ML20127F261

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Insp Repts 50-424/92-27 & 50-425/92-27 on 921025-1128.One non-cited Violation Noted.Major Areas Inspected:Plant Operations,Surveillance,Maintenance,Review of Corporate Engineering & Design Change Support & follow-up
ML20127F261
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 12/21/1992
From: Balmain P, Brian Bonser, Skinner P, Starkey R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20127F210 List:
References
50-424-92-27, 50-425-92-27, NUDOCS 9301200183
Download: ML20127F261 (16)


See also: IR 05000424/1992027

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UNITfD STATES

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NUCLEAls REGULATORY COMMISSION

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101 MARIETTA STREE T, N.W.

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ATLANTA. GEORGI A 30323

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Report Nos.:

50 424/92-27 and 50-.425/92-27

Licensee: Georgia Power Company

P. O. Box 1295-

Birmingham, AL 35201

Docket Nos.:

50-424 and 50-425

License Nos.:

NPF-68 and NPF-81-

Facility Name:

Vogtle 1 and 2

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Inspection Conducted:

October 25 - Noveniber 28, 1992

Inspector:

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Bh R. Bon.ser, Senior Resident Inspector

Date Signed

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A .,5 Kr$ey, Resident Inspector

Date Signed

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P. ATBalinaT67 Resident inspector

Date' Sighed

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Accompanied by: J

. Starefos ,

Approved by:

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P' Skinner / Chief

Date Signed

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Reactor Projects Section 3B

Division of Reactor Projects

SUMMARY

Scope:

This routine, inspection entailed-inspection in the following

areas: plant operations, surveillance, maintenance,-review of-

corporate engineering and design change support,- and follow-up.

Results:

One non-cited violation (NCV) was . identified.-

The NCV involved the failure of-the site to act upon-information

provided from the corporate office regarding a potential valve

operability issue.

The issue-involved the identification of-

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- several safety related motor operated valves (MOV) that may not

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- develop sufficient thrust to operate under certain: differential

pressure (DP) conditions that could be experienced during the

recirculation phase of' safety injection (paragraph' 2d).

The 1A diesel generator (OG) exp2rienced a failure to start.during

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testing. When the operator depressed the manual push button -in an-

9301200183 921221

ADOCK 0500

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attempt to start the DG, 'the engine . failed to roll. A similar

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incident occurred in July 1990 (paragraph 2f).

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During the. inspection period the_ licensee performed a procedure to

ensure the centrifugal charging pump alternate mini-flow relief

lines were filled and vented.

Both Unit I and ? lines contained a

minimal amount of air. While performing the procedure the

licensee determined that the setpoints on the Unit 2 relief valves

had drifted outside their required tolerances.- A review of the

work order history on these valves by the licensee and resident-

inspectors did not provide an explanation for the setpoint drift-

(paragraph 4b).

The inspectors observed the licensee's annual re-call drill.

Scheduling the drill on the Thanksgiving holiday week proved

beneficial because it utilized personnel in positions they did not

normally fill. Overall the licensee's response to the drill was

satisfactory and the objectives were met (paragraph 29).

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REPORT DETAILS

1,

Persons Contacted

Licensee Employees

  • J. Beasley, Assistant General Manager Plant Operations
  • P. Burwinkel, Plant Engineering Supervisor

S. Bradley, Reactor Engineering Supervisor

W. Burmeister, Manager Engineering Support

  • S. Chesnut, Manager Engineering Technical Support

C. Christiansen, Safety Audit and Engineering Review Supervisor

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  • C. Coursey, Maintenance Superintendent

G. Frederick, Manager Maintenance

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  • B. Gabbard, Nuclear Specialist'
  • M. Griffis, Manager Plant Modifications

M. Hobbs, Instrumentation and Controls Superintendent

  • K. Holmas, Manager Health Physics and Chemistry

D. Huyck, Nuclear Security Manager

  • W. Kitchens, Assistant General-Manager Plant Support
  • R. LeGrand, Manager Operations
  • G. McCarley, Independent Safety Engineering Group Supervisor

R. Moye, Plant Engineering Supervisor

  • M. Sheibani, Nuclear Safety and Compliance Supervisor
  • W. Shipman, General Manager Nuclear Plant
  • C. Stinespring, Manager Administration

J. Swartzwelder, Manager Outage and Planning

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C. Tynan, Nuclear Procedures Supervisor

  • J. Williams, Supervisor Work Planning and Controls

Other licensee employees contacted included tcchnicians, supervisors,-

engineers, operators, maintenance personnel, quality control inspectors,

and office personnel.

