ML20133F173

From kanterella
Jump to navigation Jump to search
Insp Rept 50-458/96-16 on 961103-1214.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support
ML20133F173
Person / Time
Site: River Bend Entergy icon.png
Issue date: 01/07/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20133F149 List:
References
50-458-96-16, NUDOCS 9701140093
Download: ML20133F173 (21)


See also: IR 05000458/1996016

Text

. . _ - - . . _ . . . . .

_

_ _ _

-___ _.__ ___. _ _. _-~._.

.

_ _ , . _ _ _ . _ _ . . _ . _ -

_

.

4

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

l

l.

REGION IV

,

Docket No.:

50-458

License No.:

NPF-47

Report No.:

50-458/96-016

Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station

Location:

P.O. Cox 220

St. Francisville, Louisiana 70775

Dates:

November 3 through December 14,1996

l

Inspectors:

W. F. Smith, Senior Resident inspector

l

D. L. Proulx, Resident inspector

i

W. M. McNeill, Reactor inspector, Division of Reactor

l

Safety

!

,

l

Approved By:

P. H. Harrell, Chief, Project Branch D

j

!

Division of Reactor Projects

l

'

Attachment:

Supplemental information

i

,

i

!

4

I

l

!

9701140093 970107

PDR

ADOCK 05000458

O

PDR

O

.

EXECUTIVE SUMMARY

River Bend Station

NRC Inspection Report 50-458/96-16

This inspection included aspects of licensee operations, maintenance, engineering, and

plant support. The report covers a 6 week period of resident inspection.

Operations

In general, the conduct of plant operations was professional and reflected a focus

on safety. Operators responded appropriately to the isophase duct cooling fan

failure. The control room was operated in a formal manner (Section 01.1).

j

A detailed walkdowr. inspection verified that the hydrogen mixing, purge,

recombiners, and igniters were capable of performing their intended safety function;

however, the inspectors identified a violation for failure to maintain adequate valve,

switch, and breaker lineup attachments for the system operating procedure

(Section O2.1).

The inspectors identified a violation because an operator failed to implement the

requirements of Technical Specifications (TS) 3.0.6 and 5.5.10, " Safety Function

Determination Program." The licensee determined that operators demonstrated

inadequate knowledge of the design bases and TSs by not identifying that

concurrently removing the high pressure core spray (HPCS) and low pressure core

spray (LPCS) systems from service could have constituted a loss of safety function

j

and required entry into TS 3.0.3 for approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> (Section 04.1).

Maintenance

I

Maintenance planners did not have adequate knowledge of the effect on plant

safety of the retest for work on a standby service water (SSW) pump.

Consequently, the licensee did not adequately assess the effects of delays in the

maintenance schedule that caused work to be performed concurrently

(Section 04.1).

During the Division til Emergency Diesel Generator (EDG) maintenance, the

electricians and mechanics properly performed the activities (Section M1.1).

A spent fuel pool cooling pump was inoperable for an excessive amount of time (10

months) because of low system flow. When the cause of the low flow was

determined to be heat exchanger fouling, the licensee did not perform the required

inservice testing (IST) prior to returning the pump to service. The inspectors

l

identified a violation for failure to obtain a new set of reference values prior to

placing a safety-related pump in service after performing analyses (Section M1.2).

t

The IST of the Division i standby liquid control (SLC) pump was performed

satisfactorily and in accordance with procedures. The operator performing the IST

,

of the Division I SLC pump exhibited a questioning attitude by ensuring that the

procedure was technically correct prior to performance (Section M1.3).

t

.

.

-2-

An operator performed the IST of the Division ll SSW system well and obtained

satisf actory results. The inspectors noted that a continuing procedure problem with

meeting ASME Code Section XI vibration measurements existed. This was the

subject of a violation in NRC Inspection Report 50-458/96-15 and corrective actians

had not yet been completed (Section M1.4).

Enaineerino

The licensee responded properly to the inappropriate use of chemicals in the plant

by correcting the specific problem and strengthening the chemical control program.

A noncited violation (NCV) was identified for failure to comply with the chemical

,

control procedure (Section E2.1).

i

The initial operability assessment of the control room air conditioning system upon

discovery of a mispositioned test switch was weak in that it did not properly

'

consider the response of the system actuation logic during a design basis accident.

Following questioning by the inspector, the licensee determined that a violation of

TS 3.0.4 occurred; however, the inspectors identified this deficiency as an example

of a configuration control violation in NRC Inspection Report 50 458/96-15

(Section E8.1).

Plant Succort

Housekeeping and plant material condition continued to be excellent throughout the

inspection period (Section 01.1).

The November 14,1996, failure to lock the door to a locked high rat.iation area was

an isolated incident that the licensee appropriately dispostioned. Ar. NCV was

identified for f ailure to comply with TS 5.7.2 (Section R1.1).

_-.

.

~-. ..

.~.

- ~ - - -

- - . _ - . - - - - . - . - . . - - - - - - - - .

.

i

.

