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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML20217C6191999-09-30030 September 1999 Application for Amend to License DPR-22,changing Tech Specs 3/4.17.B, Control Room Emergency Filtration Sys. Change Would Eliminate Unnecessary in-place Testing of HEPA & Activated Charcoal Filters Based on Sys Operating Time ML20203A3221999-01-28028 January 1999 Suppl 3 to 971125 LAR to License DPR-22 Re CST Low Level Hpci/Rcic Suction Transfer.Suppl Replaces TS Page 60d,to Include Approved Amend 103 Changes for Use by NRC in Issuing SER ML20206P1271998-12-31031 December 1998 LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4,deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR for SLCS ML20195C8911998-11-11011 November 1998 Supplemental Application for Amend to License DPR-22, Allowing Removal of One CST from Svc for Maint ML20154L9401998-10-12012 October 1998 Suppl 2 to LAR to License DPR-22,revising Statement on Normal Shift Length & Correcting Typos ML20154L8991998-10-0909 October 1998 Suppl 1 to LAR to License DPR-22,replacing Exhibits B & C of Original Submittal to Reflect Item 2 ML20153F0161998-09-25025 September 1998 Suppl 1 to LAR for Amend to License DPR-22, Replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Re Condensate Storage Tank Low Level Hpci/ RCIC Suction Transfer ML20249C5091998-06-19019 June 1998 Rev 2 to LAR Dtd 960726,requesting Changes to Ts,App a Sections 3.6.C & 3/4.17.B & Associated Bases.Proposed Changes Are to Establish TS Requirements That Are Consistent W/Analysis Inputs Used for Evaluation of MSLB Accident ML20216D2891998-03-25025 March 1998 Application for Amend to License DPR-22,providing Suppl 1 to 980313 Amend Request Re Plant Cycle 19 SLMCPR ML20216C9931998-03-19019 March 1998 Suppl Application for Amend to License DPR-22,requesting Consistent Wording Throughout TS & Providing Sound Basis for Frequency of Actions Required Each Shift ML20248L1951998-03-13013 March 1998 Application for Amend to License DPR-22,revising TS Re Safety Limit Minimum Critical Power Ratio ML20202H6861997-12-0404 December 1997 Rev 1 to Application for Amend to License DPR-22,increasing Plant Max Power Level from 1670 Mwt to 1775 Mwt ML20203A9531997-11-25025 November 1997 Application for Amend to License DPR-22,revising Tech Specs for Condensate Storage Tank Low Level Suction Transfer Setpoint for HPCI & RCIC Sys ML20210Q2881997-08-21021 August 1997 Suppl to 961125 Application for Amend to License DPR-22, Revising Page 6 of TS to Add Statement Re MCPR Values Applicable to Cycle 18 Only ML20141B9111997-06-19019 June 1997 Rev 2 to Application for Amend to License DPR-22,addressing Use of Containment Pressure for Assuring Adequate Net Positive Suction Head for ECCS Pumps Under worst-case Conditions ML20138F8661997-04-29029 April 1997 Application for Amend to License DPR-22,providing Suppl to 961125 Amend Request Re Safety Limit Minimum Critical Power Ratio ML20137W2141997-04-11011 April 1997 Rev 1 to Application for Amend to License DPR-22 Re Reactor Coolant Equivalent Radioiodine Concentration & Control Room Habitability ML20136B5361997-03-0404 March 1997 Application for Amend to License DPR-22,updating Design Basis Accident Containment Temp & Pressure Response ML20149M7221997-01-23023 January 1997 Application for Amend to License DPR-22,requesting Authorization for Changes to App A,Clarifying TS 3.5/4.5.C Re Min RHR & RHRSW Pump Requirements for Post Accident & Update of Design Basis Accident Containment & Temp Response ML20132C6361996-11-25025 November 1996 Application for Amend to License DPR-22,revising Section 2.1.A,SLMCPR Value & Deleting Sentence from Section 3.11.C of OLMCPR Re Limit Penalty for Single Recirculation Loop Operation ML20117A4281996-08-15015 August 1996 Application for Amend to License DPR-22,requesting Authorization for Changes to App a of Plant License as Shown on Attachments Labeled Exhibits A,B & C ML20116D8161996-07-26026 July 1996 Application for Amend to License DPR-22,changing TS Sections 3.6.C Re