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Oglethorpe Power Company Representative

  • T. Mozingo

NRC-Resident Inspectors

  • B.

Bonser

  • D. Starkey

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  • P. Balmain
  • J. Starefos
  • Attended Exit Interview

An alphabetical list of-abbreviatia s is located h the last paragraph-

of the inspection report.'

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2.

Plant Operations - (71707)

a.

General

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The inspection staff reviewed plant operations throughout the

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reporting period to verify conforman'ce with regulatory require .

ments, Technical Specifications (TS), and administrative controls.

Control logs, shift supervisors' logs, shift relief records,

limited Condition for Operation (LCO) status logs, night orders,

standing orders, and clearance logs were routinely reviewed.

Discussions were conducted with plant operations, maintenance,

chemistry and health physics, engineering support and technical

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support personnel.

Daily plant status meetings were routinely

attended.

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Activities within the control room were monitored during shifts

and shift changes.

Adions observed were conducted as required by

the licensee's procedures.

The complement of licensed personnel

on each shift met or exceeded the tninimum required by TS.

Direct

observations were conducted of control room panels, instrumenta-

tion and recorder. traces impurtant to safety. Operating parame-

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ters were observed to verify they were within TS limits. The

inspectors also reviewed Deficiency Cards (OCs) to determine

whether the licensee was appropriately documenting problems and

implementing corrective actions.

Plant tours were taken during the reporting period on a routine

basis.

They included, but were not limited to the turbine build-

ing, the auxiliary building, electrical equipment rooms, cable

spreading rooms, Nuclear Serdce Cooling Water System (NSCW)

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towers, Diesel Generator (UG) buildings, Auxiliary Feedwater

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System (AFW) builditas, and the low voltage switchyard.

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During plant tours, housekeeping, security: equipment status a1d

radiation control practices were observed.

The inspectors verified that the licensee's health physics (HP)

policies / procedures were followed. This included.nbservation of

HP practices and review of area surveys, radiation work permits,

postings,-and instrument calibration.

The inspectors verified the the security organizition was proper-

ly manned and security personnel were capable of performing their

assigned functions; persons and packages were chu ked prior to

entry into the Protacted Area (PA); yehicJes sera properly

authorizeA searctied, and escorted witMn the'M; persons within

the PA displayed photo identification badges; and personnel in

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vital uen were 7 uthorized.

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b.

Unit 1 Summary

The unit began the period operating at 100% power and operated at

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full power throughout the inspection period.

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c.

Unit 2 Summary

The unit began the period operating at 100% power and operated at

full power throughout the inspection period.

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d.

MOV Operability Review

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During an NRC Headquarters audit of the Vogtle Motor Operated.

Valve (MOV) program (G.L. 89-10) during the week of November 9 at

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the licensee's corporate office in Birmingham, Alabama, a concern

was raised associated with the timeliness of the licensee's

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implementation of corrective acH on. The issue involved the

identification of several- safet; related MOVs that may not develop -

sufficient thrust to operate under certain postulated DP

conditions. An example of this is the inability of these motor

operators to close _and isolate-a passive failure leak. This

requirement to consider a passive failure leak is only applicable

during the recirculation phase of safety injection.

The corporate en0ineering group analyzing the M0V thrust require-

ments transmitted this information to the plant. A Standing Order

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(C-92-07) was developed which would require certain operator

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actions to reduce the DP across the valves under certain passive-

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failure conditions.

The Standing Orcer contained detailed steps

to start or stop Residual Heat Removal (RHR) pumps or Centrifugal

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Charging Pumps (CCP), and to sequence valve operation to reduce

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the system DP to ensure that the valves in question would operate.

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The inspectars identified two concerns after a review of the-

compensatory actions in the Standing Order and the details

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surrounding the transmittal of the potential = operability concern

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from the corporate office to the site

One concern involved the

timeliness of actions.

