ML20128N856

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Amend 167 to License DPR-35,changing TSs to Implement 10CFR50,App J,Option B
ML20128N856
Person / Time
Site: Pilgrim
Issue date: 10/04/1996
From:
NRC (Affiliation Not Assigned)
To:
Shared Package
ML20128N863 List:
References
NUDOCS 9610170054
Download: ML20128N856 (10)


Text

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UNITED STATES yo j

NUCLEAR REGULATORY COMMISSION t

WASHINGTON, D.C. 2055SA)01 l

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BOSTON EDIS0N COMPANY DOCKET NO. 50-293 PILGRIM NUCLEAR POWER STATION AMENDMENT TO FACILITY OPERATING LICENSE Amendment No.167 License No. DPR-35 1.

The Nuclear Regulatory Commission (the Comission or the NRC) has found that:

A.

The application for amendment filed by the Boston Edison Company (the licensee) dated May 1, 1996, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act),

and the Commission's rules and regulations; l

B.

The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Comission; C.

There is reasonable assurance:

(i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations; D.

The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E.

The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations and all applicable requirements have been satisfied.

2.

Accordingly, the license is amended by changes to the Technical Specifica-tions as indicated in the attachment to this license amendment.

9610170054 961004 ADOCK0500gg3 DR

p 3.

This license amendment is effective as of its date of issuance and shall be implemented prior to the start of Refueling Outage 11.

FOR THE NUCLEAR REGULATORY COMMISSION S. Singh Bajwa, Acting Director Project Directorate I-l Division of Reactor Projects - I/II Office of Nuclear Reactor Regulation

Attachment:

Changes to the Technical Specifications Date of Issuance: October 4, 1996

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ATTACHMENT TO LICENSE AMENDMENT NO.167 FACILITY OPERATING LICENSE N0. DPR-35 DOCKET NO. 50-293 Replace the following pages of the Appendix A Technical Specifications with the attached pages.

The revised pages are identified by Amendment number and contain vertical lines indicating the area of change.

Remove Insert 3/4.7-4 3/4.7-4 3/4.7-5 3/4.7-5 B3/4.7-3 83/4.7-3 B3/4.7-4 B3/4.7-4 83/4.7-5 B3/4.7-5 B3/4.7-6 B3/4.7-6 B3/4.7-7 B3/4.7-7 j

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LIMITING CONDITIONS FOR OPERATION SURVEILLANCE REQUIREMENTS 3.7 CONTAINMENT SYSTEMS (Cont) 4.7 CONTAINMENT SYSTEMS (Cont)

A. Primary Containment (Cont)

A. Primary containment (Cont)

Priinary Containment Intenrity Primary Containment Intenrity l

2. a. Primary containment 2.
a. The primary containment integrity shall be integrity shall be maintained at all times when demonstrated by performing the reactor is critical or Primary Containment Leak when the reactor water Tests in accordance with t

temperature is above 212 F 10CFR50 Appendix J, Option B l

and fuel is in the reactor and Regulatory Guide 1.163 vessel except while dated September 1995*, with i

performing "open vessel" exemptions as approved by physics tests at power the NRC and exceptions as levels not to exceed follows:

5 Mw(t).

1. The main steam line Primary containment isolation valves shall be integrity means that the tested at a pressure 223 drywell and pressure psig, and normalized to a suppression chamber are value equivalent to P -

l intact and that all of the a

following conditions are

2. Personnel air lock door satisfied:

seals shall be tested at a pressure 210 psig.

1. All manual containment Results shall be isolation valves on lines normalized to a value connected to the reactor equivalent to P -

l a

coolant system or containment which are not

3. Leakage rate acceptance required to be open criteria are:

during accident conditions are closed.

1. Primary containment overall leakage rate
2. At least one door in each acceptance criterion airlock is closed and is $1.0 L.

During a

sealed.

the first unit startup following testing in

3. All blind flanges and accordance with the manways are closed.

Containment Leakage Rate Testing Program,

4. All automatic primary the leakage rate i

containment isolation acceptance criteria valves and all instrument are s 0.60 L f r the a

line flow check valves Type B and Type C are operable except as tests and 5 0.75 La specifitd in 3.7.A.2.b.

for the Type A tests.

2. Overall air lock leakage rate is 50.05 L when tested at 2 P a

a

3. Door seals leakage rate is 50.01 L when a

pressurized to 2 10 psig.

  • Definition 1.U is not applicable to Leak Rate Tests.

Amendment No. 17;-113;-136,.142,167 3/4.7-4

_ LIMITING CONDITIONS FOR OPERATION SURVEILLANCE REQUIREMENTS 3.7 CONTAINMENT SYSTEMS (Cont) 4.7 CONTAINMENT SYSTEMS (Crnt)

A.