Coolant Chemistry & 3/4.17.B Re CR Emergency Filtration Sys ML20116G8911996-07-26026 July 1996 Application for Amend to License DPR-22,proposing Increase Max Reactor Core Power Level by 6.3% to 1,775 Mwt from Current 1,670 Mwt.Request Also Changes TSs Based on Power Rerate Evaluations ML20100Q3761996-03-0101 March 1996 Application for Amend to License DPR-22,removing Surveillance Requirement Re Periodic Replacement of Containment Purge & Vent Valve Seat Seal ML20095J4271995-12-21021 December 1995 Application for Amend to License DPR-22,revising Main Steam Isolation & App J Leak Rate Test Requirements ML20095E7021995-12-11011 December 1995 Application for Amend to License DPR-22,removing SR 4.7.D.4 from Plant TS & Replaces Seat Seals for Drywell & Suppression Chamber Purge & Vent Valves Every Five Yrs ML20094M1941995-11-14014 November 1995 Suppl to 950815 LAR to License DPR-22,incorporating Requirements of Option B,Section Iii.A for Type a Testing (Primary Containment ILRT) Per Reg Guide 1.163 ML20091K6731995-08-18018 August 1995 Rev 2 to 940608 LAR to License DPR-22,re Section 3.7/4.7, SGTS ML20087J4211995-08-15015 August 1995 LAR to License DPR-22,revising Max Individual MSIV Leak Rate Acceptance Criteria of 11.5 Scfh to Overall Criteria That Encompasses Four Main Steam Lines Into One Limit of 46 Scfh ML20086D7981995-07-0505 July 1995 LAR to License DPR-22,revising TS to Extend Surveillance Test Intervals & Allowable out-of-svc Times for Selected Instrumentation ML20085N0921995-06-22022 June 1995 Application for Amend to License DPR-22,revising TS to Support Implementation of BWR Thermal Hydraulic Stability Solution ML20082N8691995-04-20020 April 1995 Rev 1 to 940608 LAR to License DPR-22,deleting 18 Month Surveillance Frequency Re Automatic Initiation of Test Specified in SR 4.7.B.2.b(3) & Modifying LCO for Spec 3.7.C.4 Re Secondary Containment ML20069J1011994-06-0808 June 1994 LAR to License DPR-22,revising TS Section 3.7/4.7, SGTS Re SR to Operate SGTS Monthly as Well as Revising Performance Requirements for SGTS Filters & Process Stream Electric Heaters ML20065B6581994-03-28028 March 1994 Revised Application for Amend to License DPR-22, Incorporating Improvement in Wording Originally Submitted for TS Section 6.7, Reporting Requirements, Re Identification of Approved Analytical Methods for COLR ML20065B6851994-03-28028 March 1994 Application for Amend to License DPR-22,changing TS Tables 3.2.4 & 4.2.1 Re SGTS Initiation Instrumentation ML20063C9821994-01-26026 January 1994 Application for Amend to License DPR-22,requesting Changes to Ts,To Require Valves Be Tested at Pressure Greater than or Equal to Calculated Peak Containment Internal Pressure Re Design Basis LOCA ML20062N8691994-01-0404 January 1994 Application for Amend to License DPR-22,revising TS Section 3.11, Reactor Fuel Assemblies by Removing Info Re Average Planar Linear Heat Generation Rate & Min Critical Power Ratio.Proposed Rev to Page 1 of 8 from COLR Encl ML20059E6011994-01-0303 January 1994 Application for Amend to License DPR-22,changing TS Surveillance Requirement 4.6.E.1.a to Require Valves to Be Tested Per Section XI Inservice Testing Requirements of ASME Boiler & Pressure Vessel Code ML20058G4311993-11-30030 November 1993 Application for Amend to License DPR-22,removing Chlorine Detection Requirements & Changing Control Room Ventilation Sys Requirments ML20056E1061993-08-10010 August 1993 LAR to Provide Clarification of Sampling & Analysis Requirements,Update Liquid Effluent Sampling & Analysis Requirements & to Correct Typographical Errors in TS Section for License DPR-22 ML20045G6061993-07-0707 July 1993 Application for Amend to License DPR-22,revising Requirements for Monitoring RCS Leakage,Per NRC Guidance Provided in GL 88-01,Suppl 1 & NUREG-1433, BWR/4 Improved Sts. ML20128M7101993-02-12012 February 1993 Application for Amend to License DPR-22,changing Ts,To Increase Minimum Core Spray Pump Flow to More Conservatively Account for ECCS Bypass Leakage Paths ML1129708521982-07-0202 July 1982 to 760907 Application for