ML20141E803

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Insp Rept 50-263/97-06 on 970412-0527.Violation Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support
ML20141E803
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 06/18/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20141E780 List:
References
50-263-97-06, 50-263-97-6, NUDOCS 9707010164
Download: ML20141E803 (20)


See also: IR 05000263/1997006

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION 111

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Docket No.

50-263

License No.

DPR-22

Report No.

50 263/97006(DRP)

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Licensee:

Northern States Power Company

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Facility:

Monticello Nuclear Generating Station

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Location:

414 Nicollet Mall

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Minneapolis, MN 55401

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Dates:

April 12 - May 27,1997

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inspectors:

A. M. Stone, Senior Resident inspector

J. Lara, Resident inspector

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Approved by:

J. McCormick-Barger, Chief

Reactor Projects Branch 7

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9707010164 970618

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ADOCK 05000263

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EXECUTIVE SUMMARY

Monticello Nuclear Generating Station, Unit 1

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NRC Inspection Report 50-263/97006

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This inspection included aspects of licens6e operations, engineering, maintenance, and

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plant support. The report covers a 6-week period of resident inspection.

Ooerations

Control and performance of the reactor shutdown activities were excellent.

Communication and teamwork during the evolution were good (Section 01.2).

The inspectors concluded that the anticipated transient without a scram (ATWS)

system was tested in accordance with technical specifications (TSs) and as

described in the updated safety analysis report I'.*0AR). Operators responded

appropriately during simulated ATWS conditions (Section O2.1).

A violation of a TS-required procedure was identified for operators being unaware

that an essential service water pump was unnecessarily operating and had been

operating for about 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> (Section 08.1).

Maintenance

The observed maintenance activities were performed in a professional manner and

in accordance with applicable TS and USAR requirements. However, isolation tags

for two valves were reversed because of inattention-to-detail by system engineering

(Section M1.1).

Ennineerina

The licensee's actions to address and resolve an inadequate net positive suction

head concern were appropriate. The decision to shut down and replace the torus

suction strainers was conservative (Gection E2.1),

The inspectors identified a concern regarding the adequacy of a TS which allowed

the alignment of two power sources through a common transformer. Discrepancies

between the as-design electrical system and USAR were also identified (Section

E2.2).

Licmcee corrective actions with respect to the reactor core isolation cooling

annunciator circuits were determined to be acceptable. An inspection followup

item was identified to review additional systems for fuse and drawing discrepancies

(Section E2.3).

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Report Details

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Summarv of Plant Status

The unit operated at power levels up to 100 percent power until May 9,1997, when

operators commenced a reactor shutdown as directed by plant management. A concern

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regarding the available net positive suction head (NPSH) for the core spray (CS) and

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residual heat removal (RHR) pumps was identified by plant personnel. After further

evaluation, plant management decided to shut down the unit to facilitate replacement of

the emergency core cooling system's torus suction strainers. This issue is discussed in

Sections 01.2 and E2.1.

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1. Operations

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Conduct of Operations

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01.1 General Comments

Using inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. These reviews included observations of control room

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evolutions, shift turnovers, operability decisions, and logkeeping. Updated Safety

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Analysis Report (USAR) Section 13, " Plant Operations," was reviewed as part of

the inspection.

In general, the conduct of operations was acceptable. Operators' performance

during routine surveillances was excellent. Command and control during the

planned reactor shutdown were excellent.

01.2 Observations of Shutdown

a.

Insoection Scoce (71707)

As discussed in Section E2.1, the licensee conservatively decided to shut down the

reactor due to concems with the emergency core cooling system (ECCS) suction

strainers, On May 9,1997, operators commenced the shutdown. The inspectors

observed portions of the evolution. Documents reviewed included:

C.3. Shutdown Procedures

TS Table 4.1.1 and 4.1.2

b.

Observations and Findinas

The inspectors observed the infrequent evolution briefings conducted for both

operations crews involved in the shutdown. Extra non-licensed, licensed, and

senior reactor operators were available to support the operations crews. Nuclear

engineering personnel were also present. In each briefing, the shif t manager

emphasized self-checking practices; maintaining a questioning attitude: roles and

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responsibilities, including expectations on communication; and reactivity

management controls.

During the shutdown sequence, the licensee conducted individual control rod scram

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testing. During the test, the inspectors observed control room operators and also

accompanied non-licensed operators in the reactor building. The test was

conducted in a controlled manner with excellent communication between control

room operators, plant operators, and the nuclear engineer. The control room

operator continuously monitored core responses to the control rod manipulations.