1

,

l

Report Details

l

Summary of Plant Status

The plant operated at essentially 100 percent power for the duration of this inspection

period, except on November 16,1996, when it was necessary to lower power to

)

approximately 60 percent because of an isophase duct cooling fan failure. By

November 19, af ter repairs, power was restored to 100 percent.

i

,

1. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent reviews of ongoing plant operations including

,

i

control room observations, attendance at plan-of-the-day meetings, and plant tours.

j

In general, the conduct of plant operators was professional and reflected a focus on

safety. During plant tours, the inspectors noted that housekeeping continued to be

excellent. Any minor discrepancies identified by the inspectors were promptly

l

corrected.

1

The inspectors reviewed the operator actions to reduce power subsequent to the

failure of the nonsafety-related isophase duct cooling fan. Power was reduced to

approximately 60 percent to reduce the heat load on the isophase duct to a level

that would not cause overheating without the fan. The operators followed the

appropriate operating procedures to reduce power and then subsequently restored

power in a well-controlled manner.

02

Operational Status of Facilities and Equipment

O2.1 Enaineered Safety Feature System Walkdown (71707)

a.

Insocction Scooe

The inspectors performed walkdowns of the systems that constitute the hydrogen

control system including the hydrogen mixing, hydrogen recombiner, hydrogen

igniter, and hydrogen purge systems. In addition, the inspectors reviewed

completed surveillance procedures and closed out condition reports (CR) to

determine the overall condition of these systems,

b.

Observations and Findinos

The inspectors noted that the systems were lined up pmoerly and that the operating

procedures adequately translated the design bases into operating practices. The

inspectors reviewed the applicable portions of the Updated Final Safety Analysis

.

Report (UFSAR) and found no discrepancies. The inspectors reviewed completed

l

surveillance test procedures and noted that the tests were satisfactorily completed

l

and documented. On a sampling basis, the inspectors reviewed closed condition

1

!

_ _ - .

-_ _

.

. _- -

i

!

l

.

2-

reports and found that the appropriate corrective actions had been implemented.

The inspectors walked down Procedure SOP-0040, " Hydrogen Mixing, Purge,

Recombiners, and Igniters," Revision 9. Procedure SOP-0040 was well written and

provided clear and correct instructions on system operation. However, the

following deficiencies were identified with the valve, switch, and breaker lineup

j

enclosures to the procedure:

l

l

Each of the four igniter panels had a master breaker that was not identified

l

on the Procedure SOP-0040 breaker lineup. Failu.e to verify these breakers

'

closed could have resulted in no less than 5, and possibly all 20, igniter

circuits being unable to perform their intended safaty function.

Procedure SOP-0040, Attachment 3C, " Electrical Lineup for the Hydrogen

Recombiners," conflicted with Attachment 4C, " Control Board Lineup -

Hydrogen Recombiners," in that Attachment 3C required the breakers to be

open while Attachment 4C required the breakers to be closed.

l

l

Procedure SOP-0040, Attachment 1, " Valve Lineup for Hydrogen Purge,"

failed to specify the required status for Valves CPP-V3, -V4, and -V5.

Valve CPP-V3 was specified open in lieu of locked open, Valve CPP-V4 was

specified locked / capped instead of locked closed and capped, and

l

Valve CPP-V5 was specified capped in lieu of closed and capped.

l

The inspectors found the above breakers and valves in the proper position for

operability. Except for failure to address master brsaker positions in the igniter

i

panels, the other examples occurred during the procedure upgrade process since

personnel had correctly aligned the systems using Procedure SOP-0040, Revision 8.

i

The above procedure inadequacies constitute a violation of TS 5.4.1.a

l

(50-458/9616-01).

l

c.

Conclusions

The inspectors concluded that the hydrogen mixing, purge, recombiner, and igniter

systems were capable of performing their intended safety function; however, a

violation was identified for failure of the licensee to maintain adequate valve,

switch, and breaker lineup attachments for the system operating procedure. This

violation resulted, in part, because of errors introduced during the procedure

l

upgrade process,

i

.

.

l

l

i

i -

I

-3-

04

Operator Knowledge and Performance

j

04.1 Potential Entrv Into TS 3.0.3 Dudna On-Line Maintenance

l

'

a.

Insoection Scoce (71707)

l

lhe inspectors reviewed control of on-line maintenance from November 11-15 to

ensure that the work was adequately sequenced such that a loss of safety function

did not exist. The inspectors reviewed the control room operator logs, the limiting

l

condition for operation (LCO) logs, administrative procedures, and monitored work

in progress.

b.

Observations and Findinas

On November 12 the licensee removed Unit Cooler HVR-UC5 (HPCS pump room

cooler) from service for planned inspection and maintenance. This activity rendered

the HPCS system inoperable, which was a 14-day shutdown LCO. The work

management center had scheduled this work to be complete on November 13 but

l

extended the maintenance because mechanics found a baffle plate missing in Unit

Cooler HVR-UC5. Further, the licensee had scheduled maintenance and testing of

l

Pump SWP-P2C (SSW Pump C), after personnel completed the work on the unit

l

cooler. Because of the delays in restoring Unit Cooler HVR-UC5 to operable,

personnel allowed these two work activities to be performed simultaneously.

The inspectors reviewed the work sequence and noted that on November 14, the

operators declared Division i SSW inoperable because both Pump SWP-P2A (SSW

Pump A) and Pump SWP-P2C were locked out to perform a retest. Therefore, at

the same time, both the HPCS pump and Division l SSW were inoperable. The

inspector noted that TS 3.5.1.H requires that operators enter TS 3.0.3 if HPCS and

LPCS are both inoperable because this situation would entail a loss of spray cooling,

which is an unanalyzed condition. This condition existed approximately from 3:30

to 4:30 p.m.

