ML20079H926

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Monthly Operating Rept for Dec 1983
ML20079H926
Person / Time
Site: Salem PSEG icon.png
Issue date: 12/31/1983
From: Miller L, Zupko J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
NUDOCS 8401240117
Download: ML20079H926 (23)


Text

.

AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-272 Unit Name Salem # 1 Date Jan. 10, 1984 Completed by L. K. Miller Telephone 609-935-6000 Extension 4455 Month December'1983 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 1106 16 1028 2 1111 17 1044 3 1109 18 884 4 1102 19 1096 5 1108 ._

20 1092 6 1089 21 1113 7 1110 22 1097 8 1107 23 1084 9 1104 24 1072 10 1105 25 1078 11 1107 26 821 12- 1107 27 1105

- 13 1065 28 1074 14 1109 29 1111 l-l 15 1109 30 139 l

31 0 i

'P. 8,1-7 R1 B401240117 831231 PDR ADOCK 0500027y R

Page 2 of 23 y -

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OPERATING DATA REPORT Docket No. 50-272 Date Jan. 10, 1984.

Telephone 935-6000 4455

_ Completed by_ L. K. Miller Extension

- Operating- Status

1. . Unit Name Salem No. 1 Notes
2. Reporting Period December 1983-
3. Licensed Thermal Power (MWt) 3336 4.- Nameplate Rating ^ (Gross MWe) 1135

'5. Design Electrical Rating (Net MWe) 1090

6. Maximum Dependable Capacity (Gross MWe)1124
7. Maximum Dependable Capacity ' (Net MWe) ID75 8.- If. Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
9. Power Level-te-Which Restricted, if any (Net MWe) N/A
10. Reasons for Restrictions, if any N/A This Month Year to Date Cumulative
11. Hours in Reporting Period 744 8760 57769 12.-No. of Hrs. Reactor was Critical. -716.6 5426.1 33141.2
13. Reactor Reserve Shutdown Hrs. 27.4 2060.8 3033.9
14. Hours Generator On-Line 707.5 5130 31777.9
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 2291066 16649180 95819371
17. Gross Elec. Energy Generated (MWH) 784020 5650250 31615100
18. Net Elec. Energy Generated (BGm) 752386 _

5376459 29971312

19. Unit Service Factor 95.1 58.6 55.0
20. Unit Availability-Factor 95.1 58.6 55.0
21. Unit Capacity Factor

. (using MDC Net) 93.7 56.9 48.1

22. Unit Capacity Factor (using DER Net) 92.8 56.3 47.6 23.' Unit Forced Outage Rate 4.9 34.5 29.1
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

Refueling 5-5-84

25. If shutdown at end of Report Period, Estimated Date of Startup:

N/A

26. Units in Test Status (Prior to Commercial Operation) :

Forecast Achieved Initial Criticality 9/30/76 12/11/76 Initial Electricity 11/1/76 12/25/76 Commercial Operation 12/20/76 6/30/77 8-1-7.R2 Page 3 of 23 i

UNIT SHUTDOWN AND POWER REDUCTIONS Dock 2t No. 50-272

. Unit Name Salem No.1 REPORT MONTH DECEMBER 1983 Date Jan. 10, 1984 L.K. Miller Telephone- 609-935-6000 Completed by Extension 4455 Method of Duration Shutting License Cause and Corrective Date Type Hours' Reason Down Event System Component Action to No.

1 2 Rea ctor Report Code 4 Code 5 Prevent Recurrence Condenser Tube and 5 HC HTEXCH Water Box Cleaning 11/30 B - 83-422 F 35.1 83-426 12/01 "

30.1 " HC 83-427 12/01 "

61.5 " HC 83-428 12/02 " 4.7 B Traveling Screens /

Trash Racks /

83-430 12/04 F 1.0 B 5 -

HF FILTER Canal Screens83-432 12/05 "

3.4 " " HF 83-434 12/05 F 3.1 B 5 HF

" B 83-435 12/05 47.0 5 -

Condenser Tube and

" " " " HC HTEXCH Waterbox Cleaning 83-436 12/06 4.7 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 1

A-Equipment Failure-explain 1-Manual Instructions Salem as F: Forced S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- Source C-Re fueling 3-Automatic Scram, tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

Page 4 of 23

UNIT SHUTDOWN AND POWER REDUCTIONS Docket No. 50-272 REPORT MONTH DECEMBER 1983 Unit Name Salem No.1 Date Jan. 10, 1984 Completed by. L.K. Miller Telephone 609-935-6000 Extension 4455 Method of Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to 1 2 Rea ctor Report Code 4 Code 5 Prevent Recurrence Condenser Tube and 5 HC HTEXCH Waterbox Cleaning 83-438 12/07 F 30.0 B -

Traveling Screens /

Trash Racks /.83-440 12/08 F 2.8 " " " HF FILTER Canal Screens Main Stop Valves83-442 12/08 F 2.0 " " "

