|
---|
Category:ARCHIVE RECORDS
MONTHYEARML20236S0921998-07-17017 July 1998 Audit Rept,Commitment Mgt for Tva,Sequoyah Nuclear Plants, Units 1 & 2 ML20138D1891997-02-28028 February 1997 Special Project Rept Audit 97-901S, Concerns Resolution Program-Sequoyah Nuclear Plant ML20138D2331997-02-28028 February 1997 Special Project Rept Audit 97-920S, Concerns Resolution Program-TVA Nuclear, Feb 1997 ML20133F3721997-01-14014 January 1997 Press Release II-97-08, NRC Staff Proposes $100,000 Fine Against TVA NRC Staff Also Prohibits TVA Executive from Involvement in NRC-Licensed Activities ML20132G8741996-12-26026 December 1996 Press Release II-96-105, NRC Staff Proposes $100,000 in Fines Against TVA at Sequoyah ML20135D0741996-12-0606 December 1996 Press Release II-96-100, NRC Staff to Hold Predecisional Enforcement Conference to Discuss Sequoyah Equipment Concerns W/Tva ML20134L3011996-11-20020 November 1996 Press Release II-96-97, NRC Staff Proposes $50,000 Fine Against TVA at Sequoyah ML20116J5221996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5251996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5361996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5391996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5441996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5411996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5171996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5151996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5091996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5051996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5021996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J4971996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20058P1321993-12-23023 December 1993 Package Containing Answers to Questionnaire Re Employee Concerns Programs ML20065B7811993-06-18018 June 1993 Degraded Voltage Analysis ML20086H9851991-11-27027 November 1991 Evaluation of Block Clamps at Welds Near Valves 0-67-1514 & 2-67-1513 ML20028G8361990-08-21021 August 1990 Foundation Investigation of ERCW Pumping Station Foundation Cells. ML20029A0061990-08-0303 August 1990 Rev 0 to SQN-00-D052 EPM-AMJ-073190, Fire Hazard Analysis of Unit 2 App R Cables in Boric Acid Tank Area,Elevation 690 Auxiliary Bldg. ML20042F2531990-04-25025 April 1990 Instrument Accuracy Calculation 1LT-63-50,-51,-52 & -53 (RWST Switchover). ML20042F2551990-04-25025 April 1990 Instrument Accuracy Calculation 1LT-63-176,-177,-178 & -179 (RB Sump Switch). ML20043H0431990-04-11011 April 1990 Steel Containment Vessel - DBA Analysis Ccts Double Differentiation Question. ML20012C6291990-02-20020 February 1990 Rev 2 to TVA Calculation SQN-SQS2-0097, Probabilistic Analysis Showing Effects of Deleting RHR Autoclosure Interlock. ML20012A3031990-01-0303 January 1990 Foundation Investigation Evaluation of ERCW Roadway Access Cells a & B. ML20245J0781989-07-12012 July 1989 Rev 3 to Best Estimate Evaluation of Ice Condenser Basket Weights for Sequoyah Unit 1 Cycle 4, Supporting 890620 Application for Amend to License DPR-77,consisting of Tech Spec Change Request 89-24 ML20154P4121988-08-17017 August 1988 Rev 1 to Extension of Ice Condenser Weighing Period Based on Predicted Group - Row & Bay Sublimation Rates ML20151A2581988-07-0101 July 1988 Rev 0 to App R,Cable to Cable Shorts for RCS High/Low Pressure Interfaces ML20195D6671988-06-17017 June 1988 Nonproprietary App R Reactivity Calculations ML20235X3791987-09-16016 September 1987 Rev 1 to SQN-SQS4-0088, Justification for Continued Operation W/Unimplemented Corrective Actions for Moderate Energy Line Breaks ML20151M9601987-07-20020 July 1987 Package of NRC Administered Requalification Exam Results Summary ML20211A0821986-10-0303 October 1986 Package Consisting of Summary Schedule Suppl & Variance Rept & Capital Project Request Summary ML20203H2851986-07-28028 July 1986 Package of Documents Re Operating Experience W/Westinghouse PWR Steam Generators Through 820131 IA-86-445, Package of Documents Re Operating Experience W/Westinghouse PWR Steam Generators Through 8201311986-07-28028 July 1986 Package of Documents Re