TS 3.0.6 provides general principles that cascading of TSs is not required even

though supported systems are inoperable unless directed to enter another TS action.

TS 3.0.6 also implements TS 5.5.10, " Safety Function Determination Program,"

which is intended to ensure a loss of safety function does not occur as a result of

l

entry into multiple TSs. TS 5.5.10 states, in part, "...a loss of safety function may

exist when a support system is inoperable, and: a. A required system redundant to

system (s) supported by the inoperable support system is also inoperable; or..."

Procedure OSP-0040,"LCO Tracking and Safety Function Determination Program,"

Revision 1, Step 3.4.1 specified that a cross-divisional check must be performed to

,

ensure that no loss of safety function goes undetected and Step 4.2.5, specified

when TS 3.0.6 is entered to prevent entering additional LCOs for supported

systems, perform an evaluation in accordance with TS 5.5.10 to ensure no loss of

safety function exists. Further, Procedure OSP-0040, Enclosure 1,

,

!

l

l

-.

.. .

.

.

.

.

l

i

!

!

t

.

4

!

" Support-Supported LCO Matrix," requires upon entry into support system LCO

l

TS 3.7.1 (SSW), a review of supported system LCO 3.5.1 (ECCS-Operating).

The inspectors determined that the Division l SSW supported LPCS and that HPCS

was redundant to LPCS as defined in the UFSAR accident analyses and TS 3.5.1.H.

The inspectors determined that the failure to invoke TS 5.5.10 as required by

TS 3.0.6 and Procedure OSP-0040is a violation (50-458/9616-02).

)

l

The inspectors questioned the control room supervisor (CRS) on the appropriateness

of this operating condition. The CRS did not consider HPCS and LPCS to be

,

!

redundant systems because one provides high pressure spray and the other

provides low pressure spray to the core. The CRS did not consider the spray

cooling function to be a credited safety function. Further, the CRS noted that

TS 3.7.1.G required that operators enter TS 3.8.1.8 and that TS 3.8.1.B allows

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> to perform an evaluation to determine if a loss of safety function existed;

also, the CRS knew that the work scheduled would take less than 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The

inspectors noted that the words in the bases for TS 3.8.1.B specify upon discovery;

whereas, this was an intentional entry by facility personnel.

The inspectors discussed the above issue with the operations and licensing

managers, who agreed that rendering the Division i SSW system inoperable with the

HPCS system inoperable was inappropriate and would potentially place the plant in

TS 3.0.3. The licensee initiated CR 96-1976 to enter this issue into the corrective

l

action program. The initiallicensee investigation revealed that most of the licensed

operators at River Bend were unaware that HPCS and LPCS were considered to

have a redundant required safety function. In addition, the licensee noted that most

operators were unaware that the Basis for TS 3.8.1.B stated that the Divisions I, ll,

and lll emergency core cooling systems were considered to be redundant to each

other. The licensee determined from interviews that, although Division i SSW was

inoperable as documented in the LCO 10g, work was not actually in progress while

Unit Cooler HVR-UCS was removed from service.

During a subsequent interview with the CRS, the inspectors noted that the CRS

thought it was appropriate to allow HPCS and Division i SSW to be inoperable at

the same time because he considered Unit Cooler HVR-UC5 available at a moment's

notice. in addition, the CRS could have stopped testing on SSW and returned one

pump to full operability from the control room well within the 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> permitted by

TS 3.8.1.B.

l

Maintenance planners did not recognize that the retest for the work on

t

l

Pump SWP-P2C required rendering Division i SSW inoperable. The licensee did not

l

reanalyze the effect of delays in work on Unit Cooler HVR-UC5 to ensure that other

scheduled work did not inappropriately overlap. The inspectors determined that

l

aspects of the maintenance rule were not effectively implemented.

10 CFR 50.65(a)(3) requires that an assessment of total plant equipment out of

service should be taken into account to determine the overall effect on performance

l

l

!

(

l

l

.

.s. )

of safety functions. NUMARC 93-01, " Industry Guideline for Monitoring the

Effectiveness of Mainter'ance at Nuclear Power Plants," Section 11.2.3 specifies, in

l

part, that prior to actually removing a system from service to begin maintenance,

the condition of the plant should be reviewed to verify that conditions are

acceptable to take the system out of service.

The inspectors determined that the licensee implemented the Maintenance Rule

using Procedure PEP-0219, " Reliability Monitoring Program," Revision 4.

Specifically, Procedure PEP-0219, Step 6.12 implemented the requirements for

taking equipment out of service, which included evaluating the effect of removing

safety-related equipment from service prior to removal for preventive maintenance,

surveillance, et cetera. Also, Step 6.12 specified that detailed guidance can be

found in Guideline EDG-AN-0002, " Guideline for On-line Maintenance at RBS."

Guideline recommendations included reminding personnel that multiple cross

divisional outages should not be scheduled concurrently and that TS 3.0.6 and

TS 5.5.10 need to be considered. Also, Guideline EDG-AN-0002, Step 5.2.4

identified that emergent work resulting from equipment failures and schedule

changes caused by changing plant conditions should be evaluated by the work

management center or an onshift senior reactor operator.

c.