HB VALVEX Turbine Traveling Screens /

Trash Racks /

83-444 12/08 "

7.7 " " " HF FILTER Canal Screens83-446 12/08 "

4.5 B 5 HF Condenser Tube and

" HC HTEXCH Water Box Cleaning 83-448 12/09 F 2.2 5 -

Traveling Screen /

Trash Racks83-450 12/09 "

6.6 B " "

HF FILTER Canal Screen 83-452 12/09 0.2 83-454 12/09 "

20.0 " HF FILTER Condenser Tube and

" 5 HC HTEXCH Water Box Cleaning 83-456 12/09 4.4 B 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 1-Manual Salem as F: Forced A-Equipment Failure-explain Instructions S: Scheduled B-Maintenance or Test 2-Manual Scr am. for Prepara- Source C-Re fueling 3-Automatic Scram, tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

Page 5 of 23

. UNIT SHUTDOWN.AND POWER REDUCTIONS . Docket No. 50-272 REPORT MONTH DECEMBER 1983 Unit'Name Salem No.1 Date Jan. 10, 1984 Completed by L.K. Miller Telephone 609-935-6000 Extension 4455 Method of 3 . Duration -Shutting License Cause and Corrective No. Date Type . Hours Reason Down Event System Component Action to.

1 2 Rea ctor Report Code 4- Code 5 Prevent Recurrence Traveling Screens /

Trash Racks /

i 83-458 12/11 F 4.4 B 5 -

HF FILTER Canal. Screens83-460 12/11 "

7.9 " " FILTER l 83-462 12/11 "

3.0 " HF FILTER Condenser Tube and HC HTEXCH Water Box Cleaning

83-464 12/12 1.5 83-466 12/12 F 3.3 B 5 -

HC-83-468 12/13 2.2 83-470 12/14 F 2.9 B 5 -

HC HTEXCH '83-472 12/14 12.2 4 83-474 12/14 5.1 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit-1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salem as S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- Source

' C-Refueling 3-Automatic Scram, tion of Data 1 D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Frevious Outage for Licensee F-Administrative 5-Load Reduction Event. Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

Page 6 of 23 ,

I a

~

UNIT SHUTDOWN AND POWER REDUCTIONS Dockat No. 50-272 REPORT MONTH DECEMBER 1983 Unit Nama Salen No.1 Jan. 10, 1984 j Date .

Completed by'LL.K. Miller Telephone 609-935-6000 Extension 4455 Method of

' License Cause and Corrective I Duration Shutting Action ~ to

? No. Date Type Hours Reason Down Event System Component 1 2 Reactor Report Code 4 Code 5 Prevent-Recurrence l'

Intercept Valves83-476 12/15 F L1.3 B 5' -- lH3 VALVEX Turbine Traveling Screens /

Trash Racks /

l 83-478 12/15 "

10.0 " " "

HF FILTER Canal Screens Screen Drive Sheer-83-480 12/15 "

0.6 A " " Pin-Broken j Condenser Tube and

" B " "

HC HTEXCH Waterbox Cleaning 83-482 12/15 4.5 Traveling Screens Trash Racks /.

i 83-484 12/16 F 7.5 B 5 - HF FILTER Canal Screens83-486 12/16 "

0.7 " " HF FILTER i

Nuclear Other Containment System 83-488 12/16 F 4.8 D 5 -

SA ZZZZZZ Problems83-492 12/16 3.2

. Traveling Screens / -

Trash Racks / ,83-494 12/17 "

6.2 B HF FILTER Canal Screens83-496 12/17 F 0.7 B 5 - HF FILTER 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salem as S: Scheduled B-Maintenance or Test 2-Manual Scram, for Prepara- Source C-Re fueling 3-Automatic Scram, tion of Data 2

D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage' for Licensee i F-Administrative 5-Load Reduction Event Report

G-Operational Error-explain 9-Other '(LER) File H-Other-explain (NUREG 0161) l Page 7 of 23

UNIT SHUTDOWN AND POWER REDUCTIONS' Dockst No. 50-272-REPORT. MONTH DECEMBER 1983 Unit N me ' Salem No.1 Date- Jan. 10,'1984 -

Completed byj

~

L.K. Miller TelephoneL609-935-6000 Extension 4455 Method of Duration . Shutting. . License. Cauce and' Corrective-Type Hours Reason Down Event System Component Action to No. Date

'l 2 Rea ctor Report Code 4 Code:S . Prevent / Recurrence' i Condenser Tube and B HC HTEXCH' Water Box Cleaning 12/17 83-498 'F 8.0 .5 Other Feedwater 5

HJ ZZZZZZ System Problems83-500 12/17 1.7

" " " " " ' ~"83-502 12/18 "