Operating Experience W/Westinghouse PWR Steam Generators Through 820131 ML20134L5811985-07-18018 July 1985 Package of Operator Exam Results Summary Sheets IA-85-442, Package of Operator Exam Results Summary Sheets1985-07-18018 July 1985 Package of Operator Exam Results Summary Sheets ML20129F4831985-05-0909 May 1985 Package of Compilations of Results of Operator Licensing & Requalification Exams ML20009A8271981-07-0808 July 1981 Viewgraphs Entitled TVA Inner Radius U-Bend Program, Presented at 810603 Meeting W/Nrc.Charts,Tables & Addl Info Encl ML19248D3401979-08-0202 August 1979 Const Deficiency Rept on 790802:chattering of Underfrequency Relay Contacts Caused Auxiliary Relay to Chatter,Delaying Reactor Trip & Cooling Pump Trip Signals.Relay & Design Changes Being Implemented ML19242D1601979-07-30030 July 1979 Possible RO on 790730 Re Failure to Seismically Qualify or Check Electrical Handholes in Conduit Between Auxiliary Bldg & Pump Station for Flow & Stress During Probable Max Flood ML19242D2311979-07-27027 July 1979 Notification of Potential Design requirement:3/4-inch Test Lines from 8-inch Low Head Safety Injection Headers Do Not Allow for Acceptable Piping Flexibility ML19247A9081979-07-17017 July 1979 Insp of Two Safety Injection Sys Accumulator Discharge Valves Revealed Severe Multiple Cracks in Stellite Facing. Notified Vendor,Velan Engineering Co.Possible Generic Implications to Unit 2 & Watts Bar 1998-07-17
[Table view] Category:OPERATIONS SUPPORT-CALCULATIONS
MONTHYEARML20116J5441996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J4971996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5021996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5051996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5091996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5151996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5171996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5221996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5251996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force (for Double Disc Split Wedge) ML20116J5361996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5391996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20116J5411996-08-0606 August 1996 Pressure Locking Evaluation for Required Pullout Force ML20065B7811993-06-18018 June 1993 Degraded Voltage Analysis ML20086H9851991-11-27027 November 1991 Evaluation of Block Clamps at Welds Near Valves 0-67-1514 & 2-67-1513 ML20028G8361990-08-21021 August 1990 Foundation Investigation of ERCW Pumping Station Foundation Cells. ML20029A0061990-08-0303 August 1990 Rev 0 to SQN-00-D052 EPM-AMJ-073190, Fire Hazard Analysis of Unit 2 App R Cables in Boric Acid Tank Area,Elevation 690 Auxiliary Bldg. ML20042F2531990-04-25025 April 1990 Instrument Accuracy Calculation 1LT-63-50,-51,-52 & -53 (RWST Switchover). ML20042F2551990-04-25025 April 1990 Instrument Accuracy Calculation 1LT-63-176,-177,-178 & -179 (RB Sump Switch). ML20043H0431990-04-11011 April 1990 Steel Containment Vessel - DBA Analysis Ccts Double Differentiation Question. ML20012C6291990-02-20020 February 1990 Rev 2 to TVA Calculation SQN-SQS2-0097, Probabilistic Analysis Showing Effects of Deleting RHR Autoclosure Interlock. ML20012A3031990-01-0303 January 1990 Foundation Investigation Evaluation of ERCW Roadway Access Cells a & B. ML20245J0781989-07-12012 July 1989 Rev 3 to Best Estimate Evaluation of Ice Condenser Basket Weights for Sequoyah Unit 1 Cycle 4, Supporting 890620 Application for Amend to License DPR-77,consisting of Tech Spec Change Request 89-24 ML20154P4121988-08-17017 August 1988 Rev 1 to Extension of Ice Condenser Weighing Period Based on Predicted Group - Row & Bay Sublimation Rates ML20151A2581988-07-0101 July 1988 Rev 0 to App R,Cable to Cable Shorts for RCS High/Low Pressure Interfaces ML20195D6671988-06-17017 June 1988 Nonproprietary App R Reactivity Calculations ML20235X3791987-09-16016 September 1987 Rev 1 to SQN-SQS4-0088, Justification for Continued Operation W/Unimplemented Corrective Actions for Moderate Energy Line Breaks 1996-08-06
[Table view] |
Text
. - .. _ . . .