Amend to License DPR-22,changing Tech Spec to Allow Plant to Remain at Substantial Power Level W/One Recirculation Pump in Operation & Equalizer Valve Closed ML1129708171981-03-19019 March 1981 Application for Amend to License DPR-22 Revising Tech Specs App a Re Reactor Protector Sys,Submitted as Revision 1 to 810206 Amend Request ML1129708131981-02-0606 February 1981 Application for Amend to Ol.Changes to Tech Specs Requested Per Encl Exhibits A,B,C & D ML20024G4151978-08-16016 August 1978 Application for Amend to License DPR-22,revising Tech Specs by Raising Permissible Setpoint of Eight Safety/Relief Valves Installed at Plant to 1,108 Psig ML20127H2001978-08-10010 August 1978 Application for Amend to License DPR-22 to Authorize Use of Partial Drilled Model for Plant ML20024G3731978-03-21021 March 1978 Application for Amend to License DPR-22,changing Tech Specs Re Partial Drilled Model for Analyzing Retrofit Fuel Design Scheduled for Fall 1978 Refueling Outage ML20024G3931978-03-20020 March 1978 Application for Amend to License DPR-22,clarifying Sections of Interim Radioactive Effluent Tech Specs ML20024G3991978-03-20020 March 1978 Suppl 1 to 770902 Application for Amend to License DPR-22, Changing Tech Specs to Permit Containment ILRT to Be Terminated in Less than 24 H 1999-09-30
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML20217C6191999-09-30030 September 1999 Application for Amend to License DPR-22,changing Tech Specs 3/4.17.B, Control Room Emergency Filtration Sys. Change Would Eliminate Unnecessary in-place Testing of HEPA & Activated Charcoal Filters Based on Sys Operating Time ML20203A3221999-01-28028 January 1999 Suppl 3 to 971125 LAR to License DPR-22 Re CST Low Level Hpci/Rcic Suction Transfer.Suppl Replaces TS Page 60d,to Include Approved Amend 103 Changes for Use by NRC in Issuing SER ML20206P1271998-12-31031 December 1998 LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4,deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR for SLCS ML20195C8911998-11-11011 November 1998 Supplemental Application for Amend to License DPR-22, Allowing Removal of One CST from Svc for Maint ML20154L9401998-10-12012 October 1998 Suppl 2 to LAR to License DPR-22,revising Statement on Normal Shift Length & Correcting Typos ML20154L8991998-10-0909 October 1998 Suppl 1 to LAR to License DPR-22,replacing Exhibits B & C of Original Submittal to Reflect Item 2 ML20153F0161998-09-25025 September 1998 Suppl 1 to LAR for Amend to License DPR-22, Replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Re Condensate Storage Tank Low Level Hpci/ RCIC Suction Transfer ML20249C5091998-06-19019 June 1998 Rev 2 to LAR Dtd 960726,requesting Changes to Ts,App a Sections 3.6.C & 3/4.17.B & Associated Bases.Proposed Changes Are to Establish TS Requirements That Are Consistent W/Analysis Inputs Used for Evaluation of MSLB Accident ML20216D2891998-03-25025 March 1998 Application for Amend to License DPR-22,providing Suppl 1 to 980313 Amend Request Re Plant Cycle 19 SLMCPR ML20216C9931998-03-19019 March 1998 Suppl Application for Amend to License DPR-22,requesting Consistent Wording Throughout TS & Providing Sound Basis for Frequency of Actions Required Each Shift ML20248L1951998-03-13013 March 1998 Application for Amend to License DPR-22,revising TS Re Safety Limit Minimum Critical Power Ratio ML20202H6861997-12-0404 December 1997 Rev 1 to Application for Amend to License DPR-22,increasing Plant Max Power Level from 1670 Mwt to 1775 Mwt ML20203A9531997-11-25025 November 1997 Application for Amend to License DPR-22,revising Tech Specs for Condensate Storage Tank Low Level Suction Transfer Setpoint for HPCI & RCIC Sys ML20210Q2881997-08-21021 August 1997 Suppl to 961125 Application for Amend to License DPR-22, Revising Page 6 of TS to Add Statement Re MCPR Values Applicable to Cycle 18 Only ML20141B9111997-06-19019 June 1997 Rev 2 to Application for Amend to License DPR-22,addressing Use of Containment Pressure for Assuring Adequate Net Positive Suction Head for ECCS Pumps Under worst-case Conditions