The nuclear engineer provided excellent support to the operators.

The inspectors verified that the activities were performed in accordance with the

C.3 procedure and that TS-required surveillances were completed prior to changing

modes.

c.

Conclusions

Control and performance of the reactor shutdown activities were excellent.

Communication and teamwork during the evolution were good.

O2

Operational Status of Facilities and Equipment

O 2.1 Ennineered Safetv Feature System Walkdowns

The inspectors used Inspection Procedure 71707 to walk down selected portions of

the #11 and #12 emergency diesel generators (EDGs), the #13 diesel generator

(non-safety related), reactor core isolation cooling (RCIC), and high pressure coolant

injection (HPCI) systems. Minor housekeeping issues identified during the

walkdowns were promptly corrected by the licensee. No operability concerns were

identified.

02.2 Anticinated Transient Without a Scram Svstem Review

a.

Insoection Scooe (71707)

During this inspection period, the inspectors performed a review of the Anticipated

Transient Without Scram (ATWS) system. The purpose of this review was to verify

various operational and design features including the following:

Operation of the system in accordance with applicable TS requirements

Operation of the system in accordance with USAR description

System alignment in accordance with plant requirements

Surveillance procedures met the TS requirements

The inspectors reviewed the following documents:

TS Table 3.2.5

TS 3/4.13.H

USAR Sections 7.6.2 and 14.8

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Operations Manual B.5.6, " Plant Protection System"

Annunciator Response Procedures

Test 1227, Revision 7, "ATWS-RPT, ATWS-ARI, ASDS Rod Insertion and

B/U Scram Valve Functional Test"

Test 0279, Revision 2, "ATWS Reactor Level and Pressure Transmitter"

Test 0278a and b, Revision 6, "ATWS Recirculation Trip for Reactor

Pressure and Level Trip Unit Test and Calibration"

Work Order (WO) 9601857, Check / Adjust damping on ATWS transmitters

WO 9601874, Check / Adjust damping on ATWS transmitters

WO 9601877 Adjust Time Delay, ATWS Relay K101B

CR (Condition Report)95-117, "DVM time delay effects on timing of ATWS

pump trip time delay"

CR 94-280, " Spurious low-low level ATWS trip"

CR 92000179/399, " Reliability of ATWS mitigation systems"

CR 94000280, " Spurious low-low level ATWS trip on "B" channel"

CR 95000117, "ATWS system timer influenced by digital volt meter during

test"

Modification 930180, Reduce Sensitivity of RPV High Pressure SCRAM

Sensing Lines

SRI 96-026, " Time Response Adjustment of ATWS Level Transmitters

LT-2-3-180A-D and Level Trip Delay"

Calculation CA-93-082, High Pressure SCRAM Time Delay

b.

Observations and Finding

The inspectors verified that periodic surveillance testing was accomplished in

accordance with TSs. Logic drawings were reviewed to verify that relays were

properly challenged during surveillances. A detailed technical review of the

surveillance tests showed that specified acceptance criteria were appropriate and

reflected design parameters. The inspectors noted that formal calculations were

not available for the acceptance criteria; however, the licensee's effort to document

supporting calculations in surveillances was ongoing.

The material condition of the system was acceptable. Valves and electrical

equipment were verified to be in the correct positions. Outstanding WOs and CRs

did not impact system operability. The inspectors reviewed previous surveillance

tests and confirme'd that acceptance criteria were met. The inspectors also

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observed instrument and control technicians perform Test 0279. The procedure

was workable and the technicians performed in a professional manner.

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The inspectors observed two operations crews respond to ATWS situations during

simulator training. The scenarios involved an ATWS with and without a standby

liquid control (SBLC) system failure. The scenarios were challenging and required

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entries into several branches of the emergency operating procedures and abnormal

procedures. The significant operator actions from a probabilistic risk assessment

perspective included controlling reactor level and injecting SBLC. The crews

responded appropriately and demonstrated knowledge of the ATWS system.

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c.

Conclusions

The inspectors concluded that the ATWS system was tested in accordance with TS

and as described in the USAR. Operators responded appropriately during simulated

ATWS conditions.