6.1 5 Traveling Screens /

-Trash Rack Canal

" B 5

" HF FILTER Screens83-504 12/18 1.7 Condenser Tube and

" " " HC HTEXCH Waterbox Cleaning 83-506 12/19 F 3.0 83-508 12/19 "

11.5 " HC 3 Method' 4 Exhibit /G 5, Exhibit 1-1 2 Reason F: Forced A-Equipment Failure-explain 1-Manual Instructions . Salem as B-Maintenance or. Test 2-Manual Scram. for Prepara- Source S: Scheduled C-Re fueling 3-Automatic Scram. tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report -

G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)-

Page 8 of 23

UNIT SHUTDOWN AND POWER REDUCTIONS Dockst No. 50-272-

-REPORT MONTH DECEMBER 1983 Unit Nnme Salen; No.1 Date Jan. 10,-1984

  • Completed by L.K. Miller Telephone 609-935-6000 Extension 4455 Method of

-Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to 1 ' 2 Reactor Report Code 4 Code 5 Prevent Recurrence Condenser Tube and B 5 HC HTEXCH Waterbox Cleaning 83-510 12/20 F 11.6 --- 83-512 12/20 2.9 83-514 12/21 3.6 Condenser Tube and 5 HC HTEXCH Waterbox Cleaning 83-516 12/21 F 3.3 B --- 83-518 12/22 3.1 83-520 12/22 2.5 83-522 12/23 2.3 83-524 12/24 F 4.9 B 5 --- HC HTEXCH Traveling Screens /

Trash Racks /

83-526 12/25 "

0.6 " " " HF FILTER Canal Screens Nuclear Other Containment 83-528 12/25 "

8.7 " " " SA ZZZZZZ System Problems 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salem as B-Maintenance or Test 2-Manual Scram. for Prepara- Source S: Scheduled C-Refueling 3-Automatic Scram. tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

Page 9 of 23

UNIT SHUTDOWN AND POWER REDUCTIONS Docket No. 50-272 REPORT MONTH DECEMBER 1983 Unit Name Salem No.1 Date Jan. 10, 1984 -

L.K. Miller Telephone 609-935-6000 Completed.by Extension 4455 Method of Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to ~

1 2 Reactor Report Code 4 Code 5 Prevent Recurrence Other Circulating B 5 HF- ZZZZZZ Water System Problem

,83-530 12/25 F 3.7 ---

Condenser Tube and l " " " "

HC 'HTEXCH Waterbox Cleaning 83-532 12/27 3.3 12/28 3.4 83-534 83-536 12/29 F 2.9 B 5 --- HC HTEXCH Circulating Water i 83-538 12/29 F 8.3 B 5 HF VALVEX Valves Traveling Screens /

Trash Racks /

j " " "

HF FILTER Canal Screens83-540 12/30 F 1.9 Intake System i Problems Other Than Traveling Screens j 83-542 12/30 "

0.6 " " " " ZZZZZZ Circ. Water 4

83-544 12/30 1.0 i " "83-546 12/30 F 7.4 B 5 --- HF ZZZZZZ i

' Nuclear Steam

! Generator Flanges /

A "

HI HTEXCH Manways/ Fittings

!83-548 12/30 F 33.2 1 Nuclear Other Steam

" " " " Generator Problems83-550 12/31 F 3.4 3

)

1 2 Reason 3 Method 4 Exhibit G S Exhibit 1 l Salem as F: Forced A-Equipment Failure-explain 1-Manual Instructions i Source S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- <

l j C-Re fueling 3-Automatic Scram. tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets

E-Operator Training & Licensing Exam Previous Outage for Licensee i F-Administrative 5-Load Reduction Event Report I G-Operational Error-explain 9-Other (LER) File '

H-Other-explain (NUREG 0161)

Page 10 of 23 i

MAJOR PLANT MODIFICATIONS Nm N-7tr2<

REPORT MONTE DECEMBER 1983 UNIT NAME: SALEM 1 DATE: JANUARY 10, 1984 COMPLETED BY : L. K. MILLER

-s TELEPHONE: (609) 339-4455 V

  • DCR NO. PRINCIPLE SYSTEM SUBJECT lEC-0724 Roadway Lighting Add roadway lighting in No. 1 Unit yard to provide proper illumination.

lEC-0918 Radiation Monitoring Add regulated air sample to fume System to Control exhaust and ventilation exhaust Facilities Building ducts.

lET-1165 #14 Fan Coil Motor Add temperature. connections to the

  1. 14 Fan Coil Motor housing access plate.

1SC-0033A Gas Turbine Provide pulse inputs into the GETAC system.

1SC-0151 Chilled Water Provide EAC air compressors cooling to Chilled Water System.