Primary Containment (Cont)

A. Primarv Containment (Cont)

5. All containment isolation 4 Combined main steam check valves are operable lines:

46 sc fh @ 2 3 or at least one psig.

containment isolation valve in each line having where P 45 psig l

a an inoperable valve is La 1.0% by weight of secured in the isolated the contained air position.

@ 45 psig for 24 hrs.

i Primary Containment Isolation Valves Primary Containment Isolation Valves 2.b.1 The primary containment

2. b. In'the event any automatic isolation valves Primary Containment surveillance shall be Isolation Valve becomes performed as follows:

inoperable, at least one containment isolation valve

a. At least once per in each line having an operating cycle the I

inoperable valve shall be operable primary j

deactivated in the isolated containment isolation condition.

(This valves that are power requirement may be satisfied operated and by deactivating the automatically initiated inoperable valve in the shall be tested for irolated condition.

simulated automatic Deactivation means to initiation and closure electrically or times.

pneumatically disarm, or otherwise secure the

b. Test primary containment valve.)*

isolation valves:

1. Verify power operated primary containment isolation valve operability as specified in 3.13.
2. Verify main steam isolation valve
  • Isolation valves closed to satisfy operability as these requirements may be reopened on specified in 3.13.

an intermittent basis under ORC approved administrative controls.

Amendment No. 113;-136;-149,-160,167 3/4.7-5

r-BASES:

3/4.7 CONTAINMENT SYSTEMS (Cont)

A. Primarv Containment (Cont)

Primarv Containment Testinn 1

The primary containment pre-operational test pressures were based upon the l

calculated primary containment pressure response in the event of a loss-of-coolant accident.

The calculated peak drywell pressure is about 45 psig which would rapidly reduce to 27 psig following the pipe break Following the pipe break. the suppression chamber pressure rises to 27 psig.

]

equalizes with drywell pressure and therefore rapidly decays with the drywell pressure decay.

The design pressure of the drywell and suppression chamber is 56 psig.

The design leak rate is 0.5%/ day at a pressure of 56 psig.

Based on the calculated containment pressure response discussed above, the primary containment pre-operational test pressures were chosen.

Also, based on the primary containment pressure response und the fact that the drywell and suppression chamber function as a unit, the primary containment will be tested as a unit rather than the individual components separately.

The design basis loss-of-coolant accident was evaluated at the primary containment maximum allowable accident leak rate of 1.25%/ day at 45 psig.

Calculations made by the AEC staff with this leak rate and a standby gas treatment system filter efficiency of 95% for halogens and assuming the fission product release fractions stated in TID 14844, show that the maximum total whole body passing cloud dose is about 13 REM and the maximum total thyroid dose is about 110 REM at the site boundary over an exposure duration of two hours.

The resultant doses that would occur for the duration of the 4

j accident at the low population zone distance of 4.3 miles are about 3 REM total whole body and 70 REM total thyroid.

Thus, the doses reported are the maximum that would be expected in the unlikely event of a design basis loss-1 of-coolant accident.

These doses are also based on the assumption of no holdup in the secondary containment resulting in a direct release of fission products from the primary containment through the filters and stack to the environs.

Therefore, the specified primary containment leak rate and filter efficiene are conservative and provide margin between expected off-site dose

)

and 10CFL.>0 guidelines.

The maximum allowable test leak rate (L ) is 1.0%/ day at a pressure of 45 l

a t

psig.

This value for the test condition was derived from the maximum allowable accident leak rate of 1.25%/ day when corrected for the effects of containment environment under accident and test conditions.

In-the accident case, the containment atmosphere initially would be composed of steam and hot air whereas under test conditions the test medium would be air at ambient I

conditions.

Considering the differences in mixture composition and temperatures, the appropriate correction factor applied was 0.8 as determined from the guide on containment testing.

1 Establishing the test limit of 1.0%/ day provides an adequate margin of safety to assure the health and safety of the general public.

It is further considered that the allowable leak rate should not deviate significantly from the containment design value to take advantage of the design leak-tightness Amendment No. 87;-113,167 B3/4.7-3

BASES:

3/4.7 CONTAINMENT SYSTEMS (Cont)

A. Primarv Containment (Cont) capability of the structure over its service lifetime.

Additional margin to maintain t he containment in the "as built" condition is achieved by l

establishing the allowable operational leak rate.

The allowable operational t

leak rate is derived by multiplying the maximum allowable leak rate or the allowable test leak rate by 0.75 thereby providing a 25% margin to allow for leakage deterioration which may occur during the period between leak rate tests.

The primary containment leakage rate testing is based on the guidelines in Regulatory Guide 1.163 dated September 1995, NEI 94-01 Revision 0 dated July 26, 1995, and ANSI /ANS 56.8-1994 Specific acceptance criteria for i

as-found and as-left leakage rates, as well as methods of defining the leakage i

rates, are contained in the primary containment leakage rate testing program.