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Miscellaneous Operations issues

08.1 (Closed) Unresolved item (URI) 50-263/97003-01: Operator Unawareness of an

Operating Emergency Service Water (ESW) Pump. The ESW pumps were normally

placed in a standby condition and were designed to automatically start upon a

transfer of the normal power source to the 4160 V buses to alternate power source

1 AR transformer or EDGs. On April 8,1997, a loss of power to the #15 essential

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. electrical bus occurred. Following the restoration of normal offsite power to bus

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15, operators performed walkdowns of control room panels and failed to identify

that the #13 ESW pump was still operating. As documented in inspection Report

(IR) 50-263/97003, this condition had existed for about 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> prior to

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identification by the inspectors, on April 10,1997. During this time, four shift

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turnovers involving three crews had occurred between shift management, control

room operators, and auxiliary plant operators. Pump status lights in the control

room provided sufficient indications of an operating pump which should have been

identified by the on-shift crews. The licensee documented this issue in CR

97001149.

TS Section 6.5, " Plant Operating Procedures," required that detailed written

procedures covering plant operations areas be prepared and followed. TS Section 6.5.A.3 required written procedures covering actions to be taken to correct specific

and foreseen potential malfunction of systems or components, including follow-up

actions required after plant protective system actions have initiated. Administrative

procedure 4 AWi-04.01.01, " General Plant Operating Activities," Revision 17, step

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4.3.4.A required that all on-duty operators and the shift supervisor shall be aware

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of the plant status at all times. The failure of operations personnel from April 8 -

10,1997, to be aware of plant status, as evidenced by an unnoticed operating

safety-related pump, was contrary to the procedure and a violation of TS

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requirements (VIO 50 263/97006-01(DRP)).

11. Maintenance

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Conduct of Maintenance

M 1.1 General Comments

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a.

Insoection Scone (62703 and 61726)

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The inspectors observed all or portions of selected maintenance and surveillance

activities, included in the inspection was a review of the surveillance procedures or

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work orders listed as well as the appropriate USAR sections regarding the activities.

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b.

Observations and Findinas

In general, the inspectors found the work performed under these activities to be

professional and thorough. All work observed was performed with the work

package present and in active use. Technicians were experienced and

knowledgeable of their assigned tasks. The inspectors frequently observed

supervisors and system engineers monitoring job progress, and quality control

personnel were present whenever required by procedure. When applicable,

appropriate radiation control measures were in place.

The following work was observed. Specific concerns or observations are provided

where appropriate.

0026, APRM-Recirc Flow Instrumentation Calibration, Revision 20

0397a, SRV Low-Low Set System Quarterly Tests

WO 9704562, Collect Core Spray Pump Performance Data

WO 9703394: PC-14-2 Valve Leaks Throuah the Seat. The inspectors

independently verified the equipment isolation tagout and observed portions

of the post-maintenance test (PMT). The shift supervisor rejected the

original PMT because guidance on how to " verify no leakage through valve"

was not provided. The system engineer subsequently wrote specific steps

in an attachment to the test document.

WOs 9703795,9703797 and 9703798: Reolace Nitroaen Purae Solenoid

Valves SV3372. SV3373, and SV3381. The inspectors reviewed the

equipment isolation tags and identified that the tags placed on two root

valves were switched. Both valves were closed, therefore, this discrepancy

did not result in a personnel or equipment safety concern. The shift

manager immediately stopped the job until the discrepancy was resolved.

Prior to hanging the isolation tags, operators had noted that the root valves

were not labelled and requested assistance from the system engineer. The

system engineer reviewed the piping and instrument diagram and mistook

the valves' identities. Based on this inaccurate information, operators

subsequently hun 0 the tags on the wrong valves. Failure to hang the

isolation valves in accordance with the isolation procedure constituted a

violation of minor significance and is being treated as a Non-Cited Violation,

consistent with Section IV of the NRC Enforcement Policy

(50-263/97006 02).

WO 9704264: #12 EDG #2 Air Start Pressure Switch Huna UD. The

inspectors noted that the work was performed while the 1 AR transformer

was ooc of service and the IR transformer was degraded due to low voltage.

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The licensee responded that because the work did not render the EDG

inoperable, the reliability of the EDG would be increased. A probabilistic risk

assessment study showed an insignificant effect on risk. The inspectors

reviewed the USAR and TS and had no further concerns.

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Test 0013: IRM Scram and Rod Block /SRM Rod Block Calibration. This test

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was required per TSs 4.1 and 4.2 prior to the unit shutdown on May 9,

1997. The inspectors performed a technical review of the procedure to

verify that the acceptance criteria complied with TS-required values, the

sequence of steps did not pre-condition the test results, and the test was

conducted as described in the USAR. No discrepancies were noted.

