ML20128H090

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Insp Repts 50-456/96-11 & 50-457/96-11 on 960615-0726. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML20128H090
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 10/02/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20128H080 List:
References
50-456-96-11, 50-457-96-11, NUDOCS 9610090235
Download: ML20128H090 (22)


See also: IR 05000456/1996011

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION III

Docket Nos:

50-456, 50-457

License Nos:

NPF-72, NPF-77

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Report No:

50-456/96011; 50-457/96011

Licensee:

Commonwealth Edison (Comed)

Facility:

Braidwood Nuclear Plant, Units 1 and 2

Location:

RR #1, Box 84

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Braceville, IL 60407

Dates:

June 15 - July 26, 1996

Inspectors:

C. Phillips, Senior Resident Inspector

M. Kunowski, Resident Inspector

Z. Falevits, Reactor Engineer

E. Plettner, Regional Inspector

T. Esper, Illinois Department of Nuclear Safety

Approved by:

Lewis F. Miller, Jr., Chief, Projects Branch 4

Division of Reactor Projects

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9610090235 961002

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ADOCK 05000456

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EXECUTIVE SUMMARY

Braidwood Nuclear Plant, Units 1 & 2

NRC Inspection Report 50-456/96011; 50-457/96011

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a 6-week

period of resident inspection.

In addition, it includes the results of

announced inspections by regional inspectors.

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Operations

Defueling practices and procedures were consistent with the licensing

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basis and reflected the current design basis of the Updated Final Safety

Analysis Report.

(Section 01.1)

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The failure to follow procedures and poor communications were

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identified by the licensee as the root causes for a Unit I

containment release made without an operable radiation monitor.

(Section 04.1)

A failure to follow a procedure to rack in a 6.9-kilovolt breaker

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was identified by the inspectors as an example of a violation of

Technical Specification 6.8.1.a.

The licensee identified and the

inspectors agreed that the root cause of the problem was poor

communications between operators.

(Section 08.4)

Maintenance

A failure to follow procedures to control the installation of a jumper

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on a ventilation damper controller was identified by the inspectors as

an example of a violation of Technical Specification 6.8.1.a.

(Section

M2.1)

The licensee removed workload from first line supervisors and

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hired contractors to work off longstanding work requests, in

response to maintenance department self-assessment.

However, some

of the department assessments lacked depth and did not address all

the items identified as weaknesses.

(Section M7.1)

Enaineerina

Operability assessments reviewed by the inspectors were adequate;

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however, the inspectors concluded that the licensee's ability to

determine the status of open assessments was weak.

(Section El.1)

The mispostioning of an instrument air vent valve for a Unit 2

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safety injection pump room ventilation damper was identified by

the inspectors as an example of a previously identified violation

for the failure to correct plant configuration control problems.

(Section E8.2)

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P_lant Suonort

Poor communications and a failure to follow procedures on the part of

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radiation protection department personnel contributed to uncorrected air

inleakage into a reactor coolant leakage detection radiation monitor and

securing a Unit I containment radiation laonitor during a containment

release.

(Sections 02.2 and 04.1)

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Report Details

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Summary of Plant Status

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Unit 1 entered the period at or near 100% power and operated routinely until

June 21, 1996. At approximately 11:30 a.m. on June 21, power was reduced to

about 80% to remove the 1A condensate booster pump from service, due to an

overheating inboard bearing, because no standby pump was available.

The IC

condensate booster pump was not available due to maintenance activities that

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were ongoing for several months. The 1A pump was repaired and the Unit was

restored to 100% power on June 26. Full power operation continued for the

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remainder of the period.

Unit 2 operated at or near 100% power for the entire period.

I.

Doerations

01

t.onduct of Operations

01.1 Reactor Defuelina Practices and the Licensina Basis

a.

Inspection Scone

In February and March 1996, the inspectors reviewed Braidwood's current

licensing basis for spent fuel decay heat removal to ensure consistency

with station core offload practices. The review included Section 9.1.3

of the Braidwood Updated Final Safety Analysis Report (UFSAR), Technical

Spec.' fications (TSs) 3.9.3 and 3.9.11, and Braidwood procedures BwAP

370-3, " Administrative Control During Refueling," and 1/2BwGP 100-6,

" Refueling Outage." The review was prompted by an event at Millstone,

Unit 1, during which the spent fuel pool (SFP) cooling system may have

been incapable of maintaining pool temperature below the design limit.

This event was discussed in NRC Information Notice 95-54, " Decay Heat

Management Practices During Fuel Outages," (IN 95-54).

b.

Observations and Findinas

Three cases of refueling modes were discussed in Section 9.1.3 of the

UFSAR:

1) Normal Refueling Discharge (nominal 84-assembly discharge -

1/3 of the core offloaded); 2) Full Core Discharge (193 assemblies); and

3) Abnormal Discharge (Full Core Discharge 17 days after a 1/3 discharge

from the other unit).

Each case assumed that the reactor had been

subcritical for 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, as required by TS 3.9.3, before defueling

began.

