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POW 28-06-01 NRC Form 384 U.S. NUCLEAR F EOULATO4Y COMMISSION APPFIOVED OMS NO. 3150-0104 EwREs ersues LICENSEE EVENT REPORT (LER)
F ACJLITY NAME (1)
DOCKET NUMSER (2)
PA(ak 0 Surry Power Station. Unit I O 15101010121810,1 loFl013 flTLE 44) lodine Spike EVENT DATE ISI LER NUMBER f6)
REPORT DATE (7)
OTHiR F ACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR E]s MONTH DAY YEAR e ACILivv e. AYES DOCKET NUM8ERtSI 5E u IAL g
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NAME TELEPHONE NUMBER AREA CODE R. F. Saunders, Station Manaaer Rio fu al;17l-;t 11 I n l t1 COMPLETE ONE LINE FOR EACH COMPONENT F AILURE DESCRIGED IN THIS REPORT (131 M
F C-REPORTA LE UTE CAU$E SYSTEM COMPONENT
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A88Th. ACT ! Limit to 1400 acecer, le, enerosmrety hfreen atng e aonce typewritsee knent USI ABSTRACT On September 27,1985 at 0800 following a controlled unit shutdown from 100%
power because Hurricane Gloria was threatening, the specific activity sample of the reactor coolant showed a dose equivalent 1-131 level of I. 36 microcuries /cc. This exceeds the dose equivalent 1-131 limit of less than 1.0 microcuries/cc specified in Tech. Spec. 3.1.D.2 and is being reported in accordance with the special reporting requirements outlined in T.S. 3.1.D. 4.
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POW 28-06-01 Nec Fere 3e4A U S NUCLE AR REQUL ATOnv COMMIS$10N LICENSt:E t: VENT REPORT (LER) TEXT CONTINUATION
<Peaoao owe a.o siso-oio4 E 1PimES 8/3i155 F ACILITV NAME til DOCEET NUh.BER (2)
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viaa Surry Power Station, Unit 1 0 15 0 0 l o l 21810 815 012 l o d0 ol 2
' 0 Il rm n-. - - we, nu.nm IODINE SPIKE Description of the Event On September 27, 1985, at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> following a unit shutdown from 100%,
because Hurricane Gloria was threatening, the Specific Actt/ity Sample of the reactor coolant showed a dose equivalent I-131 level of 1.36 microcuries/cc. This exceeds the dose equivalent I-131 limit of less than 1.0 microcuries/cc specified in Tech.
Spec. 3.1.D.2 and is being reported in accordance with the special reporting requirements outlined in Tech. Spec. 3.1.D.4.
Probable Consequences and Status of Redundant Equipment The limitations on the specific activity of the primary coolant ensure that the resulting 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> dose at the site boundary will not exceed the 10 CFR 100 limits following a postulated steam generator tube rupture.
Since the dose equivalent I-131 peak was below the Technical Specification upper limit of 10 microcuries/cc, the reactor coolant gross activity was below the value analyzed in the UFSAR for a tube rupture with 1% failed fuel. Therefore, the health and safety of the public were not affected.
Cause
The Iodine Spike was caused by known, but not specifically located, fuel element defects in the reactor core. Post shutdown conditions enhanced the release of fission products, specifically I-131.
This caused an increase of the reactor coolant specific activity.
Immediate Corrective Action
The immediate corrective action was to implement the actions required by Tech.
Spec. Table 4.1-28.
Specifically, the level of dose equivalent I-131 was monitored at least once every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> until the level returned to less than 1.0 microcuries/cc.
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POW 28-06-01 NRC Fere 3e4A U S 8eUCLE AR REQULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AreaOvEo owS w ma-cio.
EmptRES S/3115 PACILITV NAast til DOCKET 8eUMBER (2)
LER NUGASER (6)
PAGE(31 SE v T AL
- vfAR Surry Power Station, Unit I o ls jo [o [o [2 l8l 0 8l 5 0 [2l0 0l0 O j3 or 0l 3 IODINE SPIKE Supplemental Information The supplemental information required by T.S.3.1.D.4 "Special Report" is included as follows:
1.