ISS-0012 Ventilation System Provide a supply and exhaust system for the north penetration area

,_s El. 100'.

f I

'v l

  • DESIGN CHANGE REOUEST Page 11 of 23 C-1-7.Rl J

MAJOR PLANT MODIFICATIONS DOCKET NO.: 50-272 REPORT MONTH DECEMBER 1983 UNIT NAME: Salem 1 DATE: January 10, 1984 COMPLETED BY: L.K. Miller TELEPHONE: 609/339-4455

  • DC R NO . SAFETY EVALUATION 10 CFR 50.59 1EC-0724 Installation of this DCR will not affect any safety function of the system. No unreviewed safety or environmental questions are involved.

1EC-0918 The monitors being added were not used in the calculations

'for any presently performed safety analysis. No i unreviewed safety or environmental questions are involved.

1ET-1165 The addition of thermometer connections to the fan coil motor housing does not affect the safe shutdown of the plant. No unreviewed safety or environmental questions are involved.

1SC-0033A The implementation of this DCR requires the penetration of existing fire barriers. However, instructions for resealing the penetrations to maintain the fire barrier rating are included. No unreviewed safety or environmental questions are involved.

ISC-0151 Implementation of this DCR will not create any new safety hazards, nor will it effect any presently performed safety analysis. No unreviewed safety or environmental questions are involved.

ISS-0012 Provision of cooling in the mechanical penetration area does not affect any presently performed safety analysis nor does it create any new safety hazards. No unreviewed safety or environmental questions are involved.

  • DCR - Design Change Request Page 12 of 23

PSE&G SALEM GENERATING S'D&ICN SAFE 71Y REIATED WORK TDER ILE

. 2 -

SAI2M UNIT 1 WO NO IDEPT . [ NIT EQUIPMENT InE#fIFICATIm -

P " IC RMS,1R41.APD 942706 l FAILURE DESCRIPPI N : CIIBCK PAPER DRIVE CPERATICN. 831110 FOUND BRNEN RACHET SPRING AND TAKE 1 UP M71TR BINDINGS. REPIACED SPRING, M7ICR AIO >

CNRECTIVE 7CTION:

l- s A TAKE-UP'REER GE' RS. IDERICATED GEAR BUSHING. 831110 934006' MD 1 12B FEEDWATER HEATER _

'FAIIDRE DESCRIPTICN: TEST FOR AbD REPAIR 'IUBE LEAKS. 830811 Cuntm'r1VE ICTION: FOUND 2 IEAES WITH VACULM AND 4 WI'IYI 1000 PSI HYDRO. PIDGGED 12 DDS. s, 934007 MD 12C EEEDWATER HEATER 1

FAILURE DESCRIPTICN: TEST EUR AbD REPAIR 'I1EE LEAKS. 830811.

CUKKtL'nVE ACTION: EDUND 2 LEAKS WITH VACUtM AND NWE WITH 1000 PSI HYDRO. PIDGGEED 4 DOS. 830814.

934029 MD 1 16 SW PUMP STRAINER FAIIDRE DESCRIPTIN: SHEAR PIN BR NEN. 830813 CUKtm riCN ACTION: REPIACE IDNER WEAR FIATE AND SIKES. INSTAT.Tm CLEAN STRAINERS. 830817.

934030 MD 1 AUX ED FMP RM.

COOLER FAILURE DESCRIPTICN: LEAK W U BEND ON SERVICE NATER SIDE OF COOLI?G COIL. 830815 i

i CORR _ N ACTION: CLEANED AND REPAIRED WITH BELZWA. 830815.

937853 CD 1 12 C m P COOLING FAILURE DESCRIPTICN: ROCM COOLER IS LEAKING BADLY. 830721.

a CORRECTIVE ACTION: REPAIRED 4 IEAKING ELBOWS USING COPPER BELZCNA. 830818.

Page 13 of 23 1

4 1

PSE&G SAIJ!M GENERMPING SDLTIN SAFETY REUm!D WOIE 3 DER IDG '

SAIJiM LNIT 1 WO NO Dwr WIT EQUIPBENP IDrurlFICJCIm 938916 CD- 1 -12,13, 14MS167 FAILURE DESCRIPTICN:. OIL NOP VISIBIE IN SIGfr GASS CN 12 AIO 13MS167. OIL IJ! VEL ABOUT 1/4 ING IN ~

14MS167. 830823.

COERECTIVE ACTIW: FTTIrn 12,13,14MS167 AIO GBCIGD 11MS167. 830823.

938918 OD -1 1A128VDC BATT. CHGR FAILURE DESCRIPTICN: BATTERY CHARGER FAILED DURING PIMOEGENCE & PI/S-DC1. 830824.

CORRBCTIVE ACTION: REPIACED DC BREAKER AIO PERF0EGED IDAD TEST. SAT. 830826.

938794 CD 1 PZR HTR BUS BKR.

FAIwRE DESCRIPTIW: BKR 1EP7X DEICH TRIPS FOR NO APPARENT REASON. 830821.