ML20138F8661997-04-29029 April 1997 Application for Amend to License DPR-22,providing Suppl to 961125 Amend Request Re Safety Limit Minimum Critical Power Ratio ML20137W2141997-04-11011 April 1997 Rev 1 to Application for Amend to License DPR-22 Re Reactor Coolant Equivalent Radioiodine Concentration & Control Room Habitability ML20136B5361997-03-0404 March 1997 Application for Amend to License DPR-22,updating Design Basis Accident Containment Temp & Pressure Response ML20149M7221997-01-23023 January 1997 Application for Amend to License DPR-22,requesting Authorization for Changes to App A,Clarifying TS 3.5/4.5.C Re Min RHR & RHRSW Pump Requirements for Post Accident & Update of Design Basis Accident Containment & Temp Response ML20132C6361996-11-25025 November 1996 Application for Amend to License DPR-22,revising Section 2.1.A,SLMCPR Value & Deleting Sentence from Section 3.11.C of OLMCPR Re Limit Penalty for Single Recirculation Loop Operation ML20117A4281996-08-15015 August 1996 Application for Amend to License DPR-22,requesting Authorization for Changes to App a of Plant License as Shown on Attachments Labeled Exhibits A,B & C ML20116D8161996-07-26026 July 1996 Application for Amend to License DPR-22,changing TS Sections 3.6.C Re Coolant Chemistry & 3/4.17.B Re CR Emergency Filtration Sys ML20116G8911996-07-26026 July 1996 Application for Amend to License DPR-22,proposing Increase Max Reactor Core Power Level by 6.3% to 1,775 Mwt from Current 1,670 Mwt.Request Also Changes TSs Based on Power Rerate Evaluations ML20100Q3761996-03-0101 March 1996 Application for Amend to License DPR-22,removing Surveillance Requirement Re Periodic Replacement of Containment Purge & Vent Valve Seat Seal ML20095J4271995-12-21021 December 1995 Application for Amend to License DPR-22,revising Main Steam Isolation & App J Leak Rate Test Requirements ML20095E7021995-12-11011 December 1995 Application for Amend to License DPR-22,removing SR 4.7.D.4 from Plant TS & Replaces Seat Seals for Drywell & Suppression Chamber Purge & Vent Valves Every Five Yrs ML20094M1941995-11-14014 November 1995 Suppl to 950815 LAR to License DPR-22,incorporating Requirements of Option B,Section Iii.A for Type a Testing (Primary Containment ILRT) Per Reg Guide 1.163 ML20091K6731995-08-18018 August 1995 Rev 2 to 940608 LAR to License DPR-22,re Section 3.7/4.7, SGTS ML20087J4211995-08-15015 August 1995 LAR to License DPR-22,revising Max Individual MSIV Leak Rate Acceptance Criteria of 11.5 Scfh to Overall Criteria That Encompasses Four Main Steam Lines Into One Limit of 46 Scfh ML20086D7981995-07-0505 July 1995 LAR to License DPR-22,revising TS to Extend Surveillance Test Intervals & Allowable out-of-svc Times for Selected Instrumentation ML20085N0921995-06-22022 June 1995 Application for Amend to License DPR-22,revising TS to Support Implementation of BWR Thermal Hydraulic Stability Solution ML20082N8691995-04-20020 April 1995 Rev 1 to 940608 LAR to License DPR-22,deleting 18 Month Surveillance Frequency Re Automatic Initiation of Test Specified in SR 4.7.B.2.b(3) & Modifying LCO for Spec 3.7.C.4 Re Secondary Containment ML20069J1011994-06-0808 June 1994 LAR to License DPR-22,revising TS Section 3.7/4.7, SGTS Re SR to Operate SGTS Monthly as Well as Revising Performance Requirements for SGTS Filters & Process Stream Electric Heaters ML20065B6581994-03-28028 March 1994 Revised Application for Amend to License DPR-22, Incorporating Improvement in Wording Originally Submitted for TS Section 6.7, Reporting Requirements, Re Identification of Approved Analytical Methods for COLR ML20065B6851994-03-28028 March 1994 Application for Amend to License DPR-22,changing TS Tables 3.2.4 & 4.2.1 Re SGTS Initiation Instrumentation ML20063C9821994-01-26026 January 1994 Application for Amend to License DPR-22,requesting Changes to Ts,To Require Valves Be Tested at Pressure Greater than or Equal to Calculated Peak Containment Internal Pressure Re Design Basis LOCA ML20062N8691994-01-0404 January 1994 Application for Amend to License DPR-22,revising TS Section 3.11, Reactor