Conclusions

The inspectors identified a violation because operators failed to recognize the need

to implement the safety function determination program. The licensee determined

that operators had inadequate knowledge of the design bases and TS since they did

not know that concurrently removing the HPCS and LPCS systems from service

might have constituted a loss of safety function and required entry into TS 3.0.3.

Maintenance planners did not have adequate knowledge of the effect on plant

safety of the retest for work on a SSW pump. The licensee did not adequately

review the consequences of delays that resulted in work to be performed

concurrently, as required by the Maintenance Rule and administrative procedures.

08

Miscellaneous Operations issues (92901)

08.1 LQlosed) Violation 50-458/9511-02: four examples of operator errors that

contributed to loss of control of service water. This violation identified four

examples of violations that resulted in the inadvertent transfer of control of the

service water system to the remote shutdown panel. These examples included: (1)

the work control supervisor released a preventive maintenance (PM) work order

without an adequate review, (2) the control room supervisor assigned review of a

PM work order without specific directions, (3) operators communicated informally,

j

and (4) operators manipulated a remote shutdown system transfer switch outside

I

the bounds of the procedure.

l

For corrective actions, the licensee: (1) briefed the shift superintendents on

operations communication policy, (2) revised the system operating procedure for the

n

-.

~ ._ .

.

-.

-

=

l

!

!

1

-

-6-

l

remote shutdown system, (3) monitored gaitronics communications to ensure that

the communications policy was followed, (4) briefed operators on the event during

human performance workshops, (5) issued an all-employee letter from the Vice

l

President-Operations to reinforce human performance expectations, (6) provided

!

training to enhance sen:or reactor operator decision-making skills, and (7) performed

l

a review of control room workload to evaluate the impact of maintenance on

operators. The inspectors determined that the licensee satisfactorily completed the

corrective actions.

-

l

11. Maintenance

M1

Conduct of Maintenance

M 1.1 Maintenance Activities on the Division ill EDG

a.

Inspection Scope (62707)

l

On December 11 the inspectors observed portions of the work and retesting

activities covered by the following maintenance action items (MAI):

MAI P590845:

Clean fuel oil Strainer 1EGF-STR1C.

mal P588202:

Surge test on Circuit Breaker 1E22-EGS001.

MAI 308695:

Replace alternating current lubricating oil circulating

pump to lower vibrations.

'

!

b,

Observations and Findinas

The inspectors noted that the operators entered the appropriate TS LCO for placing

the Division ill EDG out of service. The craft personnel performed the work in

j

accordance with the MAI instructions and in a professional manner. The

maintenance technicians worked to minimize the outage time on the EDG and kept

the work areas clean.

During the replacement of the alternating current lubricating oil circulating pump and

motor, problems were encountered with the motor replacement. The new motor

'

would not fit without a significant modification to the skid. The parts list stated the

Frame 184 motors were no longer available and recommended using Frame 145T

l

motors. This discrepency and a number of other discrepancies on the parts list

were not identified until personnel performed the work with the EDG out of service.

The system engineer directed that the MAI to be revised to replace the pump only

and that a separate MAI be initiated to replace the motor. An inspection of the

existing motor found that the motor bearings were only slightly worn and not

i

I

indicating imminent f ailure. The system engineer initiated a CR to identify the above

discrepancies and to identify that the delay in replacing the motor could have been

avoided by a better prejob walkdown.

i

i

!

,

.

7

c.

Conclusions

Based on the inspectors' observations during the Division ill EDG maintenance

activities, the electricians and mechanics demonstrated continued improvement.

'

However, had there been a better prejob wa!kdown performed for the replacement

of the alternating current lubricating oil circulation pump and motor, the delay in

installing a new motor might havra been avoided.

M1.2 inocerability of Soent Fuel Pool Coolina Pumo

a.

Insoection Scooe (62707)

The inspectors evaluated the response to CR 96-1774, which identified that the

I:censee deferred IST of Pump SFC-P1 A for approximately 10 months because of

low system flow.

b.

Observations and Findinas

On December 11,1995, during performance of Procedure STP-602-6311,

" Division i Fuel Pool Cooling Quarterly Pump and Valve Operability Test,"

Revision 4, the performers could not obtain the 2500 gpm reference pump flow rate

with the throttle valve fully open. The maximum achievable flow rata was 2480

gpm. The licensee initiated CR 95-1156 to enter this item into the corrective action

program. An operability assessment indicated that 2480 gpm ensured

Pump SFC-P1 A could maintain the spent fuel pool temperature within limas

specified in the UFSAR and the design analysis; therefore, the pump remained

operable. The licensee performed no additional investigation at this time.

On February 22,1996, during performance of Procedure STP-601-6311,

Pump SFC-P1 A again f ailed to achieve 2500 gpm. This time the flow rate

measured 2471 gpm, and the performers initiated CR 96-0573. The operability

assessment concluded that the pump remained operable because it could maintain

spent fuel pool temperature. The operators disagreed with this operability

assessment because the pump failed to meet the IST acceptance criterion and was

degrading. Subsequently, IST personnel added Pump SFC-P1 A to the " exception

report" that tracked equipment for which surveillance testing was not necessary

l

because the equipment was inoperable. Although Pump SFC-P1 A has no

l

associated TS, UFSAR Section 9.1.3 specifies that the spent fuel pool cooling

pumps are safety-related and requires testing in accordance with the ASME Code

,

Section XI IST program.

