| | | Reporting criterion |
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| 05000352/LER-1996-001, :on 960111,automatic Isolation of RCIC Sys During Surveillance Testing Occurred Due to Less than Adequate Attention to Details.Counseled Technician & Held Team Meetings to Discuss Event |
- on 960111,automatic Isolation of RCIC Sys During Surveillance Testing Occurred Due to Less than Adequate Attention to Details.Counseled Technician & Held Team Meetings to Discuss Event
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000353/LER-1996-001-02, :on 960220,condition Prohibited by TS in That Two Independent SGTS Inoperable Due to Personnel Error. Counseled EO & Conducted Operator Standdown Meetings to Discuss Event |
- on 960220,condition Prohibited by TS in That Two Independent SGTS Inoperable Due to Personnel Error. Counseled EO & Conducted Operator Standdown Meetings to Discuss Event
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-002, :on 960118,unit Operated in Excess of 100% Rated Power Due to Core Thermal Power Calculation Methodology Error.Reactor Heat Balance Revised |
- on 960118,unit Operated in Excess of 100% Rated Power Due to Core Thermal Power Calculation Methodology Error.Reactor Heat Balance Revised
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000353/LER-1996-002-02, :on 960315,ESFA Occurred Due to Loss of Power to Rps/Ups Power Distribution Panel.Caused by Inadvertent Actuation of Underfrequency Relay.Created Necessary Addl Physical Barriers Arounds Units 1 & 2 |
- on 960315,ESFA Occurred Due to Loss of Power to Rps/Ups Power Distribution Panel.Caused by Inadvertent Actuation of Underfrequency Relay.Created Necessary Addl Physical Barriers Arounds Units 1 & 2
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000353/LER-1996-003-02, :on 960314,failed to Perform Accelerated Surveillance Testing of Unit 2 EDG Due to Inadequate Evaluation Program.Reviewed & Enhanced Program & Associated Implementing Documents for Failure Evaluations |
- on 960314,failed to Perform Accelerated Surveillance Testing of Unit 2 EDG Due to Inadequate Evaluation Program.Reviewed & Enhanced Program & Associated Implementing Documents for Failure Evaluations
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-003, :on 960204,ESFA Occurred Due to Loss of Power to Rps/Ups Power Distribution Panel Caused by Spurious Actuation of Underfrequency Relay.Replaced Relay |
- on 960204,ESFA Occurred Due to Loss of Power to Rps/Ups Power Distribution Panel Caused by Spurious Actuation of Underfrequency Relay.Replaced Relay
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000353/LER-1996-004-02, :on 960514,reactor Scram Resulted from Main Generator Lockout Due to Actuation of Voltz/Hertz Relay. Caused by Inadequate Design Change Package.Relay 359/381A Drawing Corrected & Relays Inspected |
- on 960514,reactor Scram Resulted from Main Generator Lockout Due to Actuation of Voltz/Hertz Relay. Caused by Inadequate Design Change Package.Relay 359/381A Drawing Corrected & Relays Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-004, :on 960206,reactor Scram Signal Occurred While in Hot Shutdown Due to Operator Error During Depressurization.Provided Briefing Sheet to Operations Managers |
- on 960206,reactor Scram Signal Occurred While in Hot Shutdown Due to Operator Error During Depressurization.Provided Briefing Sheet to Operations Managers
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) |
| 05000353/LER-1996-005-02, :on 960527,automatic Actuation of ESF Occurred. Caused by Burnt Circuit Board Trace on Relay Board.Radiation Monitor Satisfactorily Tested & Returned |
- on 960527,automatic Actuation of ESF Occurred. Caused by Burnt Circuit Board Trace on Relay Board.Radiation Monitor Satisfactorily Tested & Returned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-005, :on 960207,daily RECW Sys Fluid Sample Not Obtained & Analyzed within 24 H as Required by TS 3.3.7.1. Caused by Personnel Error & Inadequate Chemistry Section Sampling Program.Program Revised |