The initial dis'covery of the potsM ial

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valve operability issue was in January 1992, and the compensatory

actions described above were not-implemented by:the site until-

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November 11, 1992. The site had been verbally informed of this

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issue in January'but had not taken any action.

Normally when the-

site is notified by formal correspondence from the corporate

office of an action, the item is entered into the site commitment

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tracking system.

in this case that d H not occur.

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The other concern was associated with tb uyo of Standing Orders.

The detailed information contained in'Abe StMding Order is the

type of information that would normally be contained in an abnor-

mal operating procedure (0P) or emergency operating procedure

(EOP).

The inspectors were concerned that this dnailed operating

information may not be appropriate in a Staading Order since the

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standing order does not receive the same level of review as a

procedure.

Normally the Plant Review Board (PRB) is responsible

for review of E0Ps and abnormal operating procedures.

In this

case, revisions were made to the E0Ps incorporating the operator

actions for a passive failure. When the E0P thanges were reviewed

by the PRB a decision was made to prepare a Standing Order instead

of revising the E0Ps.

The PRS decided that t'ne revised E0Ps could

be misleading to the operators curing an event and that it was

safer and more appropriate to place thest instru;tions in a

Standing Order.

The licensee reviewed the innpectors concern

regarding the us , and impiementation of Standing Orders and has

$nitiated a Standing Order revisk by the Independ:nt Safety

Engineering Group (ISEG). The iH pectors will monitor the ISEG

review.

The failure of the site to perfc. m a timely evaluattan of the

valve operabil:ty information anc promptly issue comrensatory

actions is a violat'on of 10 CFR Ch Aependix 0 Criterion XVI,

Corrective Action.

Criterion XVI ,cluires that cosAttions adverse

to quality be promptly identified And corrected-

This violation

will not be subject to caforces ent actinn t'cause the licensee's

efforts in ided ifying and arrecting the Violatic meet the

criteria specifici in 56ction VII.B of the Enfo.cthsuit Policy.

This violatien . ideid if f ed as Non-cite. Violation (NCV)

Sp-424,425/92-?7-01: Failure Te .ake Ytnely Corrective action On

Potential M0t' Uperabil ity Issue,

e.

Engineering Perscanel Qualifications

During the revior of the MOV program several of the lices.2ee

calculations to seppcrt the MGV program were resiewed.

The

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inspectors reviewed the qualification and training of seseral of

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the engineers that perigrmed these calculations.

The requirements for personnel qualificatica are contained in TS 6.3.1.

This TS requirss that personnel meet the minimum education

and experience of Regulatory Guide 1.8, Revision 2.

The TS also

allows a person to perform specific task as long as they are

trained and qualified.

The treining and qualification require-

mentt are also spec (fied in southern C7mpany Services (SCS) Plant

Vogtle Operational Support Policy and Procedure Manual 010604.2-1

dated October 31, 1987

Training and qualification information for four mechanical and

three electrical engineers was reviewed by the inspectors. The

records indicate that all of the personnel were well experienced

and qualified and met the minimum training requirements.

However,

due to changes in required training there were varying degrees of

training records in the individual folders.

There was no master

index as to what records were needed making record auditing

di f ficul t . The inspectors observations in this area were

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discussed with engineering management during the audit debrief on

November 13, 1992.

f.

Diesel Generator lA Failure

At 2:22 a.m., on November 18, 1992, with Vogtle Unit I at 100%

power a control room operator attempted to start the 1A DG for a

normal monthly surveillance.

When the operator depressed the DG

start push button the DG did not start.

Shift supervision at that

time believed that the operator had not held the manual start push

button a sufficient length of time to start the diesel.

Further

investigation by shift personnel did not identify any evidence of

a problem and DG 1A was started successfully at 2:34 am.

The DG

ran without further problems and the surveillance was completed

satisfactorily.

A similar incident had occurred in July 1990.

The investigation

into that event revealed that once the DG start push button is

depressed the electrical relays close resulting in initiation of

the sequence to air roll the diesel engine. The 1990 event had

been caused by malfunctioning air start pilot valves.

All

operations personnel had been trained on this incident.