Fuel Assemblies by Removing Info Re Average Planar Linear Heat Generation Rate & Min Critical Power Ratio.Proposed Rev to Page 1 of 8 from COLR Encl ML20059E6011994-01-0303 January 1994 Application for Amend to License DPR-22,changing TS Surveillance Requirement 4.6.E.1.a to Require Valves to Be Tested Per Section XI Inservice Testing Requirements of ASME Boiler & Pressure Vessel Code ML20058G4311993-11-30030 November 1993 Application for Amend to License DPR-22,removing Chlorine Detection Requirements & Changing Control Room Ventilation Sys Requirments ML20056E1061993-08-10010 August 1993 LAR to Provide Clarification of Sampling & Analysis Requirements,Update Liquid Effluent Sampling & Analysis Requirements & to Correct Typographical Errors in TS Section for License DPR-22 ML20045G6061993-07-0707 July 1993 Application for Amend to License DPR-22,revising Requirements for Monitoring RCS Leakage,Per NRC Guidance Provided in GL 88-01,Suppl 1 & NUREG-1433, BWR/4 Improved Sts. ML20128M7101993-02-12012 February 1993 Application for Amend to License DPR-22,changing Ts,To Increase Minimum Core Spray Pump Flow to More Conservatively Account for ECCS Bypass Leakage Paths ML1129708521982-07-0202 July 1982 to 760907 Application for Amend to License DPR-22,changing Tech Spec to Allow Plant to Remain at Substantial Power Level W/One Recirculation Pump in Operation & Equalizer Valve Closed ML1129708171981-03-19019 March 1981 Application for Amend to License DPR-22 Revising Tech Specs App a Re Reactor Protector Sys,Submitted as Revision 1 to 810206 Amend Request ML1129708131981-02-0606 February 1981 Application for Amend to Ol.Changes to Tech Specs Requested Per Encl Exhibits A,B,C & D ML20148N4531978-11-0606 November 1978 Amend 37 to Provisional Oper Lic DPR-22,changing Tech Spec to Improve Simmer Margin of Safety/Relief Valves ML20024G4151978-08-16016 August 1978 Application for Amend to License DPR-22,revising Tech Specs by Raising Permissible Setpoint of Eight Safety/Relief Valves Installed at Plant to 1,108 Psig ML20127H2001978-08-10010 August 1978 Application for Amend to License DPR-22 to Authorize Use of Partial Drilled Model for Plant ML20024G3731978-03-21021 March 1978 Application for Amend to License DPR-22,changing Tech Specs Re Partial Drilled Model for Analyzing Retrofit Fuel Design Scheduled for Fall 1978 Refueling Outage ML20024G3931978-03-20020 March 1978 Application for Amend to License DPR-22,clarifying Sections of Interim Radioactive Effluent Tech Specs 1999-09-30
[Table view] |
Text
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I UNITED STATES NUCLEAR REGULATORY COMMISSION i
NORTHERN STATES POWER COMPANY MONTICELLO NUCLEAR GENERATING PLANT DOCKET NO. 50-263 ;
REQUEST FOR AMENDMENT TO OPERATING LICENSE DPR-22 LICENSE AMENDMENT REQUEST DATED January 26, 1994 Northern States Power Company, a Minnesota corporation, requests authorization l' for changes to Appendix A of the Monticello Operating License as shown on the ,
attachments labeled Exhibits A, B, and C. Exhibit A describes
- he proposed . -t changes, describes the reasons for the changes, and contains a safety l Evaluation, a Determination of Significant Hazards Consideration and an-Environmental Assessment. Exhibit B contains current Technical Specification pages marked up with the proposed changes. Exhibit C is a copy of the Monticello Technical Specifications incorporating the proposed changes. j This letter contains no restricted or other defense information. l r
i NORTHE. TATES POWER CC ANY By # A4 Y k ,
[Directorger'O Anderson t Licensing & Management Issues on this day of af -
8
!IN ~before me a notary public in and '
for said County, ppfsonally appeared Roger O Anderson, Director, Licensing and '
Management Issues, and being first duly sworn acknowledged that he is authorized to execute this document on behalf of Northern States Power Company, that he knows the contents thereof, and that to the best of his knowledge, information, and belief the statements made in it are true and that it is not interposed for delay.