Reactor power history 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event.
September 25, 1985 - 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at 100%.
September 26, 1985 @ 1906 -
Start rampdown at 150MW/HR.
September 26, 1985 0 2245 -
30% and holding.
September 27, 1985 0 0023 -
Continue rampdown.
September 27, 1985 0 0203 -
Unit off line.
2.
Fuel burnup by core region - as of September 27, 1985.
FUEL BATCH BURNUP S2/5A 35,581 MWD /MTU S2/6A 27,730 MWD /MTU S2/6B 30,097 MWD /MTU 6C 30,440 MWD /MTU 8A 31,186 MWD /MTU 8B 35,716 MWD /MTU 9A 20,244 MWD /MTU 98 23,083 MWD /MTU S2/984 21,62G MWD /MTU 10 8,893 MWD /MTU Cycle 8 Burnup:
7,392 MWD /MTU 3.
Prior to the reactor shutdown, the unit had established a normal letdown rate of 105 gpm.
4.
No degassing operations were performed.
5.
Duration of dose equivalent 1-131 Spike:
September 27, 1985 0 0610 Routine Sample-
. 943 microcuries /cc.
September 27, 1985 0 0800
- - Post Shutdown Sample - 1. 36 microcuries/cc.
September 27, 1985 0 1000
- - Post Shutdown Sample - 1.4 microcuries/cc.
September 27, 1985 0 1200
- - Post Shutdown Sample - I. 3 microcuries/cc.
September 27, 1985 0 1400
- - Post Shutdown Sample - 1.16 microcuries/cc.
September 27,19E.i 0 1600
- - Post Shutdown Sample
.97 microcuries/cc.
Duration approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
g,oR.=..
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| 05000280/LER-1985-001, :on 850101,safe Signal Placed in Loop B Channel 2 of Overtemp Delta T W/O Cognizance of Operations or Instrumentation Staff.Caused by Lack of Administrative Controls.Event Will Be Reviewed |
- on 850101,safe Signal Placed in Loop B Channel 2 of Overtemp Delta T W/O Cognizance of Operations or Instrumentation Staff.Caused by Lack of Administrative Controls.Event Will Be Reviewed
| | | 05000281/LER-1985-001-02, :on 850106,auxiliary Feed Pump Operated During Monthly Reactor Protection Logic Test,Contrary to Planned Evolution.Caused by Failure to Perform Test in Proper Sequence |
- on 850106,auxiliary Feed Pump Operated During Monthly Reactor Protection Logic Test,Contrary to Planned Evolution.Caused by Failure to Perform Test in Proper Sequence
| | | 05000281/LER-1985-002-03, :on 850215,svc Water Isolated to Charging Pump Intermediate Seal Cooler & Component Cooling Water Isolated.Caused by Valve Misposition Due to Operator Error. Valve Repositioned & Personnel Counseled |
- on 850215,svc Water Isolated to Charging Pump Intermediate Seal Cooler & Component Cooling Water Isolated.Caused by Valve Misposition Due to Operator Error. Valve Repositioned & Personnel Counseled
| | | 05000280/LER-1985-002-01, :on 850113,lo-lo Level in Steam Generator B Caused Reactor Scram.Caused by Failure of Personnel to Adequately Control Steam Generator Level.Feedwater Bypass Flow Indication Design Installed |
- on 850113,lo-lo Level in Steam Generator B Caused Reactor Scram.Caused by Failure of Personnel to Adequately Control Steam Generator Level.Feedwater Bypass Flow Indication Design Installed
| | | 05000281/LER-1985-002, :on 850215,charging Pump Intermediate Seal Coolers Discovered Improperly Aligned.Caused by Personnel Error.Proper Intermediate Seal Cooler Placed in Svc. Personnel Reinstructed Re Following Procedures |
- on 850215,charging Pump Intermediate Seal Coolers Discovered Improperly Aligned.Caused by Personnel Error.Proper Intermediate Seal Cooler Placed in Svc. Personnel Reinstructed Re Following Procedures