After Pump SFC-P1 A f ailed to again meet the reference flow rate on April 1, the

licensee commenced a "Kepner-Tregoe" root cause analysis. During this

investigation, the licensee cross-connected Pump SFC-P1 A with the Division 11

spent fuel pool cooling system and determined the flow rate exceeded 2500 gpm.

On April 17, the licensee concluded that no problem existed with Pump SFC-P1 A

l

\\

l

.

._

_

_ _ _

_ _ _

.

.

-8-

but the Division I heat exchanger had tube leaks. The licensee tagged out Heat

Exchanger SFC-E1 A at this time, ordered parts to plug the assumed leaking tubes,

and waited until the parts arrived on August 5 to inspect the heat exchanger in

accordance with MAI 306345. On August 18, the licensee inspected Heat

Exchanger SFC-E1 A and found the heat exchanger tubes fouled. The licensee

cleaned Heat Exchanger SFC-E1 A and returned it to service on August 18.

Af ter returning Pump SFC-P1 A to service on August 18, the licensee deferred the

IST of Pump SFC-P1 A until the next scheduled IST due date and kept the pump

listed on the " exception report." The licensee satisfactorily performed the quarterly

IST for Pump SFC-P1 A on November 11. From August 18 until November 11,

operators ran Pump SFC-P1 A on several occasions because SFC-P1B was removed

from service for maintenance.

ASME Code Section XI, Subsection IWP-3230(c), " Corrective Action," specifies

that correction shall be either replacement or repair per IWP-3111, or shall be an

analysis to demonstrate that the condition does not impair pump operability and that

the pump will still fulfillits function. A new set of reference values shall be

established after such analysis. The inspectors determined that the f ailure of the

licensee to establish a new set of reference values prior to placing Pump SFC-P1 A

in service is a violation of 10 CFR 50.55a(f)(50-458/9616-03).

Because the licensee attributed the root cause to a lack of oversight by departments

other than the IST engineers, for immediate corrective actions the licensee (1)

revised procedures such that if a safety-related non-TS item was inoperable, it

would be entered into the tracking LCO list and (2) revised work management policy

such that items on the exception list would be tracked to completion.

c.

Conclusions

The inspectors identified a violation of 10 CFR 55a because personnel f ailed to

l

obtain a new set of reference values after performing analyses as specified in ASME

l

Code Section XI. A spent fuel pool cooling pump was inoperable for an excessive

l

amount of time (1'O months) because of system low flow. When the cause of the

l

low flow was determined to be heat exchanger fouling, the licensee did not

promptly perform the required IST and return the pump to service.

M1.3 Inservice Testina of SLC Pumo

l

!

l

a.

inspection Scope (61726)

l

On December 3,1996, the inspectors witnessed the performance of

,

Procedure STP-201-6311," Division i SLC Quarterly Pump and Valve Operability

Test," Revision 6A. In addition, the inspectors reviewed the procedure for technical

adequacy in accordance with ASME Code Section XI.

1

i

l

l

.-

.

_.

.

.- .

.

-

J

-9-

b.

Observations and Findinos

Prior to commencing the test, the performer noted a number of discrepancies with

the procedure. The performer identified that Procedure STP-201-6311 specified

that the vibration data be taken on the SLC pump motor rather than the crankshaft

bearing housing as required by the ASME code and the IST plan and ensured that

the procedure was revised. In addition, the performer identified that a number of

safety-related components that were directed to be manipulated during test

performance were not listed for independent verification. These discrepancies were

revised prior to the surveillance test. The test was performed in accordance with

the revised procedure with no problems. The inspectors reviewed the completed

test data and determined that data was satisfactory.

1

c.

Conclusions

1

The IST of the SLC pump was performed satisfactorily and in accordance with

procedures. The operator performing the IST of the Division I SLC pump exhibited a

questioning attitude by ensuring that the procedure was technically correct prior to

performance.

M 1.4 IST of the Division 11 SSW System

a.

Inspection Scooe (61726)

On December 12 the inspectors observed performance of Procedure STP-256-6304,

" Standby Service Water B Loop Quarterly Pump and Valve Operability Test,"

Revision 8.

b.

Observations and Findinas

The test was performed with satisfactory results and the operators followed the

procedure in a step by step manner. However, the vibration technician failed to

obtain vibration data from the locations specified in Attachment 4 of

Procedure STP 256-6304. The drawing required taking measurements directly on

the motor bearing housing; however, the test performer took the measurements at a

lifting lug that was accessible since the motor bearing housing was not accessible.

l

A similar problem with Division i SSW was identified by the inspectors in NRC

Inspection Report 50-458/96-15 and was the subject of a violation. The corrective

actions were still in process; therefore, the procedure was not revised, the pump

motor was not modified, nor a relief request submitted to alleviate the physical

l

inability to meet ASME requirements. The inspectors expressed concern that

placing the vibration technicians in the position of noncompliance with the

procedure could undermine efforts to ensure procedure compliance at River Bend.

,

The licensee responded that they would resolve the concern.

- . . - - . - . .