h
,i , a
.=====_
% JUDY L KULPPERtCK NOTARY PUBUC-WINNESOTA ANOKACOUNTY
)w My Commisabn Expres Sept 29.1997
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9402070272 940126 PDR ADDCK 05000263
.p PDR ,
q w . l Exhibit A l
MONTICELLO NUCLEAR GENERATING PLANT .
I License Amendment Request Dated January 31, 1994 i Evaluation of proposed changes to the Technical Specifications for Operating License DPR-22 Pursuant to 10 CFR Part 50, Section 50.59 and 50.90, the holders of Operating i License DPR-22 hereby propose the following changes to the Monticello ;
Technical Specifications: '
Proposed Chances: 'I i
10 CFR Part 50, Appendix J (Primary Reactor Containment Leakage Testing for Water Cooled Power Reactors) specifies the requirements for periodic primary containment leak rate testing. The leak rate testing program at Monticello substantially conforms to these regnairements, however, the design of the Monticello plant predates Appendix J. As discussed on page 184 of the '
Monticello Technical Specifications _(Section 4.7.A Bases),'the design of the !
plant.was reviewed to determine where compliance with Appendix J was ,
impossible or impractical. In each case where a departure.from-the !
- requirements of Appendix J was identified, a request for exemption from the requiresnents of Appendix J or a plant modification was proposed and submitted for NRC Staff review. Exemptions were proposed in'those cases.where compliance with Appendix J would have provided no meaningful' improvement in _
plant safety. In their review of Appendix J compliance, the NRC Staff' l approved a number of exemption requests, denied others, and provided necessary interpretation and clarification of the requirements of Appendix J. The i current Technical Specification surveillance requirements. reflect the results of this review. .
h one of the exemptions granted involved low pressure testing of the main steam ,
isolation valves. The four main steam lines which penetrate the primary containment each have two 18 inch diameter isolation valves installed in. ,
series (one inside and one outside of the drywell), for a total of eight main steam line isolation valves. Appendix J would normally require that such valves be subjected to a leakage test at a test pressure of P, the calculated peak containment internal pressure related to the design basis loss-of-coolant accident (for Monticello, . P. is calculated to be 42 psig) . However, Techni. cal. ,
Specifications 3.7.A.2.b.3 and 4.7.A.2.b.5 provide an exemption from chis requirement and specify a test pressure of greater than or equal to 25 peig for the main steam line isolation valves.