- MdV Calc No. 1-FCV-63-26 (GL 89-10) PageIoF L PRESSURE LOCKING EVALUATION FOR REQUIRED PULLOUT FORCE (for Double Disc Solit Wedae)
'; gy =INP'UTS MOV !1.FCV-63 26 Valve type = lOD' Spilt Wedge VALVE DWG ; [93-12859[ EPRINP-6516 Calc Meth ARK nod 8B?
VALVE DESIGN DATA y :l= w 0.4l theta (A) =l: 0ldeg EPRI MOV PPP INTERNAL DEslGN INFO, Ref.
D1 E1 M1 l a= 1.8438 inches ro= 0.625 inches m2p.5[jj[2.'8752;l;.Jlg.25 l v= 0.3 a= ((D1 + E1)/ 2)/ 2 = 1,84375 b= 0.625 inches b= M1/ 2 = 0.625 = ro
! v= Poisson's Ratio = EWbj Mean Seat Dis (D1+E1)/2 = 3.6875 in l (D)
Stem Dia = emp 1.625 in l
'(d) u: seating surfaces friction coef Valve Seat Area ((D)^2*Pl/4= 10.68 (in)^2 based on Calc method. & EPRI results (S2)
(Vf) mu/(cosA + musinA) = 0.4000 theta = 1/2 total valve 2.07l(in)^2 disk angle (St3) Stem Area ((d)^2*Pl/4= l ;
Packing Load (Calculated) = 1625 lbs Valve Seat Area Based on l (PI)
(PI) Packing Load (Actual, average) = c0 Ibs Di. E1 l
PRESSURE and TEMPERATURE DATA Pbon = l;; 22735l psi (Pb) l 4
- g. a) P up = m 2600 psi l P down = v0 psi (Pd)
DP= l 2600lpsid j PRESSURE INDUCED, PRESSURE LOCKING THRUST REQUIREMENT:
THRUST = [ { (Pb - Pu) + (Pb - Pd) } * (S2} * (Vf} } - { (ST3) * (Pb) } + Pi ] + UNWEDGING WHERE: Pb = Pressure in valve Bonnet UNWEDGING = l' Oltbs Pu = Pressure upstream of Valve Pd = Pressure downstream of Valve S2 = Valve Seat Area Vf = Valve Friction Factor St3 = Stem Area Pl = Packing load (maximum value)
THRUST = 8213lbs PRESSURE INDUCED. P L - MAXIMUM BONNET PRESSURE @ ACTNALVE LIMITING CAP PRESSURE = { ANLIMTH + (S2
- Vf * (Pu + Pd)) - Pl } / { (2
PRESSURE = 4009 psi Rev. Prepared: Checked: [
9608130250 960806 r PDR ADOCK 05000327 P PDR
.i M V Calc No. 1-FCV-63-26 (GL 89-10) Page 1of 1
' PRNSSURE LOCKING REQUIREMENT = 8213 lbs ACTUATOR / VALVE CAPABILTTY EVALUAT10N CALCULATION: '1-FCV-63-26L Actuator Model F SMB-01 Motor Start Torque (MT) "i 515;ftibs Overall Gear Ratio (OGR)
- p B7.2 i Pullout Efficiency (PE) pfy fl40;%
Application Factor (AF) 0.9 or 1.0 gjhgij Valve Factor (VF) 1.0 or (VF/460)"2 j$p0.6428j 368.8VAC l
i Stem Factor (SF) EW D.0187) f Max Temperature (Temp) 215 F Loss Percentage (elevated temp) @@@% Note 1
- Torque Loss Factor = 1-Loss %*(Temp-104)/(356-77) 0.9149 1 Actuator Torque Capability = (MT
j hetuator Thrust Capability = Torque / Stem Factor 16453lbs' O.0187 1
Actuator Thrust / Torque Rating DISI53660'Ibs hSM 0}ftibs Valve Weak Link Thrust / Torque Rating ((@395"/0jlbs SF=
932.57 filbs 0.0187 i l
Seismic Thrust / Torque Rating Q Q $ _0jlbs SF= l 628.32 fttbs 0.0187 (
Note 1:
Reference:
Limitorque Technical Update 93-03 RESULTS: PRESSURE LOCKING REQUIREMENT = 8213 lbs !
ACTUATOR / VALVE LIMITING CAPABILITY = 16453lbs 1 cut = MOTOR CAP COMMENTS:
l Rev. Prepared: Checked: // g