On November 18, licensee management, upon being informed of the DG

1A malfunction, declared the DG inoperable as of 2:22 a.m.,

and

initiated an investigation into the cause of the DG failure to

start.

Based on the indications following the failure, event

investigation efforts focused on the air start system.

Follow-up

on this DG failure will be documented in NpC Inspection Report

(IR) 50-424,425/92-30.

g.

Drill Observation

On the evening of November 24, the inspectors observed an after

hours recall drill. The major objectives of the drill were to

make off-site and on-site notifications, to recall off-duty

personnel, to timely activate the emergency response facilities

(TSC, OSC & EOF) after normal working hours, and to perform a site

assembly and accountability.

The licensee concluded that the

objectives of the drill were met. The inspectors made the

following observations:

a number of key management / supervisory

personnel were on vacation at the time and many positions were

filled by individuals that were trained in their position but had

little experience in performing their duties in these positions;

the TSC was activated in about an hour, however, personnel

arriving first were not thoroughly familiar with the set-up of the

facility; TSC personnel were unsure how to activate the status

loop between the CR and the TSC; emergency facility managers did

not appear to fully understand their options on individuals that

did not meet Fitness for Duty (FFD) requirements on alcohol

consumption, although their actions were correct.

The inspectors

will review the licensee's follow-up actions.

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The inspectors concluded that scheduling the drill during the

Thanksgiving holiday week proved beneficial since it utilized

personnel in positions they did not normally fill. Overall the

licensee's response to the drill was satisfactory and the objec-

tives were met.

h.

Unplanned Pressurization of RHR Suction Piping

On November 23, Unit 1 Control Room Operators observed an increase

in RHR pump suction pressure for both trains of RHR. Subsequent

investigation revealed that during a Post Accident Sampling System

(PASS) sample of the Reactor Coolant System (RCS) back leakage

occurred through several PASS valves (3/8 inch sample line)

resulting in pressurization of the RHR pump suction piping.

According to an Emergency Response Facilities (ERF) printout, the

pressure in the RHR suction piping increased to approximately 500

psig (suction relief setpoint 450110 psig), at which time the

suction relief valves, 1-PSV-8708 A/8, lifted slightly and

relieved pressure to the Pressurizer Relief Tank (PRT).

The

relieving of the suction relief valves maintained the RHR system

below its design pressure of 600 psig. However, the licensee is

investigating the apparent discrepancy between the actual _ and-

required relief valve setpoints (DC 1-92-216.) The event was

terminated by the isolation of the PASS system and

depressurization of the RHR system. At no time during the event

was the relief capacity of the relief valves approached by the

leak through the PASS system. The licensee has initiated an

interim corrective action by attaching a " Caution Tag" to the to 1

HV-8220, RCS Hot' Leg Pass Sample Isolation Valve, handswitch

located in the Control Room. The tag requires licensed operators

to " monitor RHR pressure when 1 HV-8220 is open, and if the RHR-

pressurizes, then shut 1-2702-04-012," a manual isolation valve

near the PASS panel. The licensee has written a Design Change

Request,93-005, to add a check valve rated for RCS pressure and

temperature between the PASS Sample Cooler Rack and valve 1-2701-

U4-012.

This design change will be incorporated in a Mi_nor

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Departure from Design (MDD).

The same problem was identified on

Unit. 2 during construction and a check valve was installed-to

correct the problem. As a result, Unit 2 has not_ experienced the

back leakage problems of Unit 1.

The inspectors will follow-up on

the. licensee's long term corrective actions'and investigation into

the relief valve setpoint discrepancy.

One non-cited violation was identified.

3.

-Surveillance Observation.(61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy.

The completed tests reviewed were examined

for necessary test prerequisites, instructions, acceptance criteria,

technical content, data collection, independent verification where

required, handling of deficiencies noted, and review of completed work.

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The tests witnessed, in whole or in part, were inspected to determine .

that approved procedures were available, equipment was calibrated,

prerequisites were met, tests were conducted according to procedure,

test results were acceptable and systems restoration was completed.

Listed below are surveillances which were either reviewed or witnessed:

Surveillance No.