In case 1, the maximum calculated heat load was 35.91 million

British thermal units / hour with a maximum SFP temperature of 138.5

degrees fahrenheit (*F) assuming a single active failure of one train of

SFP cooling. The maximum SFP temperature for case 3 (the most limiting

case) was determined to be 158 'F.

Braidwood had been pract:cing full

core discharges (case 2) during refueling outages.

The licensee also conducted an independent review of SFP cooling

following receipt of IN 95-54 and concluded that the licensing basis had

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been adequately incorporated into the procedures. Based on this review,

the licensee planned two changes intended to remove ambiguities in the

UFSAR and clarify procedures to insure adherence to the UFSAR during

refueling activities.

The 'iicensee's first change was to revise the UFSAR to explicitly state

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that the current full core offload practice was the " routine" or normal

practice.

The second change was to add the UFSAR defueling rate basis

of three assembiies per hour as a caution statement to procedure BwAP

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370-3, " Administrative Control During Refueling," Revision 15.

This

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procedure improvement was to assure that fuel offloads would not be

completed in less than 128 hours0.00148 days <br />0.0356 hours <br />2.116402e-4 weeks <br />4.8704e-5 months <br /> for the 1/3 core discharge and 164

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hours for the full core discharge without a prior engineering

evaluation.

In addition, the licensee proposed to update the generic

outage schedule to reflect the assumptions in the SFP design basis

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analysis for core offloading. The licensee informed the inspectors that

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the UFSAR change regarding the current full core offload practice and

other minor clarifications to the UFSAR would be incorporated during the

next UFSAR update to be submitted on December 16, 1996.

c.

Conclusion

The inspectors concluded that the licensee's refueling practice and

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procedures were consistent with the licensing basis and adequately

incorporated the current design-basis of the UFSAR.

In addition, the

inspectors verified that procedures had been revised as planned by the

licensee.

UFSAR revision verification is an outstanding item and will

be followed up in a future inspection (Inspection Followup Item (IFI)

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50-456/96011-01).

02

Operational Status of Facilities and Equipment

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02.1 Walkdown of Plant Safety Systems

a.

Inspection Scope (71707)

On July 10-18, the inspectors conducted a detailed walkdown using

appropriate procedures and drawings of the Unit I auxiliary feedwater

(AFW) system, the Unit I safety injection (SI) system, and the Unit 2

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fuel pool cooling and clean-up system to verify operability of the

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systems and to ensure that the lineup procedures, plant drawings, and

the as-built configuration were current.

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b. Observations and Findinas

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The inspectors performed a walkdown of the Unit 1 AFW system using

Braidwood operating procedures Bw0P AF-M1, " Operating Mechanical

Lineup," Revision 4, along with Piping and Instrumentation Diagram

(P&ID) drawing M-37. During the system walkdown the inspectors found one

valve that was not labeled, nor identified on the Bw0P AF-M1 lineup

procedure and P&ID drawing. The valve was an instrument isolation valve

for pressura indicator, IPI-AF150.

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The walkdown of the Unit 1 SI system was performed using Bw0P SI-M1,

Revision 6, along with P&ID drawing M-61, sheets 1 through 6.

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inspectors found no discrepancies.

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The walkdown of the Unit 2 fuel pool cooling and clean-up system was

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performed using Bw0P FC-M1," Operating Mechanical Lineup," Revision 3,

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along with P&ID drawing M-63, sheets la through Ic. The inspectors

identified that 0FC003, the refueling water purification pump OB suction

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valve, was drawn as closed on the P&ID, but listed as open on Bw0P FC-

M1.

Licensee personnel stated that an action request to make a valve label

had been written and the need to change the plant drawings would be

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evaluated by September 30, 1996.

c.

Conclusions

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.The inspectors concluded that the current valve lineup status of the

Unit 1 AFW, Unit 1 SI, and Unit 2 fuel pool cooling system was good.

02.2 Dearaded Unit 2 Reactor Coolant System Leakaae Detection Eauioment

a.

Inspection Scope (71707)

At 5:45 p.m. on July 16, 2PR011J, the Unit 2 containment

atmosphere radiation monitor was declared inoperable after health

physics (HP) personnel informed the shift engineer that, as of

July 6, results of analyses of non-radioactive hydrogen samples

and particulate and gaseous radioactivity samples taken daily from

the monitor by HP personnel were lower than those taken before

July 6.

The inspectors observed that the gaseous radioactivity

samples were lower by a' factor of one hundred. The licensee

assembled a team of personnel from the operations, instrument

maintenance, system engineering, and HP departmein.s to investigate

the cause of the problem. The inspectors, who had been reviewing

the status of the monitor following the computer malfunction,

observed several team meetings and some troubleshooting

activities, interviewed the health physicist and the Unit

operating engineer, and reviewed sample results.

b.

Observations and Findinas

The licensee calibrated the monitor, identified no as found

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discrepancies, and determined that the radiation detectors, the

associated electronics, and the sample pump were operating

properly. Monitor fittings were then checked to ensure there was

no air inleakage.

Finally, operations personnel compared the mechanical lineup of

the monitor as listed in Bw0P AR/PR-M2, the operating mechanical

lineup for area and process radiation monitors, with the actual

configuration. Whereas the configuration for the Unit 2 monitor

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agreed with the lineup, and the configuration for the Unit 1

monitor (IPR 011J) agreed with its lineup; the configuration of

2PR011J was different from that of IPR 011J.