| | | 05000281/LER-1985-003, :on 850423,outside Recirculation Spray Pump a Suction Valve Found Degraded & Pump B Valve Found Inoperable.Caused by Inadequate Sector Gear & Sheared Pins in Extension Shafts.Pins Replaced |
- on 850423,outside Recirculation Spray Pump a Suction Valve Found Degraded & Pump B Valve Found Inoperable.Caused by Inadequate Sector Gear & Sheared Pins in Extension Shafts.Pins Replaced
| | | 05000280/LER-1985-003, :on 850126,reactor Tripped Due to Voltage Transient Induced on Vital Bus I When Momentary Overload Condition Caused Circuit Breaker 13 to Trip Open.Cause Unknown.Plant Returned to Stable Condition |
- on 850126,reactor Tripped Due to Voltage Transient Induced on Vital Bus I When Momentary Overload Condition Caused Circuit Breaker 13 to Trip Open.Cause Unknown.Plant Returned to Stable Condition
| | | 05000281/LER-1985-003-03, :on 850428,Type C Testing Revealed Both Outside Recirculation Spray Pump Suction Valves MOV-RS-255A, B(Eiis 20) Inoperable.On 850510,outside Recirculation Spray Pump Discharge Valve Inoperable |
- on 850428,Type C Testing Revealed Both Outside Recirculation Spray Pump Suction Valves MOV-RS-255A, B(Eiis 20) Inoperable.On 850510,outside Recirculation Spray Pump Discharge Valve Inoperable
| | | 05000281/LER-1985-004-01, :on 850501,discrepancies Noted W/Rosemount Model 1153 Transmitters & Conax Environ Seal Assemblies. Caused by Overtorqued Hollow Screws in Transmitters & Improper Installation of Connectors |
- on 850501,discrepancies Noted W/Rosemount Model 1153 Transmitters & Conax Environ Seal Assemblies. Caused by Overtorqued Hollow Screws in Transmitters & Improper Installation of Connectors
| | | 05000281/LER-1985-004-03, :on 850501,degraded Terminal Screws Used to Terminate Field Wiring Inside Rosemount Transmitters & Conax Seal Assemblies Did Not Provide Positive Environ Seal. Caused by Overtorquing Hollow Screws |
- on 850501,degraded Terminal Screws Used to Terminate Field Wiring Inside Rosemount Transmitters & Conax Seal Assemblies Did Not Provide Positive Environ Seal. Caused by Overtorquing Hollow Screws
| | | 05000280/LER-1985-004, :on 850127,reactor Tripped Due to Closing of Four Turbine Stop Valves.Caused by Insufficient Consideration of Steam Leakage Effect on Plant Parameters. Plant Parameters Returned to Stable Conditions |
- on 850127,reactor Tripped Due to Closing of Four Turbine Stop Valves.Caused by Insufficient Consideration of Steam Leakage Effect on Plant Parameters. Plant Parameters Returned to Stable Conditions
| | | 05000281/LER-1985-005-03, :on 850514 & 15,automatic Initiation of Hazard Zones 8 & 4,respectively,locked Out W/No Fire Watch Present. Caused by Lack of Procedure & Training.Procedure for CO2 Sys Lockouts Will Be Implemented |
- on 850514 & 15,automatic Initiation of Hazard Zones 8 & 4,respectively,locked Out W/No Fire Watch Present. Caused by Lack of Procedure & Training.Procedure for CO2 Sys Lockouts Will Be Implemented
| | | 05000280/LER-1985-005-01, :on 850403,operator Discovered Lockout of Automatic Initiation of CO2 for Fire Zone 7 W/O Required Fire Watch.Caused by Misunderstanding Between Personnel Re Fire Zone Tagging |
- on 850403,operator Discovered Lockout of Automatic Initiation of CO2 for Fire Zone 7 W/O Required Fire Watch.Caused by Misunderstanding Between Personnel Re Fire Zone Tagging
| | | 05000280/LER-1985-006, :on 850128,reactor Trip Occurred Due to Differential Pressure anti-motoring Turbine Trip.Caused by Isolation of Exhaust Pressure Sensing Line Root Valve in anti-motoring Instrumentation.Plant Returned to Svc |