Title

14644-2

SSPS Slave Relay K 643 Train A Test

Containment Spray

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28911-1

Weekly Class lE Battery Inspection

Unit 1-C train

14806-2

Containment Spray Pump and Check

Valves Inservice Test

24812-1

Delta T/T Avg loop 3 Protection

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Channel II ACOT

14980-2

Diesel Generator Operability Test B-

Train

14701-1

A-Train, Reactor trip Breakers UV &

Shunt Trip Test

24555-1

Containment H2 Monitor Train A ACOT

and Calibration

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14986-C

Security DG Operability Test

No violations or deviations were identified.

4.

Maintenance Observation (62703)

a.

General

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The inspectors observed maintenance activities, interviewed

personnel, and reviewed records to verify 1that work was conducted

in accordance with approved procedures, TS,'and applicable indus-

try codes and standards.

The inspectors also frequently verified-

that redundant components were operable, administrative controls

were followed, clearances were adequate, personnel were qualified,

correct replacement parts were used, radiological controls were

proper, fire protection was adequate, adequate post-maintenance

-testing was performed, and independent verification-requirements

were implemented.

The -inspectors independently: verified .that

selected equipment was properly returned to service.

Outstanding work requests were reviewed to ensure that the licens-

ee gave priority to safety-related maintenance activities.

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The inspectors witnessed or reviewed the following maintenance-

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activities:

MWO NOS.

WORK OESCRIPTION

29203020,3021

SG 3 & 4 Water Level Control

19201861

Battery Cell Replacement

19202700

DG Sequencer Board Investigation (UV

Detection Channel 2)

A9201246

Relief Valve Test Proc. 28207-

T-0PER-92-05

CCP Alternate Mini-flow Relief Valve-

Venting Unit 1

T-0PER-92-06

CCP Alternate Mini-flow Relief Valve

Venting Unit 2

19203033

DGlA Air start Investigation

b.

Failure of Unit 2 CCP Alternate Mini-flow Relief Valves During Venting

On October 26, the licensee approved procedures T-0PER-92-05 and

T-0PER-92-06, CCP Alternate Mini-flow Relief . Valve' Venting, for

Units 1 and 2 respectively.

The purpose of the procedure was to

provide a temporary means-to vent the CCP' alternate. mini-flow

piping. through relief valves until a permanent change can be

implemented in response to failures of a similar mini-flow design

at the Shearon Harris plant Information Notice (IN) 92-61).

The

procedure was successfully performed on Unit 1 on November 5.

The

inspectors witnessed performance of the procedure on both Unit 1

trains, did not observe any discrepancies, and noted that the

relief valves lifted within their allowable set-point range.

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valves were vented by-injecting demineralized water into the

alternate mini-flow piping using a small hand pump, which in--

creased the line pressure to the point at which the relief valve

would lift and vent any trapped air. A pressure gauge was in-

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stalled on the piping to monitor the venting and relief valve

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lifting. The inspector did not-detect significant amounts of air

vented during this process on either train.

On November 6, the-inspectors observed the licensee venting-the

Unit 2 B train CCP alternate mini-flow piping. During the'perfor-

mance of- the procedure, relief valve 2PSV-8510B lifted at- approxi-

mately 2400 psi.

The valve is required to lift at 2200166_psig.

The licensee declared CCP B inoperable and entered 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LC0'for

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TS 3.5.2, ECCS Subsystems. The licensee replaced the relief valve

with a spare valve under Maintenance Work Order (MWO) 29203358 and

exited the LC0 on November 7.

The inspectors observed subsequent =

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bench testing of the malfunctioning valve and noted that the valve

lifted consistently at about 2400 psig.

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On November 10, the inspectors observed the licensee venting the

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Unit 2 A train CCP alternate mini-flow piping.

Relief valve 2PSV-

8510A began lifting at approximately 1960 psig, which is below its

required setpoint.

The procedure was subsequently reperformed

using an air driven hydro pump. The relief lifted consistently at

approximately 2050 psig u' sing this pump.

The licensee then

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declared CCP A inoperable and entered the LCO.

The LC0 was exited

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based on verbal determination from Westinghouse that operability-

was not affected by the low setpoint.

The Westinghouse deter-

mina; ion was based on a revised calculation of ECCS flow rates

based on the A-train CCP alternate mini-flow relief valve being

fully open at 90% of 1960 psig and concluded that the lower relief

pressure did not have an adverse affect on the accident analyses.