- on 960207,daily RECW Sys Fluid Sample Not Obtained & Analyzed within 24 H as Required by TS 3.3.7.1. Caused by Personnel Error & Inadequate Chemistry Section Sampling Program.Program Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-006-01, Forwards LER 96-006-01 Re Multiple Instances of Loss of Safety Function of Control Room Emergency Fresh Air Sys, Resulting in Operating Conditions Prohibited by Tech Specs | Forwards LER 96-006-01 Re Multiple Instances of Loss of Safety Function of Control Room Emergency Fresh Air Sys, Resulting in Operating Conditions Prohibited by Tech Specs | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-006, :on 960207,control Room Emergency Fresh Air Sys Declared Inoperable.Caused by Flow Switch Coordination Deficiency.Flow Switches Adjusted,Station Guidance Revised & Site Staff Training Performed |
- on 960207,control Room Emergency Fresh Air Sys Declared Inoperable.Caused by Flow Switch Coordination Deficiency.Flow Switches Adjusted,Station Guidance Revised & Site Staff Training Performed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) |
| 05000353/LER-1996-006-02, :on 961202,inadvertent Start of D21 Edg,An ESF During Surveillance Testing Was Noted.Caused by Malfunction of Test Switch Box.Test Box Was Repaired & Tested & Generic Implications of Event Was Evaluated |
- on 961202,inadvertent Start of D21 Edg,An ESF During Surveillance Testing Was Noted.Caused by Malfunction of Test Switch Box.Test Box Was Repaired & Tested & Generic Implications of Event Was Evaluated
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000352/LER-1996-007, :on 960220,trip of FPC Pumps Resulted in Loss of Core Circulaton & Decay Heat Removal.Caused by Insufficient Procedural Guidance.C/A:Assessment Performed |
- on 960220,trip of FPC Pumps Resulted in Loss of Core Circulaton & Decay Heat Removal.Caused by Insufficient Procedural Guidance.C/A:Assessment Performed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) |
| 05000353/LER-1996-007-02, :on 961206,manual Scram Occurred Due to Leak in Main Turbine EHC Sys.Caused by Failure of Pressure Switch Support Bracket & Tubing.Replaced Failed Bracket & Tubing & Performed Walkdown of Main Steam Sys |
- on 961206,manual Scram Occurred Due to Leak in Main Turbine EHC Sys.Caused by Failure of Pressure Switch Support Bracket & Tubing.Replaced Failed Bracket & Tubing & Performed Walkdown of Main Steam Sys
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) |
| 05000353/LER-1996-008-01, :on 961214,two Closed Primary Containment Isolation Valves Were Discovered W/Motor Operator Breaker Closed.Caused by Personnel Error.Procedure GP-2 Will Be Revised to Separate Specific Steps |
- on 961214,two Closed Primary Containment Isolation Valves Were Discovered W/Motor Operator Breaker Closed.Caused by Personnel Error.Procedure GP-2 Will Be Revised to Separate Specific Steps
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000353/LER-1996-008, Forwards LER 96-008-00 Which Documents Event That Occurred at Lgs,Unit 2 on 961214.Commitment Made within Ltr,Listed | Forwards LER 96-008-00 Which Documents Event That Occurred at Lgs,Unit 2 on 961214.Commitment Made within Ltr,Listed | |
| 05000352/LER-1996-008, :on 960303,HPCI,ESFA & Condition Which Could Have Prevented Intended Safety Function Occurred Due to Personnel Error.Issued Event Training Bulletin to All I&C Technicians by 960415 |
- on 960303,HPCI,ESFA & Condition Which Could Have Prevented Intended Safety Function Occurred Due to Personnel Error.Issued Event Training Bulletin to All I&C Technicians by 960415
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-009-01, :on 960422,main Steam System Safety Relief Valve Setpoint Drift Occurred.Caused by Corrosion Induced Bonding Between Pilot Disc & Seat.Installed Special Modified Pilot Disc in Several SRVs |
- on 960422,main Steam System Safety Relief Valve Setpoint Drift Occurred.Caused by Corrosion Induced Bonding Between Pilot Disc & Seat.Installed Special Modified Pilot Disc in Several SRVs
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000353/LER-1996-009-03, :on 961224,unit Scram & Reactor Protection Sys Actuation Occurred Due to Failure of Bill Joint That Connects Recirculation Pump Motor Generator Set Scoop Tube to Tube Positioner.Failed Ball Joint Was Replaced |