For Unit 2, the valve

lineup had the containment sample directed through a dryer.

For

Unit 1, the dryer was bypassed. The inspectors noted that

although the dryer was valved-in on Unit 2, the dryer was not

operating.

In addition, an operator-aid label by the local

control switch for valving the dryer in or out directed that the

dryer be left in bypass and would normally be used only if there

was high moisture in the containment atmosphere.

On July 17, Bw0P AR/PR-M2 for Unit 2 was subsequently revised to

bypass the dryer during normal operations (consistent with Unit I

and with Byron). The local control switch was then moved to the

bypass position and a sample was taken from the monitor. The

results were comparable to those obtained before July 6,

indicating the problem had been air in leakage through the dryer

to dilute the sample. The licensee followed ep by writing a work

request to repair the leak in the dryer and a formal evaluation of

the monitor's operability from July 6-17.

The health physicist stated to the inspectors that the lower sample

readings were considered normal at first because the Unit had dropped

power to shift feed pumps. However, the readings should have returned

to normal the next day and did not. The health physicist stated that

this concern was passed on to the unit operating engineer by leaving a

note on his desk. The operating engineer stated to the inspectors that

he did not remember receiving this note.

c.

Conclusions

The inspectors concluded that there was poor communication between

HP and operations. The HP technician's cor.cern about the proper

functioning of the monitor was not passed on to the Shift Engineer

(SE) until ten days after the problem arose.

In addition, the

configuration control discrepancy was another example of an

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ongoing problem. The inspectors concluded that the licensee's

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team that investigated the problem was well coordinated and

thorough. The results of the evaluation of the monitor's

operability will be reviewed at a later date (Unresolved Item

(URI) 50-457/96011-02).

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04

Operator howledge and Performance

04.1 Containment Purae Radiation Monitors Inocerable Durina Unit 1

Containment Release

a.

Inspection Scone (71707)

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On June 20, the Unit 2 reactor operator (RO) placed the Unit I and Unit

2 containment purge particulate radioactivity samplers, IPR 0lJ and

2PR0lJ, in the purge mode, which rendered them inoperable, at the same

time a Unit I containment release was in progress. The Unit 2 R0

performed this action at the request of a radiation protection

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technician (RPT). The inspectors interviewed the SE and the PRT and

also reviewed BwRP 5820-7, " Process Radiation Monitor Particulate Filter

and Iodine Cartridge Replacement," and BwRP 6110-13, " Containment Vent

and Mini-Purge Gaseous Effluent." The inspectors also reviewed Offsite

Dose Calculation Manual (0DCN), Section 12.2.2, and a statement of what

happened written on June 21 by the SE.

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b.

Observations and Findinas

On June 20, at 5:08 a.m., the Unit 1 R0 started a Unit I containment

release. At 5:09 a.m., the Unit 2 R0 placed the Unit I and Unit 2

containment purge particulate activity samplers IPR 0lJ and the 2PR01J in

the purge mode, which rendered them inoperable, at the request of an

RPT. At about 5:20 a.m., the Unit 2 R0 informed his supervisor that the

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IPR 01J was in p rge mode. The SE stated to the inspectors that when he

overheard that the IPR 01J was in purge he recognized it as a potential

problem and at 5:26 a.m., directed that the release be secured. The

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IPR 01J was then restored to service and the release was restarted at

about 5:29 a.m.

The SE stated that after the release was restarted he reviewed the

containment release procedure, BwRP 6110-13. A note in the procedure

stated, in part, that only one release could be performed with each

noble gas and tritium aaalysis. After reading the note, the SE

concluded that the restart of the release at 5:29 a.m. constituted

another release for wt .h a new analysis was not performed, contrary to

the procedure note. The SE then had the second release terminated,

about 5:32 a.m.

According to the SE, the Unit 2 R0 told him that he (the RO) was not

aware of the Unit I release nor of the requirement to secure the release

if IPR 0lJ became inoperable.

The RPT that requested the IPR 01J and 2PR01J be placed in purge was

changing filters per BwRP 5820-7. A note under step 2 of the procedure

required the RPT to ensure that there were no containment releases in

progress prior to proceeding. The RPT stated that she was aware that a

release was phnned for that shift, but did not know that it was in

progress when she called the control room.

She also stated that she did

not have the procedure with her when changing the filters. The SE

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stated to the inspectors that the RPT was not required to have the

procedure in hand when changing the filters and that she stated to him

that she was not aware of the note. The inspectors verified that it was

not a procedural requirement to have this procedure in hand when

changing filters.

IPR 0lJ monitored noble gas, iodine, and pcrticulate. ODCM, Section

12.2.2, Table 12.2-3, Action 37, stated, in part, that with the IPR 01J

noble gas channel inoperable effluent releases must be immediately

suspenJad.

The inspectors verified the flow pathway for the release was

through the Unit I ventilation stack which was monitored for noble gas,

particulate, and iodine by IPR 028J. The inspectors verified that the

IPR 028J was operable between 5:00 a.m. and 6:00 a.m. on June 20.