Test 0081: Control Rod Drive Scram insertion Time Test. The inspectors

noted good communication between the plant operators, control room

operators, and the nuclear engineer. The evolution was conducted in a

controlled manner. Scram times were obtained from 113 fully withdrawn

control rods. Of the 113,8 control rods exceeded the 5 percent insertion

time acceptance criteria of 375 milliseconds. The diaphragms for the

associated scram solenoid pilot valves will be replaced prior to reactor

startup.

Test 1374: Monthiv Operability Test of #13 Diesel Generator. This diesel

generator was not safety-related but could be utilized during a station

blackout condition. The inspectors performed a technical review of the test

and verified that the system performed as described in USAR 8.4.2. The

inspectors noted that two indication lines showed signs of fretting caused by

loose metal clips. This was promptly resolved by the system engineer.

c.

Conclusions

The observed maintenance activities were performed in a professional manner and

in accordance with applicable TS and USAR requirements. However, isolation tags

for two valves were reversed because of inattention-to-detail by system

engineering.

M2

Maintenance and Material Condition of Facilities and Equipment (93702)

M2.1 Current Material Condition and Imoact on Ooerations Personnel

The inspectors conducted control room and plant inspections and interviewed

operations personnel to assess the material condition of plant equipment. During

this period, a pressure switch (PS 2-3-52-A), which provided an interlock for the

opening of the low pressure ECCS discharge valves, failed. The licensee

immediately initiated a work order and repaired the switch. The inspectors

reviewed TS table 3.2.2 and portions of USAR sections 6.2.2 and 6.2.3 and had no

concerns.

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Miscellaneous Maintenance issues (92700)

M8.1 (Closed) URI 50-263/97003-06: Personnel Errors During Undervoltage Relay

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Testing.

(Closed) Licensee Event Reoort (LER) 50-263/97006. RevisiorLQ: Emergency Diesel

Generators Started By Personnel Error During a Monthly Surveillance.

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On April 8,1997, surveillance Test 0301, " Safeguard Bus Voltage Protection Relay

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Unit Functional Test," Revision 21, was performed by testing undervoltage relays

and verifying that appropriate relay contacts closed upon the relays dropping out.

During the test, electricians failed to remove a test meter used to monitor continuity

across the relay contacts. As a result, the loss of voltage protection logic was

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satisfied resulting in the trip of the normal power source to 4160 V bus #15. This

resulted in the automatic start of the #11 and #12 EDGs and #11 EDG loading on

bus #15.

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The method to verify continuity (momentary contact or landing of meter leads) was

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left up to skill-of-the-craft, and there was no explicit procedural requirement to

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remove any installed test instruments upon completion of applicable procedure

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steps. Failure to provide adequate instructions for the performance of surveillance

Test 0301 is a violation of TS section 6.5.A.4, which required detailed written

procedures covering surveillance and testing requirements that could have an effect

on nuclear safety. However, this licensee-identified and corrected violation is being

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treated as a Non-Cited Violation, consistent with Section Vll.B.1 of the NRC

Enforcement Policy (NCV 50-263/97006-03).

As required by 10 CFR 50.73, on May 8,1997, the licensee submitted LER 97-

006, which documented the automatic actuation of an engineered safeguard

feature. The LER discussed the safety significance of the event,immediate actions,

corrective actions, and preventative actions. Corrective actions included meeting

with electrical maintenance personnel to discuss the lessons learned from this

event. Preventative actions included revising the surveillance procedure to provide

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instructions for the removal of installed test meters. Additionally, instead of using

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continuity measurements to monitor the status of relay contacts, voltage

measurement requirements were added. The inspectors witnessed the performance

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of the revised surveillance procedure 0301, " Safeguard Bus Voltage Protection

Relay Unit Functional Test," Revision 22, during the subsequent monthly testing of

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the degraded safeguards bus voltage relays. The test was satisfactorily performed.

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The inspectors considered the licensee's implementation of the corrective actions

discussed in the LER to be acceptable.