The licensee replaced the valve on November 11.

The inspectors were initially concerned that the improper relief

pressures indicated that the relief valves had been improperly

calibrated or that previous maintenance activities resulted in a

change to the relief valve setting.

Based on this concern the

inspectors reviewed the MWO history of the unit 2 valves. This

review identified that the A-train valve (2PSV-8510A) was last

verified by bench testing and lifted at the required setpoint in

April-1990. The valve was then placed in storage and-in October.-

1991, was installed in the CCP A alternate mini-flow piping.

This

valve has had two previous instances where the "as'found"

setpoints were-low.

The valve was reworked following both of_-

these instances. The B train valve (2PSV-85108) was last verified-

to lift at the required setpoint in April 1992.

The valve had

been reworked due to leakage prior on two prior occasions. The

MWO history did not reveal any abnormal lift setpoints.

As part of the corrective actions, since the cause of the

setpressure drifts could not be determined, the licensee currently

plans for a vendor representat.ive to validate the bench testing

procedure and to witness disassembly of the two relief' valves.

The inspectors reviewed the followup letter submitted to the

licensee from Westinghouse.

The inspectors concluded that the-

licensees actions were appropriate following_ discovery of the

failures and have no immediate concern with the operability of the-

CCP subsystems since the reliefs were replaced _with properly.

calibrated spares. The inspectors will ' follow this investigation,

c.

Unit 1 Battery Cell Failures-

In NRC IR 92-23 :the~ inspector noted a declining trend in the

performance of the Unit I lE station batteries.

During this

inspection period a cell in the _ID battery failed TS cell float

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voltage surveillance requirements and a _ cell in the IC battery did

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not meet TS category A float voltage limits and marginally met- the-

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category B allowable limits.

Both cells were replaced. Cell # 12

in the 10 battery failed its surveillance requirements on-

October 29, when its float voltage was measured at 2.068 volts.

Before failing the surveillance this cell was being tracked by the

licensee as a problem cell due to its erratic voltage trend. The

inspector observed the replacement of this cell.

Prior to its

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removal the inspector was shown a cloudy rust-like discoloration

in the electrolyte solution localized to the lower one inch of the

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cell jar. The licensee has noted this discoloration in the last

two or three failures.

On November 4, float voltage on cell #38

in the 1 C battery was measured at 2.101 volts and was replaced.

The ins)ector questioned why the licensee did not immediately

enter tie two hour LC0 action statement since the initial reading

was 2.10 volts.

The inspector found that the initial reading was

confirmed with a more accurate voltmeter. .This reading was 2.101

volts which is greater than the TS allowable limits.

The licensee

replaced this cell shortly after performing the surveillance.

In NRC IR 92-23 it was noted that the licensee has plans to

replace, during the next Unit I refueling outage, those original C

train battery cells that have not already been replaced. The

licensee decided during this inspection period to replace the

entire battery with new cells during the next Unit I refueling

outage. Replacing the entire battery will ensure uniform cell

voltage characteristics.

Prior to initial operation of Unit 1 a

large number of cells were replaced in the C battery. This may

have caused a non-uniform cell voltage behavior and contributed to

the recent cell failures.

The inspector reviewed the major loads which are supplied by the C

train DC electrical system and noted that it supplies loads for

the turbine driven auxiliary feedwater pump (TDAFW) and Channel

III vital AC instrumentation.

The inspectors were concerned with

the performance of the C battery since it provides power to the

TDAFW system.

The inspector observed single cell discharge tests on two cells

that had been removed.

Cell #38 from battery IC was determined to

have 112% of its design capacity and cell #12 from battery 10 had

100% of its design capacity.

The-inspector also discussed with

engineering personnel the affect of a failed cell- if it were to

remain in the battery.

During a full discharge, a cell with

reduced capacity could discharge to a level lower than the rest of

the battery, possibly reverse polarity, and ultimately reduce the

capacity of the entire battery.

Based on the results of the

single cell discharge tests, the inspectors concluded that the C

train and D train batteries will fulfill their safety function

prior to replacement of the two cells.

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d.