The original reason for this exemption, as. discussed in the NRC's Appendix J Safetv Evaluation Report for Monticello dated June 3, 1984, concerned the test-mett.e Jology used at the time. Leak rate testing of the main steam isolation' valves was performed by applying test pressure between the two isolation
- A-1 i
.q I
. i 4
,.. .- . _ _ _. - ~ ._
i t
- valves in a main steam line and measuring the total combined leakage past the two valves. The test method'eaused the test pressure to act.on the underside . 1 of the inboard valve disc from below the seat. Test pressures ~in excess of 25' psig tended to unseat the inboard valve, rendering the test meaningless. In addition, since it was not possible to allocate the portion of the total ,
leakage attributable to individual valves, it was conservatively assumed that ;
~
each valve-in the pair was leaking at the combined rate. This conservatism.
made it more difficult to meet the test acceptance criteria of II.5'SCFH per valve since it tended to overestimate the leak rate for individual valves, thus any added leakage induced by the test method could adversely bias the test results. '
i Since that time, the development of inflatable main. steam line plugs capable i of holding against a pressure in excess of P, has enabled us to develop and j implement improved test methodology whereby the full test pressure can be applied in the proper direction (above the disc) for all eight main steam ,
isolation valves. As an added benefit, we can now measure the leak rate for 'j each valve individually. As a result of these improvements, there is no l longer any need or justification for an exemption from the requirements of .
Appendix J to allow low pressure testing of the main steam isolation valves. .
In consideration of the above, we propose to amend Technical Specifications '}
4 3.7.A.2.b and 4.7.A.2.b, as well as the associated Bases for Section 3.7 and 4.7, to reflect the fact that the main steam isolation valves can now be j tested at a pressure.of greater than or equal to P, (42 psig). The. test !!
leakage acceptance criteria would be increased from 11.5 SCFH to 25.3 SCFH to .
reflect the higher test pressure. The. revised leakage criterion of 25.3 SCFH has been calculated using the methodology.of Appendix A to Technical !
Evaluation Report TER-C5257-30, " Containment Leakage' Testing - Northern States a Power Company, Monticello Nuclear Generating Plant", dated April 7, 1982.
This TER was used by the NRC as the bases for reviewing our current Appendix J program, and is referenced by the NRC in the June 3, 1984 Monticello Appendix ;
J Review Safety Evaluation Report and associated Appendix J Exemption Request
?
approval.
The change in test pressure and acceptance criteria differ from the equivalent ,l surveillance requirement of NUREG-1433, but this is because the NUREG assumes an exemption from Appendix J is needed to provide a practical alternative to ;
the Appendix J test criteria. This assumption is no longer true for j Monticello. The specific changes we are proposing are detailed in Exhibits'B and C.
1 Reason'for Chances:
]
l The proposed changes to the main steam isolation valve leak rate test pressure 1 and acceptance criteria are being submitted to eliminate an exemption to 10 CFR Part 50, Appendix J that is no longer technically necessary or'.
justifiable, thereby ensuring Appendix J requirements are met to the extent.
practical.
A-2 1
. ._. , _ . _ . . - _ . . . , __. - . _ , . . ~ . . ._ - _ i,...
.. . . ~ ~ . - ~
Safety Evaluation:
The Monticello primary containment system. consists of a drywell, which !
encloses the reactor. vessel and-recirculation pumpe, a pressure suppression )
chamber'which stores a large amount of water, a connecting vent system between j the drywell and the suppression chamber, and isolation valves. One of the .
functions of the primary containment system is to provide a barrier which, in j the event of a loss-of-cooling accident, controls the release of fission ~;
I products to the secondary containment. In order to. verify that the primary containment system is capable of fulfilling this function, periodic leak rate ;;
testing ~is performed using methodology that complies, to the extent practical, l with the requirements of 20 CFR Part 50, Appendix J. The design, function and f testing of the primary containment system is discussed in Section 5.2 of the Monticello Updated Safety Analysis Report.
The proposed amendment will have no adverse impact on the ability of the main l steam isolation valves to perform their intended safety function. The proposed test criteria will continue to provide a means to detect valve degradation and will not impact the validity of the. test results, since the test will simulate challenging the valves under worst case accident l conditions. Utilization of the higher test pressure P. (42 psig) would also 21 comply with 10 CFR Part 50, Appendix J requirements, l 1
Use of a higher allowable leakage (25.3 SCFH per valve) for a test conducted -l at P. (42 poig) is also appropriate, since this is equivalent to the previously specified leakage rate of 11.5 SCFH when tested at 25 psig. The methodology of Appendix A to TER-C5257-30, which was used to determine the new leakage criteria, was previously reviewed by the NRC and found to be j acceptable. The revised leak rate criteria will not result in higher main .I steam isolation valve leakage rates under actual service or. accident conditions. The proposed change will therefore have no impact on the plant's ability to meet Technical Specification 3.7.A.2.b.1, which requires that the Primary Containment overall integrated leakage rate be less than or equal to L., 1.2 percent by weight of the containment air per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at P., - 42 psig.