The licensee performed the following corrective actions:

The R0 and the RPT were counselled about the importance of knowing

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and understanding procedural requirements.

The licensee determined that this operating crew had previously

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made several errors. Licensee management replaced the SE on this

crew with a more experienced SE. The less experienced SE was

placed with a more experienced crew.

The RP shearvisor stated that RPTs used a check off list when

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performing daily radiation monitor surveillances. The requirement

to verify a containment release was not in progress was added to

the check off list.

Procedure BwRP 5820-7 was changed to incorporate in

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the body of the procedure the required verification

that a containment release was not in progress.

c.

Conclusions

The inspectors concluded that the safety consequence of this event was

small because the release was monitored by IPR 028J and that the amount

of activity released was within the limits of BwRP 6110-13.

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The inspectors concluded that the communications between the Unit 2 and

Unit 1 R0, and between the RPT and the Unit 2 R0 were poor.

The inspectors concluded that the procedure used to change the T'1ters

on IPR 0lJ (BwRP 5820-7) was weak because it had an action statement in a

note instead of in either the prerequisites section or a procedure step.

The note under step 2 of the procedure stated, in part, to ensure that

there were no containment releases in progress prior to proceeding.

The inspectors concluded that the failure to verify that a containment

release was in progress prior to placing the IPR 01J in purge as required

by procedure BwRP 5820-7, " Pro:ess Radiation Monitor Particulate Filter

and Iodine Cartridge Replacement," and the restart of the release

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without obtaining another containment release form as required by BwRP

6110-13, " Containment Vent and Mini Purge Gaseous Effluent" were

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examples of a violation of TS 6.8.1.a.

This licensee identified and

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corrected violation is being treated as a Non-Cited Violation,

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consistent with Section VII.B.1.of the NRC Enforcement Policy (50-

456/96011-03).

07

Quality Assurance in Operations

07.1 Reaular Plant Operations Review Committee (PORC) Meetina

a.

Inspection Scope (40500)

The inspectors reviewed site quality verification (SQV) written

observations from a PORC meeting SQV observed on May 14, 1996. The

inspectors reviewed the station administrative procedure on PORC

meetings, BwAP 1205-13, " Plant Operation Review Committee." The

inspectors also attended a PORC meeting on July 12.

b.

Observations and Findinas

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The SQV written observations of the PORC meeting on May 14 stated that

there were several problems with the meeting.

1.

The meeting started short of a quorum of regular members.

2.

Only two of the seven individuals listed as material presenters

actually attended the meeting.

3.

The attendees had not reviewed the material before the meeting

started.

4.

Material was presented that was still in draft form and was not

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ready for PORC review.

5.

The focus of the reviews conducted was on the number of action

items and not on the correctness and timeliness of the items.

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On July 12, the inspectors observed that a quorum of regular members

were present when the meeting started, all of the presenters were at the

meeting, and the material distributed was in a finalized form and ready

for presentation.

However, the inspectors noted that the presented material was not

distributed until about 8:00 a.m. on July 12. The PORC meeting started

at 11:00 a.m.

Most PORC members were in regularly scheduled meetings

between 8:00 and 10:00 a.m.

This allowed a limited time for premeeting

review.

The inspectors observed that one of the committee members

pointed out an inappropriate action that occurred during one event that

was not listed in the material. This indicated to the inspectors that

at least one member of the committee had reviewed the material even

though limited time was available.

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One agenda item was not discussed during the meeting because the station

manager included an unscheduled discussion on the station's preparedness

for implementation of a new out-of-service procedure the following week.

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The agenda item was moved to the next scheduled PORC meeting.

The

corrective actions for the other two agenda items were rejected based on

the adequacy of the investigations and the corrective actions presented.

This demonstrated to the inspectors that the PORC had the proper focus

on the material presented. The agenda items met the requirements for

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items to be reviewed as described in BwAP 1205-13.

c.

Conclusions

The inspectors made the following conclusions: 1) SQV was effective in

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communicating and the station was effective in correcting the weaknesses

previously observed; 2) there was inadequate time for a premeeting

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review of material by all PORC members; 3) the material reviewed was

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appropriate for the PORC, including the unscheduled discussion on the

out-of-service procedure; and 4) the rejection of the two agenda items

because of the adequacy of the investigations and corrective actions was

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appropriate.

08

Miscellaneous Operations Issues (92700)

08.1

(Closed) URI 50-456/457/95010-03: Waste Gas Valve Mispositioning.

Waste gas oxygen detector instrument sample chamber isolation valve,

0GWO70, was found mispositioned on five separate occasions between May

31 and August 18, 1995. The licensee's review of this situation could

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not establish that any of the mispositionings were deliberate. The

inspectors concluded that the licensee's corrective action (locking the

door to the room where the valve was located) in this specific case was

adequate based on no further occurrences of the valve being found

mispositioned. On May 16, 1996, a violation was issued for the failure

to take corrective actions regarding plant configuration control

problems (50-456/457/96005-05). Tne inspectors verified the corrective

actions for that violation as described in the licensee's response

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letter, dated June 14, 1996, to be reasonable and complete.