Storage of Transient Materials Near Safety Related Equipment

,

In August 1992, the licensee initiated a Request for Engineering

Review,(RER)- 92-0298, to identify areas in the plant where

material is stored which could interact with safety related or

Seismic Category 1 components.

Seismic components which may

experience interaction with unrestrained equipment during an Safe

Shutdown Earthquake (SSE) were identified by Operations,

Chemistry, and Maintenance Departments. Once identified,-the

storage areas were divided into areas that represented

unacceptable potential interactions and where-items should be

secured in place, areas where items can remain in place without

restrictions, and areas where no storage would be permitted. The

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licensee acted promptly to take the actions recommended by the RER

by identifying suitable auxiliary building equipment storage

locations and moving items where necessary. The original scope of

the RER considered only the auxiliary building, the fuel handling

building, and the control building. The licensee expanded the

scope of this review to include fire water pump houses, liquid

nitrogen storage facility, NSCW chlorination building, the main

steam valve rooms, the NSCW towers, the DG buildings, the AFW pump

houses, and additional rooms within the control building.

The inspector performed a walkdown of storage areas in both

auxiliary buildings. The licensee has made_significant progress

in moving or securing transient materials and in identifying these

rooms suitable for use as storage areas.

Some equipment, such as

welding machines, must be anchored in place and a plan is being

developed (RER 92-0438) to ensure that-a proper method is used to

restrain such equipment.

Rooms that will be used as designated

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storage areas will be clearly labeled as such.

Prior to RER 92-

0298, the licensee had previously designated a "high radiation"

storage area on level 1 of the auxiliary building where transient

high radiation items are stored until processed for offsite

disposal.

'

A follow-up RER, RER 92-0439, has been initiated which will

evaluate other areas in the fuel handling building and the

auxiliary building which were not identified in RER 92-0298. The

inspector determined that_the licensee is_taking appropriate

actions to control storage of transient materials to prevent

interaction with safety related or seismic category 1 components.

The inspectors will monitor the progress of this licensee

initiative during future plant walkdowns.

No violations or deviations were identified.

5.

Review of Corporate Engineering and Design Change Support (40703, 37838)

During this reporting period the inspectors visited the Southern Nuclear

Operating Company offices.in Birmingham, Alabama. The_ objective of the-

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visit was to review current activities of corporate engineering and

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licensing which support Vogtle. The inspectors met with representatives

q

of Southern Nuclear and Southern Company Services which provides the

engineering support for Southern Nuclear.

Each person contacted

discussed current projects in their area of responsibility which

directly related to support of site activities.

Discussions with the Southern Nuclear Manager of Maintenance and Support

highlighted several areas of ongoing work in support of the site.

These

included support in the resolution of several current plant problems and

areas of improvement.

The inspectors also reviewed several licensing

activities with the Licensing Manager and reviewed a list of current TS

submittals.

The inspectors received an update on the status of the

Individual Plant Examination (IPE) which the licensee plans to submit by

the end of 1992.

The licensee has determined that no design changes are

necessary based on the projected results of the IPE.

The Southern Nuclear Manager of Engineering for Vogtle discussed his

group's interface with the site engineering group. .He particularly

emphasized the goal of completing design change package.t at least six

months prior to implementation on site.

This goal was previously

discussed in NRC IR 92-04 and the licensee appears at this time to be

completing the reviews and submitting the change packages to the site

prior to the six-month time frame. This gives the site sufficient time

to prepare for implementation.

During.the design review process, status

meetings are held at 10%, 50%, and 90% completion stages so that DCP

progress can be reviewed and necessary changes made prior to package

completion.

Southern Nuclear engineering personnel attempt to meet on

site with their counterparts once per month to discuss program status.

The inspectors met with representatives of SCS and discussed several

ongoing projects. One project of particular interest to the inspectors

was the long term project to install an Integrated-Plant Computer to

replace Proteus, ERF,-Emergency Response Data System, and the Radiation

Monitoring System.

These modifications will be completed during' future

refueling outages.

The inspectors noted the wide range of projects being performed for the.

site by corporate support departments.

The prevailing attitude at

Southern Nuclear is that the corporate staff functions to support the

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site.

This attitude is reflected in the professionalism of the corpo-

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rate staff and the good working relationship which appears to exist

.between the corporate staff and the site.