.-

..-

- - - _ -

. - - - -

- - - -

- - -

-. - . .

!

,

l

l

-10-

c.

Conclusions

Operators performed the IST of the Division 11 SSW system well and obtained

satisfactory results. The licensee had not yet corrected the procedures to reflect

the actual points for obtaining the ASME Code Section XI vibration measurements.

This was the subject of a violation in NRC Inspection Report 50-458/96-15 and

corrective actions had not yet been completed. The licensee indicated that they

would include this example in their violation response.

M8

Miscellaneous Maintenance issues (92902,92700)

M8.1 (Closed) Violation 50-458/9511-01: preventive maintenance (PM) work order not

properly preplanned. This violation addressed an event in which control of the

service water system was inadvertently transferred from the control room to the

remote shutdown panel during a PM task because of inadequate work instructions.

l

For corrective actions, the licensee: (1) required maintenance supervision to screen

l

PM tasks prior to implementation, (2) developed a PM reviewers checklist to ensure

i

that all expectations for the work document were met, (3) issued a PM work

instruction writer's guide, and (4) trained maintenance craft on the implementation

of PM tasks. The inspectors determined that the licensee satisfactorily implemented

the corrective actions.

M8.2 (Closed) Violation 50-458/9523-01: failure to comply with Operations Policy 19,

" Restoration / Maintenance of System / Component Operability Through use of Manual

Action in Place of Automatic Action." While painting the Division 11 EDG, plant

construction personnel installed plastic sheeting over the EDG cooling vents to

prevent damage from paint overspray. However, control room operators were

unaware of the extent of this activity and that manual action would be necessary

for the EDG to perform its intended safety function.

At the time of the incident, the inspectors noted that appropriate immediate

corrective actions were taken. To prevent a recurrence, a painting impact

walkdown checklist was developed and implemented by revising

Procedure PMC-22-002, " Modification Installation," to require walkdowns by

painters and operators to ensure that safety related equipment was not impacted

without the knowledge of the operators. The inspectors noted over the past year

that the painters and paint supervision exercised caution not to impact operating

equipment during extensive painting activities in the power block.

M8.3 LClosed) Violation 50-458/9523-02: two examples of f ailure to comply with

written procedures. In the first example, a mechanic disconnected the wrong

solenoid pilot operated air start valve from the Division I EDG for troubleshooting

and/or replacement. This inattention to detail resulted because the mechanic

perceived that the job was to be expedited. The inspectors verified that an

accountability and counseling session was held with the mechanic. In addition,

.

-

..7-

-

-r-

--

-

. __

_ _

_ _ _ _ _ _ .- . _ _ _ _

__

_

.

..

.

,

.

a

-11-

training sessions were held with mechanics to stress the importance of following

i

procedures and not expediting work at the expense of quality.

In the second example, a CR was not initiated to document the error and properly

'

disposition the valve until 2 days later when prompted by the inspectors. This was

contrary to Procedure RBNP-030, " Initiation and Processing of Condition Reports,"

Revision 7. The maintenance supervisor had misinterpreted the

Procedure RBNP-030 requirements. The inspectors verified that

Procedure RBNP-030, Revision 9 contained clear instructions requiring a CR to be

initiated whenever activities are performed on the wrong equipment.

I

M8.4 (Closed) Insoection Followur; Item 50-458/9523-0_3: during the observation of the

replacement of an air start solenoid operated valve the inspectors identified a

,

question on the generic implications of the failed component being replaced.

J

i

The licensee experienced several failures of this component in service and during

l

bench testing. The EDG vendor issued a 10 CFR Part 21 report on these

components which were purchased from Calcon Corporation. The 10 CFR Part 21

,

report identified a generic impact from the failures and, thus, the generic impact

was appropriately reported to the industry.

,

M8.5 (Ocen) Licensee Event Report 50-458/95-02: deficient IST surveillance of EDG air

receiver check valves because of an inadequate procedure. On March 21,1995,

the EDG system engineer identified that the surveillance procedures for verifying the

operability of the Division I and II EDG air receiser tank inlet check valves were

deficient. The test incorrectly included nonsafety-related check valves in the test

boundary.

The corrective action for this problem was to train system engineers and other

selected personnel who review and verify IST surveillance procedures. Training was

to be given by October 26,1995. The inspectors reviewed the training records and

found that the reactor core isolation cooling system engineer, who reviewed and

verified IST surveillance procedures, had not been trained in this regard. After being

informed of this observation by the inspectors, the licensee discovered an additional

three engineers who were not trained. The licensee documented this discrepancy in

CR 96-2069. This licensee event report will remain open until all system engineers

"

who review IST procedures have been trained.

i

i

'

.

-12-

Ill. Enaineering

E2

Engineering Support of Facilities and Equipment

i

E2.1

Inacoropriate Use of Chemical Cleaner

a.

Injip_ection Scope (37551)

The inspectors reviewed licensee actions in response to an incident where personnel

used an unapproved commercial cleaner to clean a service water radiation monitor

heat exchanger.

b.

Observations and Findinas

On October 17,1996, mechanics removed the stainiess steel heat exchanger from

Radiation Monitor RMS-RE158, Train B SSW radiation monitor, to inspect it for

fouling. After attempts to flush with water, mechanically clean with brushes, and

ultrasonically clean the heat exchanger, the heat exchanger remained fouled. Upon

discovering that the heat exchanger remained clogged with sludge, the engineer

performing the inspection suggested that the mechanics contact the Chemistry

Department for guidance on an appropriate chemical cleaning agant to remove the

sludge.