CCRRBCTIVE ACTION: FOUND BKR TO BE FAULTY. INSTALLED NEN BREAKER IN 1EP7X AIO AISO IN lEP13X MIICH WAS AISO TRIPPING. 830826. ,

938839 OD 1 12 BA TRANSFER PtNP FAIMRE DESCRIPTICN: PUMP BREAKER TRIPPED APIER CNLY A FEN MINU1ES T TERATION. 8a821.

r CORRBCPIVE ACTION: DISASSDBLED PUMP AND REPIACED SHAPT IMPFJIRR, BEARINGS AtO OIL SEALS. 830825.  ;

938433 OD 1 12 CC IMP BM 0001ER FAILURE DESCRIPTICN: COMER HAS SERVICE WATER IEAK T APPORX 1 GPM FRN AREA T COOLING COIIS.

830713.

CORRECTIVE ACPICN: TWO PINHOIE IEAKS REPAIRED WITH CTPER BELZONA. 830715.  !

938442 CD 1 AUX. BLDG. SUPPIX FAN FAILURE DESCRIPTIW: 1 RIPS CUT. 830715 I

CORRECTIVE ICTICN: NOTHING OCNCWSIVE E0GD DURING THXBLESH00T. INCREASED IING TIME TRIP W BKR TO 90 AMPS STARPED 6 TIMES WITHOUT TRIP. BKR TESTED FOR OVERIDAD. TEST IAN M30 [

830817. j I

Page 14 of 23 I

l  !

PSEEG SALEM GENEEUEING STATICN SAFETY RELATED WNK 3 DER IOG SAIJM UNIT 1 WO NO DEPT WIT EQUIPPENT liiknr1CATIW _

985770 CS 1 12SW20.

FAIIURE DESCRIPTIW: REPOlE AtO DISASSEMBLE VALVE EUR INSPECTICN T SHAPT BEARINGS. REPAIR AS MJUUlmv. 821101.

CORRECTIVE ACPIN: REMOVED, INSPBCTED AIO REPAIRED VALVE. 830816.

938991 CD 1 11 mTTJm WIR PWP FAILURE DESCRIPTICN: EUMP INBCRRD SEAL IS IEAKING EKGSSIVELY. 830819.

CcHxrLTIVE ACTION: REPLACED leCHANICAL~ SEAL, CUIBOARD OIL SEAL, CERAMIC DISC AND GASKETS. 830916.

939154 CD 1 16 SW PUMP STRAINER ~

1 FAILURE DESCRIPTION: STRAINER HAS BROKEN SHEAR PIN. 830914.

CORRECTIVE ACTION: CHANGED PIN AND REPIACED STRAINERS. CNE STRAINER WAS BROKEN Af0 JApeED. 830916.

938958 OD 1 11 CHAR 3ING PWP FAILURE DESCRIPTICE: SPEED INCREASER AIR BREATHER EIDD SPEWING OIL APO TEMPERATURE WAS ABOUT 50 DEGREES HIGHER THAN LAST WEEK. SUSPECP C,IL RESERVOIR WAS OVERFTTJm. 830815.

CORpwr'PIVE ACTICE: REPLACED GEAR BOX. 830818.

936789 OD 1 16SW24 STRNR BACKWASH FAILURE DESCRIPTICN: VALVE BIONING WATER. IOOKS LIKE BIODN DIAPHRAM. 830831.

CUMMia:nVE ACTION: INSTArJm NEW BODY AND DIAPHRAM. 830907.

938125 CD 1 15 CCNT FAN COIL UNIT FAILURE DESCRIPTICN: OUPLET SK LINE BEEORE 15SW223 HAS 1/4 INCH HOLE IN PIPE. 830728.

CCRRECTIVE ACTION: PAD WEIDED OUPSIDE A!O APPLIED BELZCNA TO INSIDE T PIPE. REMOVED TUBE BUtOLE FRm 15SW223 IAW DR 1083-2977. PERFORMED MP & DEID APO INSERVICE HYDRO. 803804.

Page 15 of 23

-. .. . ..~ . . . . . ~ _ . _ . - - _ _ . . - - - . _ . . . .. . .

s

]

P S F-& G SAIJ!M GBERATING SDLTIN.

SAFETY REIATED WORK WDER IlX3

' SALDI UNIT 1 WO E urir tmir rJguttetWP 1xmir1CATIN 933866 CD 1' CCNr AIR IOCK EL. 10G FAIw RE DESCRIFFI N: TEAR W IMER DOOR SEAL. 830812.

CCRRECTIVE )CTION: INSTAU E NEW DOOR SEAL. 830812.

933820- CD 1 13 GARGING IU1P

. FAILURE DESCRIPPIW: IEAK CN RMP SEALS HAS INCREASED 'IU 1.2 GPM and IS CAUSING HIGI AIRBORNE ACTIVITY l IN THE AREA.

