." was reviewed by the inspector. With
j .
the addition of the accelerated license amendment submittal and the
1
planned checkerboarding, the inspector considered the LER appropriate.
i
The inspector verified the soluble boron limit was administratively
!
controlled and that the licensee had not been removing silica from the
SFP. The inspectors will continue to follow this issue through the
j licensee's LER supplement.
3
j c. Conclusions
A
j~
The inspector concluded that the licensee monitored the Boraflex
degradation and planned to submit a license amendment. However, the
license submittal was not being pursued in a timely manner until after
!
discussions with the NRC. Also, the decision to checkerboard the SFP
! was not made until after NRC discussions and a criticality analysis
indicated that the checkerboard must be performed to ensure the SFP
,
remained subcritical with unborated water.
'
j E2.2 Missina Scacers in Motor Control Center
i
i a. Insoection Scone
i
During refueling outage B2R06, the licensee noted that spacers were
removed from some Westinghouse motor control center (MCC) breaker
! buckets. The MCC spacers were. located between the bucket and the MCC
j
frame. The inspectors reviewed the licensee's corrective actions on the
,
1ssue.
1 b. Observations and Findings
4
i
Byron engineering contacted Westinghouse and were first told that the
j
spacers were shipping spacers and were not needed and that missing
spacers would pose no concern. Engineering continued to pursue the
t
issue with Westinghouse, who later determined that the spacers were
! installed in the original MCC seismic qualification testing.
The licensee 3erformed an interim o)erability assessment and determined
that the MCC Juckets were operable )ased on com)arisons of seismic
! testing performed at levels four times higher tlan Byron plant seismic
'
requirements. The inspectors reviewed and agreed with the assessment.
The licensee installed the spacers in the MCCs.
4
f
g 18
l
- - - - . . . - - . . , _ - . . _ _ _ . ,_ --
- _ . - . . --
..
c. Conclusions
Engineering aggressively pursued the MCC spacer issue with Westinghouse.
The operability assessment and corrective actions to install the spacers
was timely and thorough.
IV. Plant Sucoort
j R1 Radiological Protection and Chemistry Controls
.
R1.1 ALARA Concern .
a. Insoection Stone
During a routine tour of the auxiliary building, the inspectors
identified a worker lying in the Unit 1 positive displacement (PD)
charging pump (CV) room. The inspectors reviewed the licensee's
corrective actions and initial investigation results.
l b. Observations and Findings
On November 27, 1996, the inspectors identified a contracted engineer
l lying on the floor in the Unit 1 PD CV pump room. The dose rate where
the individual was lying was less than 1 mR/ hour. The worker was not
wearing a hard hat or safety glasses and had his feet propped up on the
pump skid piping. The inspector questioned the individual and was told
that he was a contracted engineer assigned instrument air system
walkdowns. In response to the inspectors ALARA concerns, the licensee
determined that the individual was in the auxiliary building for
a3 proximately 25 minutes and received no detectable radiation exposure.
T1e individual was relieved of his duties at the site.
- c. Conclusions
The inspectors noted prompt management attention to this issue.
F1 Control of Fire Protection Activities
,
F1.1 Containment Sorav Pumo Room Fire Door Blocked Open (71750)
a. Insoection Scope
During a routine tour of the auxiliary building, the inspectors
identified a fire door between the Unit 2 CS pump rooms blocked open.
,
l
The inspectors reviewed the licensee's immediate corrective actions and
l initial investigation results.
b. Findinos and Observations
On October 7,1996, the inspectors identified that fire door D-846.
located between the 2A and 2B CS pump rooms, was impaired without a Fire
19 !
-
l
l
l
_ . _ . - - . . . ._. -
(
- .
Barrier Impairment Permit (FBIP) on the door. Cables used to remotely
.
<
.. monitor RHR pump oil levels impaired the door. The inspectors notified
the operations department and the door was closed.
)
In response to the inspectors concern, the licensee determined that the i
door had a FBIP when the cables were installed: however, the FBIP was
issued for door repair due to an unrelated door hardware problem. The !
1
l
mechanics installing the cables did not add the cables to the existing i
FBIP After the door was repaired, the FBIP was removed. At the end of
the inspection period, the licensee was deteruining the chronology of
events after the original FBIP was removed.