.

Subsequently, the mechanics cleaned the heat exchanger with a diluted solution of

"Fantastik" (three ounces of cleaning agent in four gallons of water) on the verbal

suggestion of a chemistry laboratory supervisor. "Fantastik" contained caustics

that could promote stress corrosion cracking of the stainless steel surfaces in the

heat exchanger at elevated temperatures. " Fantastic" was classified by the licensee

under their chemical control program as a Class 111 chemical, which was a chemical

that was not to be used in direct contact with plant systems. Upon recognizing this

action was contrary to Procedure RBNP-040," Control of Chemicals," Revision 7A,

j

the mechanics initiated CR 96-1869. The heat exchanger was flushed with water

prior to placing it into service. Based on this and the diluted solution of "Fantastik"

used, the engineer determined that there was no degradation of the heat exchanger.

The root cause analysis associated with CR 96-1869 identified miscommunication

j

among departments and a lack of thorough understanding of the chemical control

'

program. Additionally, administrative procedures related to evaluating chemicals in

the plant did not agree on who had responsibility for designating the use of

chemicals on safety-related equipment. The inspectors expressed concern that the

chemical control program continued to be ineffective in preventing the unauthorized

use of chemicals in the plant. The licensee revised procedures to ensure clear

guidance provided on user responsibilities when using chemicals in the plant and for

approving chemicals for use in the facility. The inspectors reviewed Revision 8 to

Procedure RBNP-040 and noted that the requirements were clear and concise. The

licensee also scheduled training with maintenance shops, chemists, and engineering

_ . _ .

_-

_ ._

___ . _ __ . . _ _ _ _ _

_ . _ _ - . . _ _ _ _ _ . _ . . _ _ _ . _

,

, ,

-13-

to heighten awareness levels with the clarified chemical control program

requirements.

Failure to comply with the requirements of Section 6.1.5 of Procedure RBNP-040is

a violation of TS 5.4.1.a. This licensee-identified and corrected violation is being

treated as an NCV consistent with Section Vll.B.1 of the NRC Enforcement Policy.

Specifically, the violation was identified by the licensee, was not willful, actions

taken as a result of a previous violation should not have corrected this problem, and

appropriate corrective actions were completed by the licensee (50-458/9616-04).

c.

Conclusions

The inspectors concluded that the licensee responded appropriately to the improper

,

use of chemicals in the plant by correcting the specific problem and strengthening

the chemical control program. An NCV was identified for failure to comply with the

chemical control procedure.

E2.2 Review of Facility Conformance to UFSAR Descriptions

\\

1

A recent discovery of a licensee operating a facility in a manner contrary to the

UFSAR description highlighted the need for a special focused review that compares

plant practices, procedures, and/or parameters to the UFSAR descriptions. While

j

!

performing the inspections discussed in this report, the insptctors reviewed the

applicable portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed plant

practices, procedures, and/or parameters.

E8

Miscellaneous Engineering issues (92903)

i

!

E8.1

(Closed) Unresolved item 50-458/9615-06: potential violation of TS 3.0.4 because

l

of mispositioned test switch. The inspectors questioned the initial operability

l

assessment for Switch S1-HVKB03 being mispositioned. Subsequently, the

licensee noted that Division I of control room air conditioning would be inoperable if

l

Chiller HVK-CH1B was selected and Switch S1-HVKB03 was in the " TEST"

position. The inspectors left this item unresolved because the licensee was

reviewing whether the plant changed modes with Switch S1-HVKB03 in the " TEST"

l

position and Chiller HVK-CH1B selected for postaccident operation.

l

'

l

The licensee completed their review of this event and determined that they violated

TS 3.0.4 by changing operational modes with the control room air conditioning

system inoperable. An example of a configuration control violation was identified in

NRC Inspection Report 50-458/9615 for Switch 31-HVKB03 being out of position

!

that addressed this same deficiency. The inspectors will followup on the corrective

!

actions for this issue during review of the licensee event report.

i

.

-- .

~

-.

. -

- . .. .

.-

--=

- . ~ . _ . - ~ .. - - . - ..- . . - ..

.

-. j

d

14-

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 - Locked Hiqh Radiation Area Door left Unlocked

a.

Insoection Scooe (71750)

The inspectors reviewed licensee actions in response to CR 96-1954 that

documented the failure to maintain a high radiation area door locked.

b.

Observations and Findinas

On November 14,1996, while on a routine tour, a maintenance supervisor

discovered Door RW-136-62 urdocked and unattended. This door provided a locked

barrier for a locked high radiation area as defined in TS 5.7.2 (i.e., areas with

radiation levels greater than or equal to 1000 millirem per hour). The maintenance

supervisor contacted Radiation Protection and stood by the door until a radiation

j

protection technician arrived at the scene. The door was one of three in the

radioactive waste building that did not automatically lock when latched. The

radiation protection technician who last used the door failed to check that the door

was locked as well as latched. The door was promptly locked and the CR was

q

initiated.