- on 961224,unit Scram & Reactor Protection Sys Actuation Occurred Due to Failure of Bill Joint That Connects Recirculation Pump Motor Generator Set Scoop Tube to Tube Positioner.Failed Ball Joint Was Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000353/LER-1996-009, Forwards LER 96-009-00,documenting Event That Occurred at Limerick Generating Station,Unit 2 on 961224.LER Is Being Submitted Pursuant to Requirements of 10CFR50.73(a)(2)(iv) | Forwards LER 96-009-00,documenting Event That Occurred at Limerick Generating Station,Unit 2 on 961224.LER Is Being Submitted Pursuant to Requirements of 10CFR50.73(a)(2)(iv) | 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000352/LER-1996-009, :on 960314,five of Six as-found Setpoint Tests on Main Steam Sys SRVs Found Outside Required Pressure Ranges.Caused by Setpoint Drift Due to Corrosion Induced Bonding.Modified Pilot Disc Installed in SRVs |
- on 960314,five of Six as-found Setpoint Tests on Main Steam Sys SRVs Found Outside Required Pressure Ranges.Caused by Setpoint Drift Due to Corrosion Induced Bonding.Modified Pilot Disc Installed in SRVs
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-010, :on 960423,discovered Two Remote Shutdown Panel (RSP) Control Circuits Inoperable.Caused by Inadequate Procedures.Rsp Surveillance Test Procedures Revised by 960731 and RSP Cleaned by 960731 |
- on 960423,discovered Two Remote Shutdown Panel (RSP) Control Circuits Inoperable.Caused by Inadequate Procedures.Rsp Surveillance Test Procedures Revised by 960731 and RSP Cleaned by 960731
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-011, :on 960425,manual Operation of CREFAS Sys Resulted from Initiation of Toxic Chemical Detection Sys. Caused by Insufficient Guidance in Planning Process.Work Packages for Cleaning & Sealing Reviewed |
- on 960425,manual Operation of CREFAS Sys Resulted from Initiation of Toxic Chemical Detection Sys. Caused by Insufficient Guidance in Planning Process.Work Packages for Cleaning & Sealing Reviewed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-012, :on 921103,identified Improper Fuse Sizing. Caused by Personnel Error.Approved Design Change Re Proper Fuse Coordination & Reviewed Modifications Associated W/Fuse Ratings |
- on 921103,identified Improper Fuse Sizing. Caused by Personnel Error.Approved Design Change Re Proper Fuse Coordination & Reviewed Modifications Associated W/Fuse Ratings
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-013, :on 960521,Unit 1 Reactor Scram Occurred.Caused by Inadequate Procedural Guidance & Undetermined Equipment Malfunction.Procedure Will Be Revised to Ensure Appropriate Barriers,In Place to Minimize Risk of Scram |
- on 960521,Unit 1 Reactor Scram Occurred.Caused by Inadequate Procedural Guidance & Undetermined Equipment Malfunction.Procedure Will Be Revised to Ensure Appropriate Barriers,In Place to Minimize Risk of Scram
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-014, :on 960702,discovered Improperly Controlled Safeguards Information.Cause Undeterminate.Corrective Actions Will Be Provided by 960930 |
- on 960702,discovered Improperly Controlled Safeguards Information.Cause Undeterminate.Corrective Actions Will Be Provided by 960930
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000352/LER-1996-015, :on 960726,failure to Maintain Equipment Needed for Operator Actions to Assure Fire Safe SD Capability. Caused by Unclear Ownership & Accountability of Procedures. Interim Procedure Revs Implemented |
- on 960726,failure to Maintain Equipment Needed for Operator Actions to Assure Fire Safe SD Capability. Caused by Unclear Ownership & Accountability of Procedures. Interim Procedure Revs Implemented
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-016, :on 960725,core Thermal Power Exceeded Licensed Power Limit During Power Transient.Caused by Defective EHC Sys Component & Reactor Scram.Defective Primary Frequency/ Voltage Converter Replaced & Calibration Performed |
- on 960725,core Thermal Power Exceeded Licensed Power Limit During Power Transient.Caused by Defective EHC Sys Component & Reactor Scram.Defective Primary Frequency/ Voltage Converter Replaced & Calibration Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-017, :on 960820,4 EDGs Inoperable Resulting from Separate Crankcase Pressurization Events.Caused by Plugging of Exhaust Stack Bird Screens by Rust Debris in Stream Gas Flow.Exhaust Stacks Scraped,Cleaned & Vacuumed |