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M8.2 1 Closed) LER 50-263/97005. Revision 0: Failure to Analyze Diesel Fuel Samples

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Within the Technical Specification Required Surveillance Period, in response to

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Violation 50-263/96009-14, the licensee committed to review other surveillances

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for potential timeliness concerns. During this process, the licensee identified that

diesel generator fuel oil samples were taken monthly, but not analyzed within the

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TS surveillance time interval. Although analyzed late, all samples supported diesel

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operability. The procedure was revised to require the analysis prior to completing

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the surveillance. The inspectors considered this example to be acceptable

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implementation of corrective actions for a previous violation. Failure to analyze the

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fuel oil samples within the surveillance window is considered another example of a

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previous violation (VIO 50 263/96009 14).

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E2

Engineering Support of Facilities and Equipment

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E2.1

Concerns with Net Positive Suction Head for low Pressure ECCS Pomos

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insoection Scoce (37551)

In February 1997, the licensee initiated a CR to evaluate the applicability of a NPSH

concern identified at another nuclear utility. On April 15,1997, the licensee

completed the evaluation and concluded that the concern was applicable. The

inspectors reviewed the licensee's evaluation, prompt operability determination, and

corrective actions. Several conference calls between cognizant NRC and licensee

staff members were held throughout this period. Also, the following documents

were reviewed:

LER 50-263/97007, " inadequate NPSH for the ECCS Pumps for Certain

Single Failures During Loss of Coolant Events"

CR 97001188, " Higher ECCS Suction Strainer Head Losses Calculated"

b.

Observations and Findinas

The current NPSH calculation assumed a 1-foot head loss per 10,000 gallons per

minute (gpm) through the suction strainers. The licensee determined that the actual

calculated head loss was about 11.7 feet. The licensee identified that under certain

conditions, the available NPSH for the CS pumps was insufficient and would result

in pump cavitation. Specifically, during a design bases loss of coolant accident, a

failure of the low pressure coolant injection (LPCI) loop select logic could cause all

four RHR pumps to inject into the broken recirculation pipe. This water would

suppress the drywell pressure and subsequently decrease available NPSH. The CS

pumps would be the only pumps available to recover reactor vessellevel. About 3

minutes into the accident, the available NPSH for the CS pumps would be less than

the required NPSH and would result in pump cavitation.

The licensee concluded that the CS pumps would remain operable and would

supply sufficient flow to the reactor vessel under deficient NPSH conditions. This

conclusion was based on previous vendor testing performed on a similar pump that

operated for several hours with NPSH deficits with no observable damage. The test

pump also supplied 90 percent flow for 30 minutes without damage. The licensee

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also performed calculations to show that the degraded flow was sufficient to re-

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flood and maintain level in the vessel.

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The inspectors requested support from the NRC Office of Nuclear Reactor

Regulation staff to review the licensee's basis for operability. The staff had several

technical questions and requested additional information with respect to (1) the

material similarity of the vendor-tested pump and that installed at the plant; (2) the

assumed containment overpressure available and required; and (3) how potential

strainer plugging from debris (as discussed in NRC Bulletin 96-03, " Potential

Plugging of Emergency Core Cooling Suction Strainers by Debris in Boiling Water

Reactors," was addressed.

The licensee performed strainer clogging calculations and concluded that debris

from insulation material had the potential to further degrade the available NPSH for

the CS pumps. On May 9,1997, the licensee conservatively decided to shut down

the reactor to replace the ECCS torus suction strainers.

c.

Conclusions

The licensee's actions to address and resolve the inadequate NPSH concern were

appropriate. The decision to snut down and replace the strainers was conservative.

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E2.2 USAR Chaoter 8 Electrical Svstems Concerns

a.

Insoection Scoce (37551)

The inspectors reviewed the licensee's offsite power supplies to evaluate whether

the plant electrical configurations were as described in the USAR and TS.

b.

Observations and Findinas

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A simplified electrical one-line diagram is shown in Attachment 1 of this report.

The USAR described three transformers to supply the site with offsite power from

substations and all three sources can provide adequate power for the plant's safety-

related loads. These included primary station auxiliary transformer 2R, reserve

transformer 1R, and reserve auxiliary transformer 1 AR. Transformers 2R and 1 AR

were considered one offsite source when 1 AR was supplied from 345-kilovolt (kV)

bus #1 since numerous common mode failures existed which could ause

simultaneous de-energization of both transformers.

in order to maintain 1R transformer operable, a minimum of 119 kV was required at

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the high voltage side of the transformer. The inspectors noted that on two recent

occasions, less than 119 kV was experienced at the high side of 1R transformer

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when the #10 transformer was taken out-of service. These two instances indicated

that 1R transformer was dependent on the 345-kV lines through the #10

transformer. The inspectors were concerned that system load growth had

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increased to where the plant would be outside the licensing basis whenever the

  1. 10 transformer provided power to both the 1 AR and 1R transformers. Although

the USAR was not clear on the dependence of the 119-kV and 345-kV lines on the

  1. 10 transformer, the licensee stated that the current design was within the

licensing basis. The inspectors were provided with a safety evaluation from a 1984

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modification (84MO41) which acknowledged the dependence on the #10

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transformer and possible low 115 kV bus voltage.