- on 850128,reactor Trip Occurred Due to Differential Pressure anti-motoring Turbine Trip.Caused by Isolation of Exhaust Pressure Sensing Line Root Valve in anti-motoring Instrumentation.Plant Returned to Svc
| | | 05000281/LER-1985-007-02, :on 850612,spurious Safety Injection Occurred During Periodic Functional Test.Caused by Procedure Deficiency.Function Test Will Be Modified to Provide Separate Steps & Signoffs |
- on 850612,spurious Safety Injection Occurred During Periodic Functional Test.Caused by Procedure Deficiency.Function Test Will Be Modified to Provide Separate Steps & Signoffs
| | | 05000280/LER-1985-007, :on 850429,turbine/reactor Trip Occurred as Result of Main Feed Pump a Trip.Caused When Valve Open Signal Not Sent to Feed Pump Trip Logic.Valve Position Actuator Arm Modified |
- on 850429,turbine/reactor Trip Occurred as Result of Main Feed Pump a Trip.Caused When Valve Open Signal Not Sent to Feed Pump Trip Logic.Valve Position Actuator Arm Modified
| | | 05000281/LER-1985-008-01, :on 850619,auxiliary Ventilation Damper I-VS-MOD-58A Drifted Closed.Cause Undetermined.Unit 2 Containment Purge Stopped & Damper Manually Opened.Parts Needed to Repair Actuator Ordered |
- on 850619,auxiliary Ventilation Damper I-VS-MOD-58A Drifted Closed.Cause Undetermined.Unit 2 Containment Purge Stopped & Damper Manually Opened.Parts Needed to Repair Actuator Ordered
| | | 05000281/LER-1985-008, :on 850619,auxiliary Ventilation Damper 1-VS-MOD-58A Drifted Closed.Caused by Short in Damper Actuator Relief Valve Coil.Actuator Sent to Mfg for Overhaul |
- on 850619,auxiliary Ventilation Damper 1-VS-MOD-58A Drifted Closed.Caused by Short in Damper Actuator Relief Valve Coil.Actuator Sent to Mfg for Overhaul
| | | 05000280/LER-1985-008, :on 850318,tag Inadvertently Placed on Fire Zone 5,locking Out Automatic Initiation of CO2 W/O Fire Watch as Required by Tech Specs.Caused by Operator Error.Sys Returned to Automatic.Red Tags Used in Future |
- on 850318,tag Inadvertently Placed on Fire Zone 5,locking Out Automatic Initiation of CO2 W/O Fire Watch as Required by Tech Specs.Caused by Operator Error.Sys Returned to Automatic.Red Tags Used in Future
| | | 05000280/LER-1985-009, :on 850512,PORV PCV-1455C Cycled Twice Due to Overpressure Condition.Caused by Failure of Normal Letdown Pressure Control Valve PCV-1145 Due to Positioner Misadjustment.Part Adjusted |
- on 850512,PORV PCV-1455C Cycled Twice Due to Overpressure Condition.Caused by Failure of Normal Letdown Pressure Control Valve PCV-1145 Due to Positioner Misadjustment.Part Adjusted
| | | 05000281/LER-1985-009-03, :on 851107,six Individual Rod Position Indicators in Controlling Bank D & One Indicator in Bank C Declared Inoperable Due to Incorrect Positions.Caused by Instrumentation Drift.Indicators Calibr |
- on 851107,six Individual Rod Position Indicators in Controlling Bank D & One Indicator in Bank C Declared Inoperable Due to Incorrect Positions.Caused by Instrumentation Drift.Indicators Calibr
| | | 05000281/LER-1985-009, :on 851107,individual Rod Position Indicators for Six Rods in Controlling Bank D & One Rod in Controlling Bank C Indicated More than 12 Steps from Bank Demand Position.Caused by Instrument Drift |
- on 851107,individual Rod Position Indicators for Six Rods in Controlling Bank D & One Rod in Controlling Bank C Indicated More than 12 Steps from Bank Demand Position.Caused by Instrument Drift
| | | 05000281/LER-1985-010-02, :on 850813,unit Experienced Turbine Runback to Approx 48% Power Resulting in Partial Loss of Emergency Bus. Caused by Tripped Series Breaker to Vital Bus 2-1 Sola Transformer.Breakers Reset |