Based on

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the corrective action taken in this specific case and the broader based

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corrective actions described in the letter, this item is closed.

08.2 (Closed) URI 50-456/457/95017-01: Configuration Control Problems. The

inspectors identified a trend when three valves were found mispositioned

during the inspection period. On May 16, 1996, a violation was issued

for the failure to take corrective actions regarding plant configuration

control problems (50-456/457/96005-05). The inspectors verified the

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corrective actions for that violation as described in the licensee's

response letter, dated June 14, to be reasonable and complete.

Based on

these actions, this ites is closed.

08.3 (Closed) URI 50-456/457/96008-01: Continued Problems With Out-0f-

Service and Configuration Control. Between March 21 and April 24, the

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licensee identified configuration control problems with 14 separate

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components. On May 16, a violation were issued for the failure to take

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corrective actions regarding plant configuration control problems (50-

456/457/96005-05). The inspectors verified the corrective actions for

those violations as described in the licensee's response letter, dated

June 14, to be reasonable and complete.

Based on these actions, this

item is closed.

08.4 (Closed) URI 50-457/96009-01: Mispositioned 6.9-kilovolt breaker

on May 12 due to miscommunications and a failure to follow

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procedure Bw0P MP-8, " Restoring Unit 2 Main Generator, Main Power

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Transformers 2E and 2W, and Unit Auxiliary Transformers 241-1 and

241-2."

The licensee's investigation determined that the root

cause was poor communications and that corrective actions from

previous events should have prevented this problem. The

inspectors concluded that the failure on May 12, to rack in

breaker 2581, for the Unit Auxiliary Transformer feed to 6.9-

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kilovolt bus 258, when restoring Unit Auxiliary Transformer 241-2,

as required by Bw0P MP-8, was an example of a violation of TS 6.8.1.a. which, in part, required implementation of procedures

recommended in Appendix A, of Regulatory Guide 1.33, " Quality

Assurance Program Requirements (Operations)," Revision 2, February

1978 (Violation 50-457/960ll-04a).

II. Maintenance

M1

Conduct of Haintenance

M2.1 Ju=ner For Controller OPDC-VWOO8

a.

Event (62703)

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On July 10, System Engineering generated Problem Identification Form

(PIF) 456-201-96-1574 to document that a potential unmonitored release

from the radioactive waste (radwaste) building occurred due to a

ventilation supply damper being jumpered cpen. Two aspects of this PIF

were researched by the inspectors: whether an unmonitored release

actually occurred and the administrative controls used to control the

installation of the jumper.

The inspectors reviewed BwAP 400-9, " Maintenance Alterations," BwAP

2321-18, " Temporary Alterations," and work request 960065296. The

inspectors interviewed RP personnel, the system engineer, the instrument

maintenance (IM) first-line supervisor, IM personnel, the system

engineering manager, the IM work planner, and operations shift

personnel. The inspectors also performed a walkdown of the installed

jumper assembly.

b.

Observations and Findinas

Potential Unmonitored Release:

RP and System Engineering personnel

concluded no unmonitored release occurred. This conclusion was based on

air samples taken in the radwaste building, the assumed duration of the

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condition (less than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />), and the activities that were in progress

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when the condition existed. The inspectors were unable to reach the

same conclusion because the bases for the conclusion, including the air

sample results, were not documented and could not be reviewed. However,

due to increased sensitivity by plant personnel regarding the initiating

event, RP planned to perform an analysis of the event and compile

documentation to substantiate their conclusions. The decision t<:

perform the analysis was made on July 23 and the results of the analysis

were scheduled to be reviewed at a plant operations review committee

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meeting on August 16, 1996.

Jumper For Controller OPDC-VW008: On the midnight shift of July 9, the

radwaste building fans were off in the pull-to-lock position with the

supply dampers closed due to a failure of a pressure transmitter.

Operations personnel determined that it was necessary to operate the

radwaste building ventilation system in order to generate more flow up

the auxiliary building stack during a containment release.

l

As part of the work request 960065296 to repair the damper, a pneumatic

jumper without a pressure regulator was installed on controller OPDC-

VW008 to fail tie damper open and allow operation of the ventilation

systea. After the containment release was complete the radwaste

ventilation system was secured. With the damper failed fully open,

radwaste building negative pressure approached 0.0 inches water gauge,

which led plant personnel to conclude that the potential for an

unmonitored release existed. Section 9.4.3.3.2.c of the UFSAR,

stipulated that the ventilation system control radwaste building

negative pressure be at least 0.125 inches negative water gauge.

The jumper was controlled using BwAP 400-9, " Maintenance Alterations."

Use of BwAP 400-9 allowed the jumper to be controlled by the work

request while the work request was still open and work was-in progress.

When the IM first-line supervisor arrived at work for day shift on

July 9, he reviewed the work package from the midnight shift.

Since the

containment release was complete, operation of the radwaste building

ventilation system was no longer required and the system was off. The

IM supervisor stated, upon review of the documentation, that the jumper

should have been covered by temporary alteration controls (as opposed to

maintenance modification controls) if the jumper was to remain in place.

The IM supervisor instructed his workers to remove the jumper and then

notified IM work planners that a temporary alteration was required for

re-installation of the jumper.