I I COERECTIVE ACTIN: REPACKED 5 CYLIEERS W PlNP. 830901.

)

933805 CD 1 15 SW PUMP STRAINER i

FAIIERE DESCRIPTIW: STRAINER HAS BROKEN SHEAR PIN. 830806.

1 CWRECTIVE ACTION: REPLACED SHOES AhD SHEAR KEY. 830806.

I i 933797 OD 1 1A DIESEL GEN

.l t

i FAILURE DESCRIPfICN: 1A DIESEL GEN ALARM PANEL INER SECTIN INOPERABLE DUE 'IO BIDel EUSE MfIG WHEN I REPLACED, INSTANTLY BLEW NEW EUSE. 830804.

I CORRECTIVE ACTIN: REPIJCED LOWER PCMER SUPPLY FOR Al@KNCIAIOR WORKS SAT. 830805.

j i 931734 PD 1 SPARE SW PUMP l FAIIURE DESCRIPTIN: REBUIID SPARE RMP WIIG WAS REMOVED FROM #13 HOLE. PUMP HAD NO DISGARGE HEAD.

! 830707.  !

CORRECTIVE ACTICN: REBUILT PtNP. 830822.  ;

i j 924360 RE 1 INCORE FIUX MAP SYS i

l
FAIIURE DESCRIPTICN
CHAMEL "A" DRIVE 5 PMYi WILL Nor ROTATE.

CORRECTIVE ACTION: BROKE MOTOR FREE, TESTED SAT. 830804.

l i Page 16 of 23 i

PSE&G SAIBt GIBERATDG SD2Im SAFE 1Y REIATED WOIE WDER ILG SAIDt INIT 1

- WO ND Drrr WIT muunra a "wwnnCinICN 929974 IC 1 VALVE 11MS10 FAIIURE DESCRIPTIW: VALVE IEES 'IYROUGH. VALVE SIDNE WAS GBOED. 830726.-

CWRECTIVE ACTION: REPIJCED SEAT RING GASKET, BODY GASKET AND REPACIGD VALVE. 830809.

934090 10 1 15SW24 SCREEN WASH FAILURE DESCRIPTICN: VALVE LINING RIPPED. 830819.

CCRRBCTIVE ACTION: INSTALLED NEW VALVE BCDY. 830821.

936823 CD 1 12 CC ROOM CODIER FAILURE DESCRIPTIW: SERVICE WATER IEAK. 830903.

Cumex;nVE ACTION: REPAIRED IEAK WI'IH MNECUIAR BELZCNA AND CU90 U 'IUBES. 830904.

l 935597 OD 1 12 CC BOOM CODIER FAILURE DESCRIPTIW: SERVICE WATER IEAK IN ROOM COCER. 831018. l

! CCRRECTIVE ACTION: REPAIRED LEAK USING BELZWA C000CTIVE METAL. 83114. __

l 936890 CD 1 12 S/G EEED PtMP FAILURE DESCRIPTIW: SPEED DEMAND-SPEED MISMR'ICH. 830908.

VERIFIED FEED PUMP SHAPT SPEED. REPIACED N00DNARD SIGNAL CONERTED AIO CALIBRATED CNRECTIVE ACTION:

IAW DELAVAL INST. 83112.

936926 CD 1 PZR PRESS CQffROL FAILURE uthLauvriCN: 1 PSI DOES NOP RESPOPD 'IO PRESSURE CCN1 DOL IN ADIO BUT WILL CREN IN MANUAL.

831110.

CORRECTIVE ACTIN: ADJUSTED CCNIBOLLER BUT DOES NOP SEEM 'IO BE INfH3 RATING PRDPERLY. REPIJCED AUIO/"M3UAL STATICN AND CCNPRfYJFR GBCES SAT. 83115.

Page 17 of 23

P S E fr G SALEM GENERMPING STATIN SAFETY RELMPED WWtK GOER IOG SAIEM UNIT 1 WD NO Drrr WIT EQUIPBENT IDiNnrICATIN

991779 OD 1 22 S/G FEED P W P FAILURE DESCRIPTI N
PUMP INBOWD OIL SEAL STARTING 'IO ROCK IN.' 820601.

5 CORRECTIVE ACTION: REPIACED OIL SEAL. 830730.

937529 CD 1 11 SW PUMP SIRAINER FAILURE DESCRIPTIW: SHEAR KEY BROBEN. 830926.

l CORRECTIVE ACTION: REP 9CED IOWER SHOES MO SHEAR KEY. 830926.

I

937530 OD 1 CNT AIR IOCK
EL. 100 i

i FAIIURE DESCRIPTIW: FAILED LEAK RATE TEST. 830926.

CORRECTIVE ACTION: REPIACED BOIH SEAL CN OUTER DOOR. 830926.