The primary containment leak rate test frequency is based on maintaining adequate assurance that the leak rate remains within the specification.

The leak rate test frequency is in accordance with 10CFR50 App. J Option B and Regulatory Guide 1.163 dated September 1995.

Type A, Type B and Type C tests will be performed using the technical methous l

and techniques specified in ANSI /ANS 56.8 - 1994, or other alternative testing methods approved by the NRC.

A note is included in Surveillance 4.7.A.2.a stating that definition 1.U is not applicable.

The 25% allowable extension of surveillance intervals is already included in the primary containment leakage rate testing program, therefore an additional 25% is not allowed.

The penetration and air purge piping leakage test frequency, along with the containment leak rate tests, is adequate to allow detection of leakage trends.

Whenever a bulted double gasketed penetration is broken and remade, the space between the gaskets is pressurized to determine that the seals are performing properly.

It is expected that the majority of the leakage from valvas, penetrations and seals would be into the reactor building.

However, it is possible that leakage into other parts of the facility could occur.

Such leakage paths that may affect significantly the consequences of accidents are to be minimized.

The personnel air lock is tested at 10 psig, because the inboard door is not designed to shut in the opposite direction.

Primary Containment Isolation Valves Double isolation valves are provided on lines penetrating the primary containment and open to the free space of the containment.

Closure of one of the valves in each line would be sufficient to maintain the integrity of the pressure suppression system. Automatic initiation is required to minimize the po'ential leakage paths from the containment in the event of a loss of coolant accident.

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Amendment No. 113;-136,167 g3/4.7 4

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BASES:

i 3/4.7 CONTAINMENT SYSTEMS (Cont)

A. Primarv Containment (Cont)

Group 1 - process lines are isolated by reactor vessel low-low water level in order to allow for removal of decay heat subsequent to a scram, yet isolate in time for proper operation of the core standby cooling systems.

The valves in I

group 1 are also closed when process instrumentation detects excessive main steam line flow, high radiation, low pressure, main steam space high temperature, or reactor vessel high water level.

i Group 2 isolation valves are closed by reactor vessel low water level or I

high drywell pressure.

The group 2 isolation signal also " isolates" the reactor building and starts the stan<

gas treatment system.

It is not desirable to actuate the group 2 isoi

=on signal by a transient or spurious 1

signal.

I l

Group 3 - isolation valves can only be opened when the reactor is at low pressure and the core standby cooling systems are not required.

Also, since the reactor vessel could potentially be drained through these process lines, these valves are closed by low water level.

Group 4 and 5 - process lines are designed to remain operable and mitigate the consequences of an accident which results in the isolation of other process lines.

The signals which initiate isolation of group 4 and 5 process lines are therefore indicative of a condition which would render them inoperable.

Group 6 - process lines are normally in use and it is therefore not desirable to cause spurious isolation due to high drywell pressure resulting from non-safety related causes.

To protect the reactor from a possible pipe break in

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the system, isolation is provided by high temperature in the cleanup system

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area or high flow through the inlet to the cleanup system.

Also, since the vessel could potentially be drained through the cleanup system, a low level isolation is provided.

Groun 7 - The HPCI vacuum breaker line is designed to remain operable when the HPCI system is required.

The signals which initiate isolation of the HPCI vacuum breaker line are indicative of a break inside containment and reattor pressure below that at which HPCI can operate.

The maximum closure time for the automatic isolation valves of the primary containment and reactor vessel isolation control system have been selected in consideration of the design intent to prevent core uncovering following pipe breaks outside the primary containment and the need to contain released fission products following pipe bceaks inside the primary containment.

In satisfying this design intent an additional margin has been included in specifying maximum closure times.

This margin permits identification of degraded valve performance, prior to exceeding the design closure times In order to assure that the deses that may result from a steam line break do not exceed the 10CFR100 guidelines, it is necessary that no fuel rod perforation resulting from the accident occur prior to closure of the main steam line isolation valves. Analyses incicate that fuel rod cladding perforations would be avoided for main steam valve closure times, including instrument delay, as long as 10.5 seconds.

Amendment No, 113,167 B3/4.7-5

BASES:

3/4.7 CONTAINMENT SYSTEMS (Cont)

A. Primarv Containment (Cont)

These valves are highly reliable. have low service requirements and most are normally closed.

The initiating sensors and associated trip channels are also checked to demonstrate the capability for automatic isolation.

The test interval of once per operating cycle for automatic initiation results in a failure probability of 1.1 x 10-7 that a line will not isolate.

More frequent testing for valve operability results in a greater assurance that the valve will be operable when needed.