Based on discussions with system engineering and operations personnel',

the IM work planners decided to revise the work request on July 9, to

install a temporary jumper with a pressure regulator and control the

jumper using BwAP 400-9, " Maintenance Alterations." The regulator used

in the jumper allowed manual control of the damper. Operators checked

radwaste building pressure twice a shift and adjusted the regulator for

the jumper as needed to maintain building negative pressure greater than

or equal to 0.125 inches water gauge. This jumper was installed on July

9, and was still in place on July 25.

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The inspectors questioned plant personnel on the use of BwAP 400-9,

Maintenance Alterations, instead of BwAP 2321-18, " Temporary

Alterations," to control the re-installation of the jumper.

System

engineering and operations personnel stated that, since the work package

for the damper was still open and the system was not safety-related,

BwAP 400-9 could be used.

The inspectors reviewed the applicable procedures and found guidance

that conflicted with the logic used by the operations and system

i

engineering personnel.

Specific items noted by the inspectors included:

BwAP 400-9, " Maintenance Alterations," step C.3 stated:

-

"If the alteration is to be turned back to the Operating

.

Department, and the item is to be declared operable, then

"

any remaining Temporary Alterations will be documented in

accordance with BwAP 2321-18.

For example, if a work

function is interrupted by the lack of replacement parts and

it cannot be restored to its original design condition and

an alteration has been installed to make the item operable,

BwAP 2321-18 will be initiated."

,

Work request 960065296 was started July 9, and, as of July 25, was

-

ongoing due to unavailability of replacement parts for the

controller. The jumper installed as part of the work package was

still installed to allow operations to run the system. This case

exactly duplicated the example presented in step C.3.

BwAP 2321-18T11, " Determination of Temporary Alterations," step

.

C.1 stated:

"A work request with a Maintenance Alteration Form will not

be used to track temporary installation, removal, or

replacement of equipment if the equipment is of different

form, fit or function than the original; requires different

operating procedures; or requires a change to plant design

documents."

The temporary jumper with the regulator was of different form, fit, and

function than the original equipment. Additionally, since control of

radwaste building pressure was manual instead of automatic, the

operating procedure with the jumper for the radwaste system was

different than with the original equipment.

For these reasons, the

inspectors concluded that the jumper installation should have been

controlled by BwAP 2321-18.

c.

Conclusions

i

Use of BwAP 400-9 to control the second installation of the jumper for

controller OPDC-VWOO8 on July 9 was contrary to the requirements of

procedures BwAP 400-9 and BwAP 2321-18. The failure to follow

procedures was an example of a violation of TS 6.8.1.a, which required

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that procedures be established, implemented, and maintained for

activities covered in Appendix A of Regulatory Guide 1.33 (50-456/96011-

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04b).

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M7

Quality Assurance in Maintenance Activities

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M7.1 Maintenance Report and Self-Assessment

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a.

Inspection Scope (40500)

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+

The inspectors:

1) interviewed the maintenance superintendent and

members of the maintenance staff, and 2) reviewed maintenance department

!

]

self-assessment reports, data, and corrective actions.

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b.

Observations and Findinas

,

Two self-assessment methods were used. The first was a statement by

each sub-department (e.g., mechanical or electrical) head of what were

.

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the strengths and weaknesses of the department.

Each department then

developed a list of strategies / corrective actions to address weaknesses.

The licensee planned to reperform the self-assessment effort every

,

quarter with the next coming due July 31. .The second was a compilation

'

and trending of data from several different sources: maintenance field

monitoring reports, quality control deficiency reports, and station

'

problem identification forms.

The inspectors observed that some sub-departments stated specific

weaknesses, but did not indicate any actions to address the weaknesses.

The inspectors also observed that the compilation of trending data

'

showed that the corrective maintenance backlog was growing. The data

also showed that the average work request age had about doubled, to over

'

200 days, in the past 12 months. The maintenance superintendent stated

that there were several initiatives to make the departments more

efficient in order to bring down the backlog.

For example, senior work'

crew members instead of first line supervisors were making in field

decisions on such things as whether scaffolding should be used and

ordering parts. This took some of the work load off first-line

supervisors. The maintenance superintendent also stated that the reason

the average age of work request had gone up was that many of the work

requests were waiting on unresolved engineering issues. The maintenance

superintendent stated that unbudgeted money had been allotted from Comed

corporate headquarters to accelerate material condition improvements and

some of this money had been allocated to hire contractors to

specifically work off older work requests. The maintenance

superintendent stated that these activities would commence soon, but did

not know exactly when.

c.

Conclusion

The inspectors concluded that the licensee's corrective actions of

removing workload from the first line supervisors and hiring contractors

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to work off longstanding work requests were reasonable corrective

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actions. ; However, some of the departments' assessments lacked depth and

,

did not address all the items identified as weaknesses. The maintenance

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department heads did not state in their assessments the severity of the

weaknesses. The inspectors were unclear whether all the weaknesses

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mentioned were major or if some were just areas that could be improved.

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III. Enoineerina

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El

Conduct of Engineering

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El.1 Ooerability Assessments

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a.