937532 CD 1 1AMS10, A'IMOS RELIEF i FAILURE DESCRIPTIN: VALVE LEAKING 'IERWGH S'IR'EE VALVE. 830926.

i

!, CNRECTIVE ACTION: REPIACED REIAY IN POSITINER. REMOVED LIMIT SWTICHES FOR MAINT. 'IO REPACK VALVE.

STROKE VALVE AFTER MAINT. TEST SAT. 830929.

I 937712 W 1 C NP AIR LOCK i EL. 100 FAILURE DESCRIPTIW: Of1ER DOOR HAS EXCESSIVE SEAL IEAKAGE. 831003.

Cumerm'E ACTION: ADJUSTED DOOR SEALS. 831003.

s i 937728 OD 1 IMS132 VALVE TERATE 3

FAILURE DESCRIPTIW: VAINE WILL NOT CLOSE DUE TO TORN DIAIHRAM W VALVE WERA'IOR. 831005.

l

! CORRECTIVE ACTION: REPIACED VALVE ON DIAPHRAM. 831005.

Page 18 of 23

PSE&G SALEM GENERATING SDLTIN SAFE 1Y REIATED WORK WDER IOG SAI2M UNIT 1 WO NO DEPT LMIT EQUIP 9ENT IfnwnrICATIN 939139 OD 1 149W223 14 CECU J

FAIIERE DESCRIPTIm: SERVICE WATER IIAK AT FLAEE. 830912.

C@RECTIVE ACTION: REPIACED CAVITRG. 'IUBE BUNDLES. GD SPACER WAS ERCDED CAUSING FAINGE IEAK.

830921.

939170 m) 1 12 BAT PUMP FAILURE DESCRIPTIN: DISCHARGE FIDW REMAINS 2-3 GPM INER 'DRN MINIEN REQUIRED WITH DIFF. PRESS AT-MINIMtM LEVEL.

CORRECTIVE ACTIN: ADJUSTED IMPFFIER CIEARENCE 'ID .012. 830916.

i 939175 CD 1 12 BAT PUMP 4

FAILURE DESCRIPTIN: PUMP KEEPS TRIPPING OUT W OVERIDAD IN BOTH FAST AIO SION SPEED. 830916.

s CORRECTIVE ACTION: REBUILT PLNP. REPIACED OIL AND MBCHANICAL SEAL, O-RINGS AND BEARINGS. 830918.

939217 OD 1 DIESEL AIR STARP MER FAIIERE DESCRIPTIN: REPLACE BROKEN CmPWENT T DIESEL AIR SPARP EAST IBBE IfUBCIIR. 830914.

5 CmRECITVE ACTION: REPIACED WI'IH NEW IUBRICA'IDR. 830926.

! 939236 OD 1 1CV75 FAILURE DESCRIPTIN: VALVE HAS .4 GPM PACKING LEAK.

Cutoca nVE ACTION: FURMANITED USING T68 PROCEDURE. No i 934641 WRITTEN FOR PERMENANP REPAIR DURING OUTAGE. 830920.

I 940425 CD 1 CONT AIR IOCK I EL. 130 I

i FAILURE DESCRIPTIN: EX'IERIOR DOOR SEAL LEAKS. 831031.

i a

CORRECTIVE ACTION: REMOVED AND REIIETAT.TRn DOOR SEALS. 831031.

i Page 19 of 23 l

_ _ _ _ _ _ _ - _ _ _ _ _ = _ _ . .__

PSE&G SAIDI GENERATING SDLTIN SAFF1Y REIATED WORK WDER IOG SAIEM UNIT 1 WO NO Drrr NIT EQUIFiEif i*NnFICATIN

-943406 OD 1 IED CCNPROL SYS.

FAILURE DESCRIPTICN: WITH 1 DEG F DEVIATICN, RCDS SION A 72 SPM IED SPEED CUT IN NTIO. 831116.

CNRECTIVE ACTION: NO 15 VOLT CUITt7f Fim 1TM-412Q POWER SUPPLY. REPIACED QS in 1%4120. CAL SAT.

831116.

943467 CD 1 12 CC ROO4 00CLER FAILURE DESCRIPTIN: SERVICE WATER IRLK IN COOLER. 831116.

CuceL'nVE ACTION: CIEANED U-TUBE. PATOHED WITH M2EOULAR BELZCNA. 831117.

940631 CD 1 12SW129 CCNfROL FAILURE DESCRIPTIN: VALVE IS CPEN AT ALL TIMES AND SCLENOID VALVE VENT PORT IS CCNSDNFLY BICWING AIR. 831104.

CORRECTIVE ACTIN: REPIACED SOLENOID VALVE. 831114.

940692 CD 1 12 SW STRAINER FAILURE DESCRIPTICN: SHEAR PIN BRNEN. 831110.

CORRBCTIVE ACTICN: PIECE CF PEPAL JM91ED BE5 WEEN BOITE SHOES AbD PLATE. REPIACED BOP 10M SHOES AND SHEAR KEY. 831110.  !

