Letter Sequence Other |
|---|
|
Results
Other: 05000267/LER-1986-022, :on 860715,failure Point in 480-volt Ac Essential Bus 1 & 2 Undervoltage Relay Logic Identified. Caused by Misunderstanding of Basic Design Requirements. Designer & Independent Reviewer Reprimanded, ML20134A365, ML20135H559, ML20135H563, ML20137B356, ML20137K999, ML20137S363, ML20140H110, ML20206T734, ML20207R947, ML20212G867
|
MONTHYEARML20074A7561983-04-27027 April 1983 Clarifies Proposed Changes in Undervoltage Protection & Reiterates Schedule for Implementation of Design Changes & Mods.Existing non-Class IE Undervoltage Relays Will Be Retained as Protection for 4,160-volt Buses Project stage: Request ML20212N6621985-08-31031 August 1985 Technical Evaluation Rept for Proposed Change to Operation of Ginna Fuel Pool Charcoal Filter Sys, Informal Rept Project stage: Request ML20135H5631985-08-31031 August 1985 Truth-Analysis/Action-Reaction Review of 480-Volt Essential Bus Tie Breaker Control Scheme, Final Rept Project stage: Other ML20135H5591985-09-13013 September 1985 Forwards Truth-Analysis/Action-Reaction Review of 480-Volt Essential Bus Tie Breaker Control Scheme, Final Rept & Provides Evaluation of Control Logic Design Project stage: Other IR 05000267/19850171985-09-13013 September 1985 Insp Rept 50-267/85-17 on 850617-0816.Violation Noted: Failure to Rept Nine Circulator Trips in 1984 & Seven Trips in 1985 & No Differential Helium Pressure Maintained When Pcrv Pressure Above 100 Psia Project stage: Request ML20137S3631985-09-13013 September 1985 Corrected Page 1 to Responding to 850614 Commitment to Perform Evaluation of Emergency Diesel Generator Control Logic Circuitry.Ltr Number Changed Project stage: Other ML20134A3651985-10-23023 October 1985 Amends Correction Portion of Item 2 (286G1A & 286G1B) in Util Re Results of Proto-Power Corp Analysis Concerning Emergency Electrical Power Sys Independence Project stage: Other ML20137B3561986-01-0303 January 1986 Informs That Design Changes Involving Emergency Diesel Generator (EDG) Control Logic Circuitry Implemented.No Single Failure Will Interfere W/Proper Operation of Redundant EDG Project stage: Other ML20137K9991986-01-14014 January 1986 Notifies That Design Changes in Emergency Diesel Generator Control Logic Circuitry Implemented,Per 850913 Commitment. Changes Assure That Failure Will Not Interfere W/Operation of Redundant Generator.Ltr Supersedes Project stage: Other ML20140H1101986-03-31031 March 1986 Submits Info Re Startup Check List for Automatic Operation of Emergency Diesel Generators,Sys Operating Procedure 92-04,in Response to NRC .Numbers Will Be Assigned to All Valves in Emergency Diesel Generator Rooms Project stage: Other ML17251A7911986-03-31031 March 1986 Reactor Containment Bldg Integrated Leakage Rate Test Project stage: Request ML20206T7341986-07-0101 July 1986 Submits Summary & Schedule of Mods to Be Performed on Emergency Diesel Generator Control Circuitry in Response to 860515 & 21 Telcons.Mods Will Be Completed Prior to Startup from Current Equipment Qualification Outage Project stage: Other ML20213G5811986-08-0707 August 1986 Draft Review of Fort St Vrain Onsite AC Standby Power Sys W/Regards to Compliance to Single Failure Criterion & Ser Project stage: Draft Other 05000267/LER-1986-022, :on 860715,failure Point in 480-volt Ac Essential Bus 1 & 2 Undervoltage Relay Logic Identified. Caused by Misunderstanding of Basic Design Requirements. Designer & Independent Reviewer Reprimanded1986-08-14014 August 1986
- on 860715,failure Point in 480-volt Ac Essential Bus 1 & 2 Undervoltage Relay Logic Identified. Caused by Misunderstanding of Basic Design Requirements. Designer & Independent Reviewer Reprimanded