Byron Administrative Procedure (BAP) 1100-3, " Fire Protection Systems,
Fire Rated Assemblies, Ventila'lon Seals, and Flood Se'al Impairments "
Revision 10, stated, in part, tilat a FBIP was required for all fire
- protection equipment, fire detection instrumentation, fire rate
i
assemblies, fire rated assemblies sealing devices, ventilation seals,
and flood seals which were impaired. Contrary to these requirements,
fire door D-846 was impaired without a FBIP initiated. The inspectors
considered this failure to follow procedures a violation of TS 6.8.1,
" Procedures and Programs" (50-455/96009-06(DRP)). -
l
'
4
c. Conclusions \
The inspectors concluded the blocked open CS fire door without a FBIP
indicated a need for additional improvement in procedure adherence when
)
impairing fire protection equipment. '
i
V. Manaaement Meetinas
X1 Exit Meeting Summary
l The inspectors presented the inspection results to members of licensee
management on November 14, 1996, and at the conclusion of the inspection on
December 17, 1996.
5
a
1 The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary. No proprietary information
.
was identified.
l
,!
.
e
' 20
4
______ _ __ __ _ _ _
- - . --- -- - - .. - . . _-
!
.
PARTIAL LIST OF PERSONS CONTACTED
, licensee
K. Kofron, Station Manager
D. Wozniak, Site Engineering Manager
T. Gierich, Operations Manager
P. Johnson, Technical Service Superintendent
E. Campbell, Maintenance Superintendent
M. Snow Work Control Superintendent
D. Brindle, Regulatory Assurance Supervisor
K. Passmore, Station Support & Engineering Supervisor
J. Feimster Site Engineering Mechanical Lead
M. Robinson, System Engineer
P. Donavin, Site Engineering Mod Design Supervisor
T. Schuster, Site Quality Verification Director
R. Colglazier, NRC Coordinator ,
'
B. Gossman, Chemistry Supervisor
S. Gackstetter, Thermal Group Leader
W. Walter. 0]erations Engineer Unit 0
R. Wegner, S1ift Operations Supervisor
W. Kouba, Long Range Work Control Superintendent
i
INSPECTION PROCEDURES USED
IP 37551: Onsite Engineering
IP 61726: e
Surveillance Observations l
IP 62703: Maintenance Observations '
IP 71707: Plant Operations
IP 71750: Plant Support Activities
IP 92901: Followup - Plant Operations
IP 92902: Followup - Maintenance
21
j
l
J
.
ITEMS OPENED. CLOSED, Af40 DISCUSSED
~
Opened
i
EE: 454/455/96009-01 V10 Failure to have sufficient quantitative
acceptance criteria in procedure OBVS SX-5.
eel 454/455/96009-02 V10 Failure to use adequate test instrumentation to ;
measure the amount of silt in the SX cooling {
tower basins. '
EEI 454/455/96009-03A VIO Failure to take appropriate corrective action
for previous silt accumulation in the SX cool,ing I
tower basins. ,
EEI 454/455/96009-03B VIO Failure to take prompt corrective action to
repair degraded SX cooling tewer basin trash
racks.
EEI 454/455/96009-04 VIO Failure to have adequate design control measures
in place to ensure that the design-basis of the
SX system was correctly translated into
specifications.
eel 454/455/96009-05 VIO Failure to update the UFSAR.
50-454/455/96009-06 VID Failure to follow procedure BAP 1100-3 regarding
fire door impairment.
Closed
50-454/94022-02 VIO Inadequate procedures
50-454/95003-03 IFI Diesel generator hairline cracks on air l
intake manifolds were identified during a
monthly surveillance.
50-454/96003-03 IFI Potential effects of boric acid corrosion on
the carbon steel filtered vent system.
50-454/96007-02 IFI CS pump room 1A contaminated due to floor
drain plugging.
22
.,
LIST OF ACRONYMS USED
.
ALARA As Low As Reasonably Achievable
ASME American Society of Mechanical Engineers
BAP Byron Administrative Procedure .
BOS Byron Operating Procedure
BVS Byron Surveillance Procedure
FBIP Fire Barrier Impairment Permit
MCC Motor Control Center
mR millirem
_ 00S Out of Service
RH Residual Heat Removal System
RSH River Screen House
SAT Station Auxiliary Transformer
SFP Spent Fuel Pool
SI Safety Injection
SSPS Solid State Protection System
SX Essential Service Water
SXCT Essential Service Water Cooling Tower
TS Technical Specification
UFSAR Updated Final Safety Analysis Report
VF Filtered Vent System
23