Additional reviews indicated that TS 3.9.A.1 allowed for continued plant operation

with transformers 1R and 1 AR serving as the two offsite sources. However, there

were no restrictions on both transformers being powered frorn the #10 transformer.

Thorefore, a loss of the #10 transformer would cause the unavailability of both

offsite sources; the de-energization of the 1 AR transformer and less than 119 kV at

the 1R transformor. The licensee stated that although allowed by TS, the 1R and

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1 AR transformers would not both be energized from the #10 transformer,

whenever possible. This operational restriction was not described in the TS or

USAR, but was in Operations Manual B.9.3-05, "345 kV Substation," section

A.2.c. The inspectors concluded that the current design of transformers 1R and

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1 AR being dependent on #10 transformer was not described in the licensee's USAR

and required further NRC review. This issue is an inspection Followup Item (IFl 50-

263/97006-04(DRP)) pending review by the Office of Nuclear Reactor Regulation.

Additional review by the inspectors indicated a discrepancy in USAR 8.3.3,

Performance Analysis. The USAR stated that " provisions are made for automatic,

fast transfer of the auxiliary load from the primary station transformer to the

reserve transformer or the auxiliary reserve transformer": (i.e. 2R,18, and 1 AR,

respectively). The inspectors noted that the electrical design included a fast

transfer feature from transformer 2R to 1R upon protective relaying actuation.

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However, there was no fast transfer feature of the auxiliary loads from transformer

1R to 1 AR. The licensee stated that there was never a fast transfer scheme for all

auxiliary loads among the three transformers. The inspectors noted that USAR

section 8.2.1 stated that transformers 2R and 1R were of adequate size to provide

the plant's full auxiliary load requirements. However, transformer 1 AR was sized to

provide only the plant's essential 4 kV buses and connected loads. The licensee

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was asked to evaluate the USAR discrepancy. The results of that evaluation will be

reviewed during a future inspection (IFl 50-263//97006-05(DRP)).

c.

Conclusions

The inspectors identified a concern regarding the adequacy of a TS which allowed

the alignment of two power sources through a common transformer. Discrepancies

between the as-design electrical system and USAR were also identified.

E2.3 As-Built Discreoancies in RCIC 250 Vdc Motedfipatrol Center (MCC)

a.

Insoection Scoce (37551)

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The inspectors performed a review of the licensee's 50.72 event notifications

associated with the RCIC system.

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b.

Observations and Findinas

On May 6,1997, the licensee reported to the NRC that the RCIC system was

declared inoperable due to an undervoltage alarm on the 250 volts-direct current

(Vde) MCC. The following day, the RCIC was returned to service and declared

operable after replacement of internal components on the MCC undervoltage

monitoring system. Later that day, the licensee again notified the NRC regarding a

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loss of the undervoltage alarm monitoring system for the RCIC 250 Vdc MCC. In

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this case, the ability to monitor the available power to primary containment group 5

isolation valves was lost. A loss of power could have gone undetected and;

therefore, could have resulte.d in a failure of the Group 5 valves to close on

demand.

Corrective action for the first event included replacement of internal electronic

components followed by a burn-in test of the annunciator monitor circuit. For the

second event, additional electronic components were replaced which were not

replaced for the first event. The inspectors reviewed the licensee's corrective

actions and post-maintenance testing and determined that they were acceptable.