Project stage: Other ML20213G5641986-11-12012 November 1986 Forwards Onsite Class 1E Power Sys Design Features Review Status Rept Based on FSAR & NRC 860814 Meeting W/Licensee & Inel Draft Review of Fort St Vrain Onsite AC Standby Power.... Resolution to Problems Requested Before Restart ML20212D8641986-12-24024 December 1986 Summary of 861209 Meeting W/Util Re Plant Emergency Electrical Power Sys.Fsar Commitment Re Emergency Diesel Generators revised.Marked-up Draft Rept Re Ac Standby Power Sys Encl ML20212G8671987-01-0909 January 1987 Forwards Rev a to EE-92-0008, Engineering Evaluation of Load Shedding,Load Auto Start Prohibit,Load Sequencing,Bus Tie Breaker Alignment & Generator Breaker Closing Portions of Emergency Diesel Generator Control Circuitry Project stage: Other ML20207R9471987-03-0606 March 1987 Rev 1 to Review of Fort St Vrain Onsite AC `Standby Power Sys Re Compliance to Single Failure Criterion & Ser Project stage: Other ML20207R9381987-03-0606 March 1987 Forwards Rev 1 to EGG-NTA-7456, Review of Fort St Vrain Onsite AC `Standby Power Sys Re Compliance to Single Failure Criterion & Ser Project stage: Approval ML20207S6271987-03-12012 March 1987 Summary of 870210 Meeting W/Util Re Emergency Diesel Generator Electrical Independence.List of Attendees Encl Project stage: Meeting 1986-12-24
[Table View] |
Text
r W.
OPublic Service ~
~., *.
Company of Colorado 2420 W. 26th Avenue, Suite 1000, Denver, Colorado 80211 March 31, 1986 Fort St. Vrain Unit No. 1 P-86228 Director of Nuclear Reactor Regulation U.S. Nuclear Regulatory Comission Washington, D.C.
20555 Attn: Mr. H. N. Berkow, Director Standardization and Special Projects Directorate Docket No. 50-267
SUBJECT:
Emergency Diesel Generators
REFERENCES:
- 1) NRC letter dated 2/24/86, Gagliardo to Lee (G-86099)
- 2) PSC letter dated 1/17/86, Gahm to Hunter (P-86046)
Dear Mr. Berkow:
This letter is in response to the NRC concerns discussed in Reference 1, regarding the startup check list for automatic operation of the Emergency Diesel Generators, System Operating Procedure (S0P) 92-04, Section 2.2.
As previously noted in Reference 2, S0P 92-04 Section 2.2 has been revised to ensure that the valves associated with Emergency Diesel Generator service water, engine lube oil drains, and engine water jacket heaters are aligned correctly for automatic Emergency Diesel Generator operation.
In addition, PSC has initiated General Services Action Request (GSAR) - 1105, to assign valve numbers to all valves in the Emergency Diesel Generator Rooms. This will include valves in the instrument air lines, which operate the service water temperature control val ves, engine lube oil drain valves and drain plugs, and engine water jacket heater valves.
PSC has implemented Procedure Deviation Report (PDR)86-290 which revises 50P 92-04 to require a I
documented valve line-up check and independent verification, for the I D 8604040050 860331 PDR ADOCK 05000267 l
P PDR
e P-86228 March 31, 1986
.., -p..
Emergency. Diesel Generator auxiliary systems.
The valve line-up check list refers to the instrument air valves for the service water temperature control valves, engine lube oil drain valves and drain plugs, and engine water jacket heater valves by nomenclature.
When valve numbers have been assigned to these valves, the valve line-up-check list will be revised to refer to the valve numbers.
These administrative changes will ensure that the valve line-ups for the Emergency Diesel Generator auxiliary systems are correct, to support automatic operation of the Emergency Diesel Generators, and that the valve line-up check and independent verification are documented.
If ou have 'any further questions, please contact M. H. Holmes at (303 480-6960.
Very truly yours, R&w H. L. Brey, Manager Nuclear Licensing and Fuels HLB /8RD:bt