ML20127L140

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Notice of Violation from Insp on 850408-0503
ML20127L140
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 05/30/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20127L118 List:
References
50-414-85-12, NUDOCS 8506270758
Download: ML20127L140 (2)


See also: IR 05000408/2005003

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ENCLOSURE

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NOTICE OF VIOLATION

Duke Power Company

Docket No.

50-414

Catawba Unit 2

License No. CPPR-117

The following violations were identified during an inspection conducted on

April 8 - May 3, 1985. The Severity Levels were assigned in accordance with the

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NRC Enforcement Policy (10 CFR Part 2, Appendix C).

1.

10 CFR 50, Appendix B, Criterion V, and the accepted Quality Assurance (QA)

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program, Topical Report Duke 1A, requires that activities affecting quality

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shall be prescribed by and accomplished in accordance with documented

instructions, procedures, or drawings.

Contrary to the above, on April 19, 1985, temporary operating instruction

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TOI/2/A/6150/01, Initial Filling and Venting of the Reactor Coolant System

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and Control of NC System for NC Cold Hydro, was inadequate and was not

followed during Unit 2 cold hydrostatic testing activities in the following

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instances:

a.

It was not identified in TOI/2/A/6150/01 that there was no overpressure

protection for a portion of the residual heat removal (RHR) system in

that the header into which RHR relief valve 2ND31 discharged was

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isolated and no alternate relief path had been provided.

b.

Motor-operated valves 2NI173A and 2NI1788 were not closed as required

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by TOI/2/A/6150/01 when the reactor coolant system (RCS) was being

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pressurized, thereby allowing RCS pressure into the RHR system.

Items a. and b. above resulted in various piping, valves, and equipment in

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_ portions of the RHR system, boron recycle system, sampling system, and

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chemical and volume control system being overpressured to approximately 2000

psig for approximately three hours on April 19, 1985.

This is a Severity Level IV Violation (Supplement II).

2.

10 CFR 50, Appendix B, Criterion V, and the accepted QA program, Topical

Report Duke 1A, requires that activities affecting quality shall be

prescribed by documented instructions, procedures, drawings...

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' Contrary to the above, on April 20, 1985, TOI/2/A/6150/01 was inadequate in

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that it did not identify that there was no overpressure protection for the

volume control tank (VCT) due to the header into which VCT relief valve

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2NV223 discharged being isolated, and no alternate relief path had been

provided.

This resulted in total destruction of the VCT when it was

inadvertently overpressurized and ruptured during hydrostatic testing

activities.

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8506270758 850530

PDR

ADOCK 05000413

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Duke Power Company

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Docket No.

50-414

Catawba Unit 2

License No.

CPPR-117

This is a Severity Level IV Violation (Supplement II).

Pursuant to 10 CFR 2.201, you are required to submit to this office within 30

days of the date of this Notice, a written statement or explanation in reply,

including:

(1) admission or denial of the alleged violations; (2) the reasons

for the violations if admitted; (3) the corrective steps which have been taken

and the results achieved; (4) corrective steps which will be taken to avoid

further violations; and (5) the date when full compliance will be achieved.

Security or safeguards information should be submitted as an enclosure to

facilitate withholding it from public disclosure as required by 10 CFR 2.790(d)

or 10 CFR 73.21.

Date:

MAY 3 01965

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