During the review of ongoing work activities, the inspectors identified discrepancies

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regarding as-built configuration. These included:

as-built wiring connections for the reflash annunciator monitor were not

accurately reflected in drawing NF-36969-1;

fuses sized at 1 ampere (A) and 1.5 A were found installed whereas drawing

NF-36969-1 required 0.5 A fuses;

in MCC cubicle D31114 (RCIC test return valve MO-3502), a 6% A fuse

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was installed where a 6 A fuse was required (also, different fuse type)

undervoltage relay isolation fuses were shown on individual MCC bucket

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drawings but not on Class 1 elementary drawings. Class 1 drawings were

defined as drawings which were considered essential to safe and reliable

plant operation,

it should be noted that the wiring and fuses within the reflash annunciator

enclosure (first 2 items above) were categorized as nonsafety-related. At the end

of the inspection period, the licensee was reviewing past modifications and design

documents to determine if the discrepancies were the result of past design

weaknesses or current design and fuse replacement practices. This issue will be an

Inspection Followup Item pending further NRC inspections of additional MCC

circuits to determine if the incorrect fuse and drawing omissions were examples of

broad deficiencies (IFl 50-263/97006-06(DRP)).

c.

Conclusions

Licensee corrective actions with respect to the RCIC annunciator circuits were

determined to be acceptable. An IFl was identified to review additional fuse

configurations and drawings.

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E2.4 Core Sorav Test Retum Valve Position Limit Switch

a.

Insoection Scone (37551)

The inspectors reviewed the licensee's corrective actions regarding the potential for

the CS test return valve to remain partially open following an ECCS signal.

b.

Observations and Findinas

CR 97001001, " Potential Limit Switch Closure of CS Test Return MOVs on ECCS

Initiation," documented that modification 90ZO71 changed the control logic for the

CS Test return motor-operated valvas (MO-1749 and MO-1750). The change was

intended to bypass the close torque switch on an ECCS auto initiation signal,

thereby closing on the limit switch. However, this logic change resulted in the

valves closing to the position where the close indication light limit switch was set

(approximately 98 percent). Therefore, the valves could remain partially open and

divert flow from the reactor to the torus.

At the time that the licensee identified this issue, the test return valves had been

manually seated closed with the torque switch; therefore, no operability concerns

existed. The licensee performed WOs 9704004 and 9704065, CS Valves MO-

1749/1750, " Limit Switch Setting Determination," to determine the true valve

position at the close limit switch indication.

The inspectors reviewed the operability determination and observed the

implementation of the WOs to evaluate the effectiveness of the corrective actions.

The test return valves were stroked open and manually closed to determine the

valves' position based on the !!mit switch indication light. The licensee's evaluation

concluded that the vaives were essentially closed upon limit switch actuation.

Additionally, mcior contactor dropout time and motor inertia would p< ovide an

additional seating force. The inspectors did not identify any deficie 1cies during the

review of the licensee's operability and reportability determinations.

c.

Conclusions

The licensee's evaluation of the conditio, r.nd corrective actions were determined

to be acceptable.

E8

Miscellaneous Engineering issues (37551)

E8.1

(Closed) IFl 50-263/96002-01: This item pertained to a discrepancy in the USAR

regarding the performance of surveillances. The inspectors observed that

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instrument technicians lifted covers off of instrumentation during surveillances.

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However, USAR section 7.6.3.3.1 stated that operations personnel must remove

the cover plate, access plug, or sealing device from instruments. The licensee has

revised the USAR section (revision 14) to allow any authorized personnel to remove

the cover plate, access plug, or sealing device from instruments.

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E8.2 (Closed) IFl 50-263/96002-02: This item pertained to a discrepancy in the USAR

regarding the required fuel pool cooling temperatures. USAR 10.2.2.3 contained

two may uum spent fuel storage pool temperatures (125 degrees Fahrenheit ( F)

and 140 F). This issue was subsequently reviewed by the NRC as documented in

IR 50-263/96003, paragraph 3.4. Using more realistic decay heat loads, the

licensee determined a maximum spent fuel pool temperature of 140 F. The

licensee has revised USAR 10.2.2.3 (revision 14) to reflect the results of the

analysis.

E8.3 (Closed) IFl 50-263/96005-05: This item pertained to a discrepancy in USAR

section 8.5.2.2 which stated that each 125 Vdc battery was rated for 96 As at a

4-hour rate. However, the actual battery capacity as indicated on the battery

nameplate was 95 As at a 4-hour rate. The licensee had evaluated the actual

battery capacity and determined that the battery size was sufficient to carry design

loads. The licensee has revised the USAR section (revision 14) to reflect the actual

battery capacity.

IV. Plant Suonort

R1

Conduct of Radiological Protection and Chemistry Controls (71750)

During normal resident inspection activities, routine observations were conducted in the

areas of radiological protection and chemistry controls. No discrepancies were noted.