- on 850813,unit Experienced Turbine Runback to Approx 48% Power Resulting in Partial Loss of Emergency Bus. Caused by Tripped Series Breaker to Vital Bus 2-1 Sola Transformer.Breakers Reset
| | | 05000281/LER-1985-010-01, :on 850813,turbine Runback to Approx 48% Power Occurred,Initiating Loss of Vital Bus 2-I.Caused by Tripped Transformer Breaker.Breakers Replaced |
- on 850813,turbine Runback to Approx 48% Power Occurred,Initiating Loss of Vital Bus 2-I.Caused by Tripped Transformer Breaker.Breakers Replaced
| | | 05000280/LER-1985-010, :on 850515,intermediate Range High Flux Trip Bistables NI-35 & NI-36 Tripped at 30% & 31% Power, Respectively.Apparently Caused by Lack of Experience in Developing Intermediate Setpoints |
- on 850515,intermediate Range High Flux Trip Bistables NI-35 & NI-36 Tripped at 30% & 31% Power, Respectively.Apparently Caused by Lack of Experience in Developing Intermediate Setpoints
| | | 05000281/LER-1985-011-02, :on 851023,emergency Diesel Generator (EDG) Automatically Started.Caused by Inadequate Design Change Test Procedure.Control of EDG 2 Transferred to Main Control Room Panel & Diesel Shut Down |
- on 851023,emergency Diesel Generator (EDG) Automatically Started.Caused by Inadequate Design Change Test Procedure.Control of EDG 2 Transferred to Main Control Room Panel & Diesel Shut Down
| | | 05000280/LER-1985-011, :on 850626,while Racking Charging Pump B Breaker 15J5 Out for Pump Maint,Normal Feeder Breaker 15H6 for Operating Charging Pump C Tripped Due to Electrical Interlock.Caused by Inadequate Precautions |
- on 850626,while Racking Charging Pump B Breaker 15J5 Out for Pump Maint,Normal Feeder Breaker 15H6 for Operating Charging Pump C Tripped Due to Electrical Interlock.Caused by Inadequate Precautions
| | | 05000281/LER-1985-012-01, :on 851026,results of RCS Sample Indicated Drop in Boric Acid Concentration from 2,217 Ppm to 1,952 Ppm. Caused by Out of Calibr Flow Transmitter That Inputs to Boric Acid Integrator.Flow Transmitter Calibr |
- on 851026,results of RCS Sample Indicated Drop in Boric Acid Concentration from 2,217 Ppm to 1,952 Ppm. Caused by Out of Calibr Flow Transmitter That Inputs to Boric Acid Integrator.Flow Transmitter Calibr
| | | 05000280/LER-1985-012, :on 850609,during Testing of Discharge Valves, Chemical Addition Tank Water Level Decreased.Caused by Failed Closed Contact,Resulting in Valve Reopening.Flow Path Isolated & Failed Contacts Replaced |
- on 850609,during Testing of Discharge Valves, Chemical Addition Tank Water Level Decreased.Caused by Failed Closed Contact,Resulting in Valve Reopening.Flow Path Isolated & Failed Contacts Replaced
| | | 05000280/LER-1985-013, :on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller Unit. Component Restarted & Chiller Condenser Svc Water Tubes Cleaned |
- on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller Unit. Component Restarted & Chiller Condenser Svc Water Tubes Cleaned
| | | 05000280/LER-1985-013-01, :on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller I-CD-REF-IA Due to Tube Fouling on Water Side Causing High Chiller Condenser Pressure |
- on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller I-CD-REF-IA Due to Tube Fouling on Water Side Causing High Chiller Condenser Pressure
| | | 05000281/LER-1985-013-02, :on 851107,turbine Trip/Reactor Trip Occurred as Result of High Steam Generator Level.Caused by Operator Inexperience W/Manual Feed Control During Low Power Startup Conditions.Status Tree Reviews Performed |