940695 OD 1 CONT PRESS COGUIER FAILURE DESCRIPTICN: 03GUIER POINT SPIKING 70 .7 PSIG N ALARM TYPENRITE. 831110.

Cuc<rLr1VE JCIION: REPIACED IEAKING CAPACITCR C4 IN 1PM-948B ISOLATOR. ALSO REPIACED OED SITLE CAPACITORS C2, C3, C6, C7, C8, C9. 831114.

940702 CD 1 12SW24 OPERATOR 831111.

FAILURE DESCRIPTICN: VALVE NERATOR HAS AIR LEA 1'C FRQ4 (20ERSIDE N DIAPHRAM.

Cuws;r1VE ACTION: REPIACED ACIUATOR DIAPHRAM AND REBUILT ACIUNIOR. 831116.

l Page 20 of 23 l

PSE&G SALEM GENERATING SIKI'IN SAFETI REIATED NOR CEDER IOG SAIEM UNIT 1 WO NO Drzr INIT ECUIPMENT IDEknrICATI N 942732 IC 1 12 BCP SEAL OUTLET 831116.

' FAILURE DFSCRIPTIN: 'IDIPERATURE CHAMEL ETX10 OUT T CAL DURING GANNEL CAL.

CumrL~nVE ACTION: PEPIFm CAPACITORS C30 AND C31 IN ION-LEVEL AMPLIFIER 1D1-146. 831117.

943449 OD 1 12SW77 CHECK VALVE l

831119.

FAILURE DESCRIFFICN: GECK VALVE FAILED SPO 405V MO WAS EU.ND OPEN BY X-RAY.

CumtLnVE PCTION: REPLACES SPRING, PINS, IDG BEARINGS, Nt7FS MO SIUDS. FTTJFD ERCDED AREAS T BWY WTIII BELZONA CERAMIC R METAL. TEST SAT. 831127.

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1 Fage 21 of 23

SALEM UNIT 1 OPERATIONS

SUMMARY

REPORT DECEMBER 1983 Unit No. I began the month operating at full power, and with the exception of minor load reductions on December 1st, 17th, and 22nd, continued full power operation until December 25, 1983. On December 25th, buildup of ice in the circulating traveling screens forced a unit load reduction to approximately 50%. The icing conditions decreased with the rising tide, and Unit No. I was restored full power operation on December 26th. Full power operation of the unit continued until December 30th, when circulating water icing conditions again forced a reduction in load. Unit No. I was subsequently shutdown to perform repairs to No. 14 Steam Generator tube lane blocking device handhole cover which was leaking in the containment.

Repairs were satisfactorily completed and the unit was returned to service on January 1, 1984.

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Page 22 of 23

. . . .~ _ -- .. .. - _ _ - . . - . -

REFUELING INFORMATION .

DOCKET NO.: 50-272 COMPLETED BY: L.K.' Miller UNIT NAME: Salem 1 DATE: January 10, 1984

-> ' TELEPHONE: 609/935-6000 EXTENSION: 4455 Month' -December 1983

1. Refueling information has changed from last month:

YES X ,

NO

2. . Scheduled date for next refueling: May 31, 1984
3. Scheduled date for restart following refueling: September 4,1984
4. A) Will Technical Specification changes or other license  ;

amendments be required?

t YES NO NOT DETERMINED TO DATE 1/1/84 B) 'Has the reload fuel design been reviewed by the Station Operating Review Committee?

YES NO X If no, when is it scheduled? April 1984

5. Scheduled date (s) for submitting proposed licensing action:

April 1984 (if required) i

6. Important licensing considerations associated with refueling:

NONEL 1

7. Number of Fuel Assemb'.ies:

A) ,Incore 193 B) In Spent Fuel Storage 212 8.- Present licensed spent ftel storage capacity: 1170 Future spent fuel storage capacity: 1170  ;

9. Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity: September 1996 8-1-7.R4 Page 23 of 23

k O PSEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge. New Jersey 08038 Salem Generating Station January 10, 1984 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In Compliance with Section 6.9, Reporting Requirements for the Salem Technical Specifications, 10 copies of the following monthly operating reports for the month of December 1983 are being sent to you.

Average Daily Unit Power Level Operating Datu Report Unit Shutdowns and Power Reductions Major Plant Modification Summary of Safety Related Maintenance Operating Summary Refueling Information Sincerelyyours,7

[

J. M. Zupko, Jr.

General Manager - Salem Operations (h$LKM:sbh cc: Dr. Thomas E. Murley Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Director, Office of Management Information and Program Control U.S. Nuclear Regulatory Commission ff)Ly Washington, DC 20555 Enclosures l Page lof 23 8-1-7.R4 The Energy People am am n en