P1

Conduct of Emergency Preparedness Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

area of emergency preparedness. No discrepancies were noted. Three notifications were

made to the NRC pursuant to 10 CFR 50.72. The licensee later retracted two notifications

involving a foss of a power monitoring system for the RCIC motor control center. The

inspectors agreed these events were not reportable.

S1

Conduct of Security and Safeguards Activities (71750)

During no; mal resident inspection activities, routine observations were conducted in the

areas o' security and safeguards activities. No discrepancies were noted. On May 14

1997, the intpectors met with the security superviser to discuss current security issues.

Topics included personnel performance trending, new training initiatives, status of

corrective actions to previously identified concerns, and material condition of security-

related equipment.

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V. Manaaement Meetinas

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Exit Meeting Summary

On June 3,1997, the inspectors presented the inspection results to the Plant Manager and

the Manager, Quality Services. The licensee acknowledged the findings presented.

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The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

M. Wadley, Vice President, Nuclear Generation

W. Hill, Plant Manager

M. Hammer, General Superintendent, Maintenance

K. Jepson, Superintendent, Chemistry & Environmental Protection

L. Nolan, General Superintendent, Safety Assessment

M. Onnen, General Superintendent, Operations

E. Reilly, Superir:tendent, Plant Scheduling

C. Sch!bonski, General Superintendent, Engineering

A. Ward, Manager, Quality Services

J. Wiridschill, General Superintendent, Radiation Protection

L. Wi P.orsen, Superintendent, Security

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B. Day, Training Manager

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INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 61726:

Surveillance Observations

IP 62703:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

IP 93702:

Prompt Onsite Response to Events at Operating Power Reactors

ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

50-263/97006-01

VIO

Failure to Follow Procedure: Operators Did Not Know Status of

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ESW Pump

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50-263/97006-02

NCV Failure to Hang isolation Tags on Correct Valves

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50-263/97006-03

NCV Failure to Provide Adequate instructions for Performance of

Surveillance Test

50-263/97006-04

IFl

Restrictions on Operation with #10 Transformer

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50-263/97006-05

IFl

USAR Discrepancy Regarding Fast Transfer Capability

50-263/97006-06

IFl

As-Built Discrepancies in RCIC Motor Control Center

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Closed

50-263/96002-01

IFl

Discrepancy Between USAR Description and Conduct of

Surveillances

50-263/96002-02

IFl

Discrepancy in USAR Regarding Fuel Pool Temperatures

50-263/96005-06

IFl

Discrepancy in USAR Regarding Battery Capacity

50-263/97003-01

URI

Operator Unawareness of Operating ESW Pump

50-263/97003-06

URI

Personnel Errors During Undervoltage Relay Testing

50-263/97005-00

LER

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Failure to Analyze Diesel Fuel Samples Within TS Required

Surveillance Period

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50-263/97006-00

LER

Emergency Diesel Generators Started By Personnel Error

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During a Monthly Surveillance

50-263/97006-02

NCV Failure to Hang Isolation Tags on Correct Valves

50 263/97006-03

NCV Failure to Provide Adequate instructions for Performance of

Surveillance Test

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Discussed

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50-263/96009-14

VIO

Test Results Not Evaluated Prior to Return of Equipment to

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Service

50-263/97007-00

LER

Inadequate NPSH for the ECCS Pumps for Certain Single

Failures During Loss of Coolant Events

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LIST OF ACRONYMS USED

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.A

Ampere

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ATWS

Anticipated Transient Without Scram

CR

Condition Report

CS

Core Spray

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  • F

Degrees Fahrenheit

DRP.

Division of Reactor Projects

ECCS-

. Emergency Core Cooling System

EDG

Emergency Diesel Generators

ESW -

Emergency Service Water

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gpm

. Gallons Per Minute

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HPCI

High Pressure Coolant injection

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IFl

inspection Followup Item

IR .

Inspection Report

kV

LER-'

Kilovolt

Licensee Event Report

LPCI

Low Pressure Coolant injection

MCC

Motor Control Center

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NCV

Non-Cited Violation

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NPSH

Net Positive Suction Head

PMT

Post-Maintenance Test

RCIC

Reactor Core Isolation Cooling

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RHR'

Residual Heat Removal

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SBLC

Standby Liquid Control

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TS

Technical Specification

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USAR

Updated Safety Analysis Report

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Vdc

Volt-Direct Current

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VIO

Violation

V

Volt

WO

Work Order

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ATTACHMENT 1

Simplified Electrical Diagram

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