The main steam line isolation valves are functionally tested on a more frequent interval to establish a high degree of reliability.

The primary containnent is penetrated by several small diameter instrument lines connected to tae reactor coolant system.

Each instrument line contains a 0.25 inch restricting orifice inside the primary containment. A program for periodic testing ar.d examination of the excess flow check valves is in place.

Primary Containment Paintinn The interiors of the drywell and suppression chamber are painted to prevent rusting.

The inspection of the paint during each major refueling outage, assures the paint is intact.

Experience at Pilgrim Station and other BWR's with this type of paint indicates that the inspection interval is adequate.

Vacuum Relief The purpose of the vacuum relief valves is to equalize the pressure between the drywell and suppression chamber and reactor building so that the structural integrity of the containment is maintained.

The vacuum relief system from the pressure suppression chamber to reactor building consists of two 100% vacuum relief breakers (2 parallel sets of 2 valves in series).

Operation of either system will maintain the pressure differential less than 2 psig; tha external design pressure.

One valve may be out of service for repairs for a period of seven days.

If repairs cannot be completed witl seven days, the reactor coolant system is brought to a condition where snanun relief is no longer required.

The capacity of the 10 drywell vacuum relief valves is sized to limit the pressure differential between the suppression chamber and drywell during post-accident drywell cooling to the design limit of 2 psig.

They are sized on the basis of the Bodega Bay pressure suppression system tests.

The ASME Boiler and Pressure Vessel Code,Section III, Subsection B, for this vessel allows a 5 psig vacuum; therefore, with two vacuum relief valves secured in the closed position and eight operable valves, containment integrity is not impaired.

Reactor operation is permissible if the bypass area between the primary containment drywell and suppression chamber does r.ot exceed an allowable area.

The allowable bypass area is based upon analysis considering primary system break area, suppression chamber effectiveness, and containment design pressure.

Analyses show that the maximum allowable bypass area is 0.2 ft2, which is equivalent to all vacuum breakers open 3/32" (See letters from Boston Edison to the Directorate of Licensing, dated May 15, 1973 and October 22, 1974)

Amendment No. 113;-151,167 B3/4.7-6

EASES:

3/4.7 CONTAINMENT SYSTEMS (Cont)

A. Primary Containment (Cont)

Reactor operation is not permitted if differential pressure decay rate is demonstrated to exceed 25% of allowable, thus providing a margin of safety for j

the primary containment in the event of a small break in the primary system.

l Each drywell suppression chamber vacuum breaker is equipped with three switches.

One switch provides full open indicatior. only. Another switch provides closed indication and an alar, should any vacuum breaker come off its closed seat by greater than 3/32".

The third switch provides a separate and redundant alarm should any vacuum breaker come off its closed seat by greater than 3/32" The two alarms above are those referred to in Section 3.7.A.4.a.3 and 3.7.A.4.d.

The water in the suppression chamber is used only for cooling in the event of an accident; i.e., it is not used for normal operation; therefore, a daily check of the temperature and volume is adequate to assure that adequate iieat removal capability is present.

Inertine The relatively small containment volume inherent in the CE-BWR pressure suppression containment and the large amount of zirconium in the core are such that the occurrence of a very limited (a percent or so) reaction of the zirconium and steam during a loss of-coolant accident could lead to the liberation of hydrogen combined with an air atmosphere to result in a flammable concentration in the containment.

If a sufficient amount of hydrogen is generated and oxygen is available in stoichiometric quantities, the subsequent ignition of the hydrogen in rapid recombination rate could lead to failure of the containment to maintain a low leakage integrity.

The 4%

oxygen concentration minimizes the possibility of hydrogen combustion following a loss-of-coolant.

The occurrence of primary system leakage following a major refueling outage or other scheduled shutdown is much more probable than the occurrence of the loss-of-coolant accident upon which the specified oxygen concentration limit is based.

Permitting access to the drywell for leak inspections during a startup is judged prudent in terms of the added plant safety offered without significantly reducing the margin of safety.

Thus, to preclude the possibility of starting the reactor and operating for extended periods of time with significant leaks in the primary system, leak inspections are scheduled during startup periods, when the primary system is at or near rated operating temperature and pressure.

The 24-hour period to provide inerting is judged to be sufficient to perform the leak inspection and establish the required oxygen concentration.

The primary containment is normally slightly pressurized during periods of reactor operation. Nitrogen used for inerting could leak out of the containment but air could not leak in to increase oxygen concentration.

Once the containment is filled with nitrogen to the required concentration, no monitoring of oxygen concentration is necessary.

However, at least twice a week the oxygen concentration will be determined as added assurance.

Mark I containment Long Term Program testing showed that maintaining a drywell to Amendment No. 317-53 -55; 113,-158,167 B3/4.7-7