- on 960820,4 EDGs Inoperable Resulting from Separate Crankcase Pressurization Events.Caused by Plugging of Exhaust Stack Bird Screens by Rust Debris in Stream Gas Flow.Exhaust Stacks Scraped,Cleaned & Vacuumed
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-018-01, Forwards LER 96-018-01 Which Discusses Event That Occurred on 960925 Re Inoperability of HPCI Sys Due to Loss of HPCI Turbine Speed Signal Caused by Loose Speed Sensor Connector | Forwards LER 96-018-01 Which Discusses Event That Occurred on 960925 Re Inoperability of HPCI Sys Due to Loss of HPCI Turbine Speed Signal Caused by Loose Speed Sensor Connector | 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000352/LER-1996-018, :on 960925,single Train HPCI Sys Was Declared Inoperable Due to Loose Signal Cable Connector.Connector Was Replaced on 970102 & Common HPCI Turbine Maint Procedures Have Been Revised |
- on 960925,single Train HPCI Sys Was Declared Inoperable Due to Loose Signal Cable Connector.Connector Was Replaced on 970102 & Common HPCI Turbine Maint Procedures Have Been Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-019, :on 961026,capability to Reject Electrical Load of RHR Pump Not Fully Verified.Caused by Inadequate Test Procedure.Tests Will Be Revised Prior to Next Performance & TS Change Request Is Being Pursued |
- on 961026,capability to Reject Electrical Load of RHR Pump Not Fully Verified.Caused by Inadequate Test Procedure.Tests Will Be Revised Prior to Next Performance & TS Change Request Is Being Pursued
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000352/LER-1996-020, :on 961205,primary Containment Isolation Valves Inadvertently Closed Due to Personnel Error.Reopened Valves & Counseled Individual Involved on Work Techniques |
- on 961205,primary Containment Isolation Valves Inadvertently Closed Due to Personnel Error.Reopened Valves & Counseled Individual Involved on Work Techniques
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) |
| 05000352/LER-1996-021-01, Forwards LER 96-021-01 Re Ability to Achieve Safe Shutdown in Event of Fire as Provided by Fire Protection Program | Forwards LER 96-021-01 Re Ability to Achieve Safe Shutdown in Event of Fire as Provided by Fire Protection Program | |
| 05000352/LER-1996-021, :on 841026,determined Fire Safe Shutdown Made in Fire Safe Shutdown Repair Would Not Function as Desired Due to Incorrect Assumption.Revised Fire Safe Shutdown Procedures |
- on 841026,determined Fire Safe Shutdown Made in Fire Safe Shutdown Repair Would Not Function as Desired Due to Incorrect Assumption.Revised Fire Safe Shutdown Procedures
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) |
| 05000352/LER-1996-022-01, Forwards LER 96-022-01 Re Event Which Occurred on 961102 Re Amount of Fuel Oil Contained in D14 EDG Fuel Oil Storage Tank.Challenging Method for Determining Tank Oil Level Resulted in Operator Obtaining an Incorrect Level Re | Forwards LER 96-022-01 Re Event Which Occurred on 961102 Re Amount of Fuel Oil Contained in D14 EDG Fuel Oil Storage Tank.Challenging Method for Determining Tank Oil Level Resulted in Operator Obtaining an Incorrect Level Reading | 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-022, :on 961102,D14 EDG Was Declared Inoperable Due to Low Fuel Oil in Storage Tank.Caused by Challenging Method for Determining Tank Level.Increased Operator Awareness of Potential for Error Is Being Utilized |
- on 961102,D14 EDG Was Declared Inoperable Due to Low Fuel Oil in Storage Tank.Caused by Challenging Method for Determining Tank Level.Increased Operator Awareness of Potential for Error Is Being Utilized
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000352/LER-1996-023, :on 950403,FPS Surveillance Tests Not Performed.Caused by Personnel Error.Individuals Involved Disciplined & New Supervisor Assigned to Onsite Fire Protection Group |
- on 950403,FPS Surveillance Tests Not Performed.Caused by Personnel Error.Individuals Involved Disciplined & New Supervisor Assigned to Onsite Fire Protection Group
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) |