Inspection Scone (37551)

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The inspectors reviewed the operability assessment process and its

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implementation to determine the technical adequacy of selected

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assessments, compliance with 10 CFR 50.59, and conformance to

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UFSAR design requirements, applicable codes &nd standards.

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b.

Observations and Findinas

!

The inspectors determined that a tracking mechanism was not in

place to identify which assessments were still open; which did not

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conform with applicable codes and standards; which did not meet

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UFSAR design requirements; and which involved a condition of a

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structure, system, or component where a compensatory action was

!

needed to ensure functional capability. Also, the existing

tracking process was not proceduralized.

The inspectors requested that the licensee provide a list of open

and completed assessments that identified compensatory and

corrective actions needed to ensure o)erability, including

deviations from UFSAR commitments. T1e licensee could not readily

provide the data requested.

Subsequently, the licensee initiated

a new computer program that would include the status of

assessments and required corrective actions to close any

identified concerns.

The inspectors examined six assessments and found them, in

general, technically adequate. However, the inspectors identified

the following concern regarding operability screening 95-026

(Attachment B).

This assessment was performed to justify

operability of the containment spray additive tank with nitrogen

to the tank isolated for maintenance. The assessment stated that

a nitrogen blanket of approximately 1 pound per square inch gauge

was used to maintain an inert atmosphere in the tank to prevent

degradation of the sodium hydroxide. To enable maintenance on the

pressure control loop, nitrogen would be isolated. The assessment

further stated that this condition was acceptable for up to 30

days, provided the low pressure relief was still operable or the

tank was vented to atmosphere. The assessment concluded that the

30-day isolation of nitrogen would not significantly degrade the

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sodium hydroxide. 'When questioned by the inspectors, the licensee

could not provide documentation of the technical bases or

engineering justification that isolation of the nitrogen for 30

days would not degrade the sodium hydroxide. This is an inspector

followup ites (50-456/96011-05).

c.

Conclusions

The inspectors concluded that, in general, the operability

assessments reviewed were technically adequate; however, the

inability to readily determine the status of open assessments was

a weakness.

E8

Miscellaneous Engineering Issum

E8.1

(Ocen) Violation 93022-Ola:

Inadequate actions to correct auxiliary

building ventilation system construction problems resulting in a fire

door impairment. Due to initial construction scheduling deficiencies

causing the ventilation exhaust ducts to be installed in a tortuous

path, the exhaust systen had more backpressure than it was designed for.

Thus, restricted flow in the ducts caused the fans to operate in or near

the stall region of their operating curve, resulting in the blades being

fatigued by the cyclic backpressure waves in the ducts and subsequently

'

failing when operating with two supply fans and two exhaust fans

running. To prevent this, the auxiliary building ventilation system was

operated in a configuration outside the original design with one supply

fan running and one exhaust fan running, typically resulting 1n a high

differential pressure on the main access door between the auxiliary and

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turbine buildings. A fire door adjacent to the main door was maintained

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open to reduce the pressure on the main door and allow personnel to

safely enter and exit. The Updated Final Safety Analysis Report does

not state how many supply and exhaust fans should have normally been

running. However, the design basis for the auxiliary building exhaust

system, paragraph 6.5.1.1.2.b, states that on a loss of coolant accident

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concurrent with a loss of offsite power, the auxiliary building supply

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and exhaust fans powered by the unit are tripped and two out of six

charcoal booster fans are started to maintain a negative pressure in the

auxiliary building and route exhaust air through charcoal adsorbers and

high efficiency filters before exhausting to the outdoor atmosphere,

The running of one supply fan and one exhaust fan does not appear to

conflict with their design basis.

The licensee was in the process of replacing the cast aluminum

blades of the exhaust fans with forged aluminum blades. The

replacement blades should offer better fatigue resistance to the

apparent cycle fatigue the existing blades were experiencing.

However, because of the long lead time (approximately one year) to

obtain the blades, exhaust duct modifications were currently in

progress downstream of the exhaust fans. These should reduce the

backpressure and allow the existing fans to operate properly.

In

parallel with the modifications, the licensee was actively

evaluating adding an additional intake plenum to the auxiliary

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building which would further reduce the pressure on the existing

personnel door and allow the fire door to be closed. This

modification would also have the advantage of allowing only

filtered air into the auxiliary building. This item remains open

pending the completion of the licensee's actions to address the

fire door impairment.

E8.2

(Closed) URI 50-456/96009-06: 2B SI Pump Room Not Able To Satisfy

Pressure Requirements. This item was opened pending inspector review of

the licensee's resolution of three issues, as described below:

a.

Reason for apparent movement of the caution card hung on the

instrument air (IA) supply valve to controller OPDC-VA192:

The

caution card was moved inadvertently during troubleshooting (by

system engineering and operations personnel) of the failed open

damper on June 3.

The licensee determined that moving the caution

card was not the root cause of damper OVA 303Y failing open. At

some time between January 23 and June 3, damper OVA 303Y opened due

to a combination of two conditions:

The IA supply valve for controller OPDC-VA192 leaked past

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its seat.