6.

Follow-up (92701)

(Closed) Part 21 50-424,425/P21-136, Defect-In'DSRV-16-4 Enterprise

Standby DG Jacket Water _ Pump Shaft Caused by Incorrect Tapers Machined

-on Shaft.

On September 4,1992, Cooper Industries notified the licensee of a

potential defect with the jacket water pump shaft of the DSRV-16-4

Enterprise Standby _DG.

The cause of the defect was incorrect machining

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of the pump shaft taper on thafts supplied by a vendor to Cooper-

Enterprise. Only 8 shafti purchased by two other utilities were known

to have the defect, but because there was the possibility of the defect

being present in previously supplied parts, all utilities hich had

receised jacket water pump shaf ts from the affected it.t were included in

the notification.

Vogtle determined that three shafts from the affected lot,02-425 03 AF,

are in warehouse stores,

inspection by the licensee, vendor, and

resident inspector, determined that none of the three spare shafts were

defective. Also, as described in the Part 21 notification, due to the

physical differences between the jacket water pump ge'tr and the

incorrectly machined shafts, it is unlikely that a defective shaft could

be assembled in a jacket water pump.

Even if assembly were to occur,

shaft failure would occur within a short period of time.

Vogtle has

experienced many operating hours on the existing installed jacket water

pumps with the pumps performing as designed.

The inspector concluded that Vogtle does not have in inventory any of

the defective jacket water pump shafts as described in the Part 21

notification.

1his item is considered closed.

7.

Exit Meeting

The inspection scope and findings were summarized on November 30,

1992, with those persons indicated in paragraph 1.

The inspector

inspected and discussed in detail the inspection

described the a-

t

findings listed

)w.

No dissenting comments were received from the

licensee,

lhe i

isee did not identify as proprietary any of the

material providea o or reviewed by the inspectors during the inspec-

tion.

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2

JT[M NO._

[LEJCRIPTION AND REFER [!4C[

NCV 424,425/92-27-01

Failure to Take Timely Corrective Action

on Potential MOV Operability issue. (Para-

graph 2d)

8.

Abbreviations

AC

- Alternating Current

ACOT

- Analog Channel Operational Test

AT W

- Auxiliary feedwater System

CCp

- Centrifugal Charging Pump

CfR

- Code of federal Regulations

CR

- Control Room

DC

- Deficiency Card

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DG

- Diesel Generator

DP

- Differential Pressure

DSRV

- Designation for Diesel Engine

ECCS

- Emergency Core Cooling Systems

EDG

- Emergency Diesel Generator

EOF

- Emergency Operations facility

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ERDS

- Emergency Response Data System

E0P

- Emergency Operating Procedures

ERT

- Emergency Response facilities

ESTAS

- Engineered Safety Feature Actuation System

ffD

- fitness for Duty

I&C

- Instrumentation and Controls

IN

- Information Notice

IPE

- Individual Plaat Examination

IR

- Inspection Report

ISEG

Independent Safety Engineering Group

LC0

- Limiting Condition for Operation

MDD

- Minor Departure from Design

MOV

- Motor Operated Valve

MWO

- Maintenance Work Order

NCV

Non-Cited Violation

NRC

- Nuclear Regulatory Commission

NRR

- Office of Nuclear Reactor Regulation

NSCW

- Nuclear Service Cooling Water System

OSC

- Operations Support Center

PA

- Protected Area

PASS

- Post Accident Sampling Svstem

PRD

- Plant Review Board

PRT

- Pressurizer Relief Tank

PSIG

- Pounds per Square inch - Gaugo

RCS

- Reactor Coolant System

RER

- Request for Engineering Review

RHR

- Residual Heat Removal

Reactor Protecti9n S). tem

RPS

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Safety Audit And Engineering Review

SAER

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SCS

- Southern Company Services

Steam Generator

SG

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SSE

- Safe Shutdown Earthquake

SPDS

- Safety Parameter Display System

SSPS

- Solid State Protection System

TDAFW

- Turbine Driven Auxiliary feedwater System

TS

- Technical Specifications

TSC

- Techrical Support Center

USS

- Unit Shift Supervisor

UV

- Undervoltage

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