- on 851107,turbine Trip/Reactor Trip Occurred as Result of High Steam Generator Level.Caused by Operator Inexperience W/Manual Feed Control During Low Power Startup Conditions.Status Tree Reviews Performed
| | | 05000281/LER-1985-014-01, :on 851226,control Rod Urgent Failure Alarm Occurred as Rods Stepping in Automatic.Caused by Problem in Logic Cabinet Pulser Card A101.Card Replaced & Sys Tested Satisfactorily |
- on 851226,control Rod Urgent Failure Alarm Occurred as Rods Stepping in Automatic.Caused by Problem in Logic Cabinet Pulser Card A101.Card Replaced & Sys Tested Satisfactorily
| | | 05000280/LER-1985-017-01, :on 850911,following Reactor trip,I-131 Level Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Equivalent Monitored Until Less than 1.0 Uci/Cc |
- on 850911,following Reactor trip,I-131 Level Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Equivalent Monitored Until Less than 1.0 Uci/Cc
| | | 05000280/LER-1985-018, :on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operation Error.Covers Placed on Inlet Valve Switches & Operator Reinstructed |
- on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operation Error.Covers Placed on Inlet Valve Switches & Operator Reinstructed
| | | 05000281/LER-1985-018-01, :on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operator Inadvertently Closing Four Condenser Inlet Valves While Throttling Four Condenser Outlet Valves |
- on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operator Inadvertently Closing Four Condenser Inlet Valves While Throttling Four Condenser Outlet Valves
| | | 05000280/LER-1985-019, :on 850927,individual Rod Position Indicator for Two Rods Inoperable.Spurious Incorrect Rod Position Indication Is Generic Westinghouse PWR Concern.Portion of Sys Outside Containment Tested & No Problems Found |
- on 850927,individual Rod Position Indicator for Two Rods Inoperable.Spurious Incorrect Rod Position Indication Is Generic Westinghouse PWR Concern.Portion of Sys Outside Containment Tested & No Problems Found
| | | 05000280/LER-1985-020, :on 850927,following Controlled Shutdown Due to Hurricane Gloria,Iodine Spike Discovered.Caused by Known Fuel Element Defects in Reactor Core.Level of Dose Equivalent I-131 Monitored Per Tech Spec Table 4.1-2B |
- on 850927,following Controlled Shutdown Due to Hurricane Gloria,Iodine Spike Discovered.Caused by Known Fuel Element Defects in Reactor Core.Level of Dose Equivalent I-131 Monitored Per Tech Spec Table 4.1-2B
| | | 05000280/LER-1985-021, :on 851114,unexpected Start of Auxiliary Feed Pump 2-FW-P-3A Occurred.Caused by Open Coil in Bfd Relay AFP-2XA.Relay Replaced & Tested Satisfactorily |
- on 851114,unexpected Start of Auxiliary Feed Pump 2-FW-P-3A Occurred.Caused by Open Coil in Bfd Relay AFP-2XA.Relay Replaced & Tested Satisfactorily
| | | 05000280/LER-1985-022-01, :on 851121,spurious auto-start of Auxiliary Vent Emergency Fans Occurred.Cause Not Determined.Steam Generator Pressure Returned to Normal & Letdown Trip Valve TV-1204 Opened |
- on 851121,spurious auto-start of Auxiliary Vent Emergency Fans Occurred.Cause Not Determined.Steam Generator Pressure Returned to Normal & Letdown Trip Valve TV-1204 Opened
| | | 05000280/LER-1985-022, :on 851121, Auxiliary Vent Sys Safety Mode Initiated Alarm Received.Caused by Momentary Decrease of Instrument Air Pressure from Ice Formation.Bypass Valve Adjusted |
- on 851121, Auxiliary Vent Sys Safety Mode Initiated Alarm Received.Caused by Momentary Decrease of Instrument Air Pressure from Ice Formation.Bypass Valve Adjusted
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