An air vent valve for controller OPDC-VA192 that was opened

.

on January 23 was closed. With the IA supply valve leaking

by and the vent valve closed air pressure built up and

opened the damper. This vent valve did not have a caution

card affixed and no other plant controls were 1n place to

ensure the valve remained open.

Efforts by the licensee and

the inspectors to identify the actual date that the vent

valve was closed have been unsuccessful.

b.

Period of time that the refueling water storage tank pipe tunnel

hatch seal was degraded: The exact date that the seal was

degraded has not been determined; however, since the surveillance

test for the 2B SI pump room met its acceptance criteria when it

was performed on January 23, it can be concluded that the seal was

not degraded sufficiently on January 23 to adversely affect SI

pump room pressure. The inspectors concluded the seal degraded

sometime between January 23 and June 3.

A refueling outage

occurred during that period and the hatch was accessed to route

equipment cables for steam generator eddy current testing.

c.

Period of time Unit 2 was unable to meet TS vacuum limit:

The

exact date that damper OVA 303Y failed open was not known; however,

a picture taken in the Unit 2 curved wall area on April 15, showed

that the damper was open. Therefore, from at least April 15 until

June 3, TS 3/4.7.7.d.3 was not satisfied for the 2B SI pump room.

Failure to satisfy pressure requirements for the 2B SI pump room for a

period between at least April 15 and June 3, is a violation of TS

3/4.7.7.d.3.

The root cause of the TS violation was the failure to

,

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maintain proper configuration control over the IA valves that controlled

the damper. On May 16, a violation was issued for the failure to take

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corrective actions for plant configuration control problems (50-

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456/457/96005-05). The inspectors verified the corrective actions for

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that violation as described in the licensee's response letter, dated

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June 14, to be reasonable and complete.

Based on the corrective action

l

taken in this specific case (the damper was repaired and the hatch was

sealed) and the broader based corrective actions described in the

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letter, this item is closed.

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V. Manacement Meetinas

X1

Exit Neeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on July 26, 1996. The

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licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

  • H. G. Stanley, Site Vice President

T. Tulon, Station Manager

  • H. Pontious, Nuclear Licensing Administrator

W. McCue, Support Services Director

R. Flessner, Site Quality Verification Director

  • J. Stone, Maintenance Work Director

R. Byers, Maintenance Superintendent

  • D. Miller, Work Control Superintendent
  • T. Simpkin, Regulatory Assurance Supervisor
  • H. Cybul, System Engineering Supervisor
  • A. Haeger, Health Physics and Chemistry Supervisor
  • F. LeSage, Site Quality Verification Audit Supervisor
  • J. Meister, Engineering Manager
  • D. Cooper, Operations Manager
  • M. Cassidy, Regulatory Assurance - NRC Coordinator

E.C

L. Miller, Chief, Reactor Projects Branch 4

  • C. Phillips, Senior Resident Inspector
  • M. Kunowski, Resident Inspector

IDM

T. Esper

Present at the exit meeting

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INSPECTION PROCEDURES USED

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IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Prob ms

t

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power

l-

Reactor Facilities

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IP 92902:

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

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Opened

50-456/96011-01; 50-457/96011-01

IFI

review UFSAR revision on defueling

50-457/96011-02

URI

review operability of rad monitor

50-456/96011-03

NCV

failure to follow containment

release

procedure

50-457/96011-04a

VIO

failure to follow transformer

,

restoration procedure

i

50-456/96011-04b; CD 457/96011-04b VIO

failure to control jumper

50-456/96011-05; 50-457/96011-05

IFI

justification of 30-day limit for

isolating nitrogen to spray add tank

GlQ1td

50-456/95010-03; 50-457/95010-03

URI

waste gas valve mispositioning

50-456/95017-01; 50-457/95017-01

URI

configuration control problems

50-456/96008-01; 50-457/96008-01

URI

continued problems with out-of-

service and configuration control

'

50-457/96009-01

URI

mispositioned 6.9-kilovolt breaker

50-456/96009-06; 50-457/96009-06

URI

28 SI pump room unable to satisfy

pressure requirements

50-456/96011-03

NCV

failure to follow containment

release

procedure

Discussed

50-456/93022-01a; 457/93022-01a

VIO

inadequate actions to correct

auxiliary building ventilation

system construction problems

50-456/96005-05; 50-457/96005-05

VIO

failure to take corrective actions

regarding plant configuration

control

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LIST OF ACRONYMS USED

1

AFW

Auxiliary Feedwater

CFR

Code of Federal Regulations

HP

Health Physics

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IA

Instrument Air

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IFI

Inspection Followup Item

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IM

Instrument Maintenance

J

IN

Information Notice

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NCV

Non-Cited Violation

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NRC

Nuclear Regulatory Commission

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ODCM

Offsite Dose Calculation Manual

PIF

Problem Identification Form

PDR

Public Document Room

4

I

P&ID

Piping and Instrumentation Diagrams

PORC

Plant Operations Review Committee

R0

Reactor Operator

RPT

Radiation Protection Technician

SE

Shift Engineer

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SFP

Spent Fuel Pool

SI

Safety Injection

SQV

Site Quality Verification

,

TS

Technical Specification

9

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

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VIO

Violation

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