In response to the incident, the licensee checked to determine if someone could

have entered the area through the door while it was unattended and found none. A

l

check was made for abnormally high exposures for the day involved and none were

identified. The radiation protection technician who left the door unlocked was

l

counseled about self-checking. The licensee initiated an investigation to determine

j

if the three doors that did not automatically lock could be modified so that alllocked

!

high radiation area doors lock automatically when latched. The inspectors

determined that this was an isolated incident.

,

Failure to maintain locked high radiation area Door RW-136-62 tocked or

!

continuously guarded is a violation of TS 5.7.2. This licensee-identified and

l

corrected violation is being treated as an NCV consistent with Section Vll.B.1 of the

NRC Enforcement Policy. Specifically, the violation was identified by the licensee,

was not willful, actions taken as a result of a previous violation should not have

corrected this problem, and appropriate corrective actions were completed by the

licensee (50-458/9616-05).

c.

Conclusions

1

i

The inspectors concluded that the November 14 f ailure to lock the door to a locked

!

high radiation area was an isolated incident that the licensee appropriately

dispositioned. An NCV was identified for failure to comply with TS 5.7.2.

<

v-

-

-

r

-

-

.. .._ _. ___._ .~. _

. _ _ _ _ . _ _ _ _ . _ . _ . . _

.

,

.

,

e

-15-

(

S1

Conduct of Security and Safeguards Activities

S 1.1

General Comments (71750)

Throughout the inspection period, the inspectors observed security officers as they

performed their duties. The security officers were alert at their posts, security

boundaries were being maintained properly, and entry screening processes were

performed well at the primary access point.

,

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on December 19,1996. A subsequent exit was held on

Janaury 2,1997, to reclassify several inspection findings. The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

I

i

!

l

i

4

i

I

!

.-

- .

. . . . .

.

.

- . ..

_- -

- . . - . -

. - . - . - - - _ . - - . . _ . - _ . - .

. - . . . .

. . . - -

e

'.

6

'

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

,

l

'

Licensee

!

J. P. Dimmette, General Manager, Plant Operations

l

M. A. Dietrich, Director, Quality Programs

'

D. T. Dormady, Manager, System Engineering

l

J. R. Douet, Manager, Maintenance

J. Holmes, Superintendent, Chemistry

l

H. B. Hutchens, Superintendent, Plant Security

l

T. R. Leonard, Director, Engineering

l

D. N. Lorfing, Supervisor, Licensing

C. R. Maxson, Senior Lead Licensing Engineer

J. R. McGaha, Vice President-Operations

W. P. O'Malley, Manager, Operations

W. H. Odell, Superintendent, Radiation Control

-l

lNSPECTION PROCEDURES (IP) USED

l

IP 37551

Onsite Engineering

IP 61726

Surveillance Observations

IP 62707

Maintenance Observation

lP 71707

Plant Operations

i

IP 71750

Plant Support Activities

IP 92700

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92901

Followup - Operations

IP 92902

Followup - Maintenance

l

iP 92903

Followup - Engineering

!

,

t

!

!

!

!

- -.

.

-

.

. _ .

. . .

.

. _ _ _ .

- . -

- . .

_

!

O

4

.

,

0

-2-

'

ITEMS OPENED, CLOSED, AND DISCUSSED

,

Ooened

i

l

50-458/9616 01

VIO

Failure to maintain an operating procedure (Section O2.1)

)

50-458/9616-02

VIO

Failure to implement the safety function determination

program (Section 04.1)

,

,

50 458/9616-03

VIO

Failure to establish reference values prior to placing pump

in servica (Section M1.2)

Closej

50-458/9511-01

VIO

Inadequate preventive maintenance instruction

(Section M8.1)

50-458/9511-02

VIO

Four examples of operator errors led to loss of control of

SSW (Section 08.1)

50-458/9523-01

VIO

Failure to comply with administrative controls over manual

actions (Section M8.2)

50-458/9523-02

VIO

Two examples of failure to follow procedures

(Section M8.3).

50-458/9523-03

IFl

Review of generic implications of EDG start valves

(Section M8.4)

50-458/9615-06

URI

Potential violation of TS 3.0.4 because of mispositioned

4

test switch (Section E8.1)

I

Opened and Closed

50-458/9616-04

NCV

Improper use of chemical cleaner (Section E2.1)

50-458/9616-05

NCV

Failure to lock a locked high radiation area door

(Section R1.1)

Discussed

50-458/95 002

LER

Deficient IST of EDG air receiver check valves

l

(Section M8.5)

,

!

i

-

- -

-

__

--

.- .

-

-

a

, ,

, .

t

e

1

,

,

!

-3-

!

LIST OF ACRONYMS USED

ASME

American Society of Mechanical Engineers

!

CR

Condition Report

l

CRS

Control Room Supervisor

EDG

Emergency Diesel Generator

gpm

gallons per minute

!PCS

High Pressure Core Spray

IP

inspection Procedure

lST

Inservice Testing

LCO

Limiting Condition for Operation

LPCS

Low Pressure Core Spray

mal

Maintenance Action item

!

,,CV

Noncited Violation

PDR

Public Document Room

PM

Preventive Maintenance

SLC

Standby Liquid Control

l

SSW

Standby Service Water

'

TS

Technical Specification

I

UFSAR

Updated Final Safety Analysis Report

1

!

l

,

1

d

E

_ , _

_