The proposed changes will have no impact on the function, operation, or reliability of the main steam isolation valves as described above or in the Monticello Updated Safety Analysis Report (USAR) or the Bases for the Technical Specifications, therefore the change will have no impact on any accident or transient analysis, nor will it increase the likelihood of an accident occurring. The proposed change will not result in any increase in post accident off-site or on-site radiation dose, since-the adjusted leakage limit is consistent with inputs previously established for the dose analyses.
Based on the above discussion, we conclude that the proposed change is technically acceptable and does not adversely impact public health or safety.
In addition, we conclude that thia amendment does not involve any significant increase in the types or amounts of effluents released from the site and therefore has no significant environmen*al impact.
i i
A-3 1
4 e
f f
- petermination of Sionificant Hazards' Consideration:
1This proposed change to the-Operating License has been evaluated to determine ~
if it constitutes a significant hazards consideration _as required by 10 CFR Part 50, Section 50.91 using the standards provided in Section 50.92. This !
analysis is provided below
- a. The proposed amendment will not involve a sionificant increase in the probability or consecuences of an accident previously ev31 pated.
The proposed amendment is limited to changes to the surveillance. testing requirements (test pressure and allowable leakage criteria) applicable to the main steam line isolation valves. The proposed criteria are {
equivalent to the current criteria with respect to monitoring main steam isolation valve performance to ensure that leakage past the valves would l be within acceptable limits under accident conditions. This !
surveillance test is performed while the plant is-in a cold shutdown i condition at a time when the main steam isolation valves are not {
required to be operable. Performance of the test itself is not an input- l or consideration in any accident previously evaluated, thus the proposed ,
change will not increase the probability of any such accident occurring. ;
The proposed amendment will not adversely affect the function, .i operation, or reliability of the valves, nor will it diminish the 'i capability of the valves to perform as required during an accident. i There will be no increase in post accident off-site or on-site radiation ;
dose, since the adjusted leakage limit is consistent with inputs .
I previously established.for the dose analyses. The proposed amendment 3.s '
consistent with regulatory requirements (10 CFR Part 50, Appendix J) and f guidance (TER-C5257-30) that has been previously reviewed by the NRC and' ]
found to be acceptable. Therefore, the amendment will not increase the consequences of any accident previously evaluated. _l t
- b. The proposed amendment will not create the possibility of a new or _
differe.nt kind of accident from any accident previously analyzed. :
~1 The proposed amendment does not involve any modification to plant i equipment or operating procedures, nor will it introduce any new main ;
steam isolation valve failure modes that have not been previously !
considered. The proposed amendment is limited to a change in the l surveillance test pressure & acceptance criteria used to leak test the i valves. This test is performed while the plant is in a cold shutdown l condition at a time when the valves are not required to be operable. We j therefore conclude the proposed changes will not create the possibility. -j of a new or different kind of accident from any accident previoasly 1 analyzed. )
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- c. The propoced amendment will not involve a sionificant reduction in the l maroin of safety.
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The proposed amendment will result in the. main steam isolation valves 'I being subjected to'the maximum pressure ( P,, 42 psig). calculated to occur under worst case accident conditions, and will therefore provide a i more realistic and challenging test of valve performance under those ~i conditions. The leakage rate criteria for the test has been adjusted upward to be commensurate with the higher test pressure, but this does not represent lany increase in actual leakage under accident conditions. l i
On-site and off-site dose analyses will not be affected. The proposed amendment does not involve any change in operability requirements or l limiting conditions for operation beyond the replacement of the old test :
pressure & acceptance criteria with equivalent criteria consistent with 10 CFR Part 50, Appendix J, NUREG-1433, and TER-C5257-30. Based on ;
these considerations, we conclude the proposed amendment will not l involve a significant reduction in the margin of safety >
A Based on the evaluation described above, and pursuant to 20 CFR Part 50,
- Section 50.91, Northern States Power Company han-determined that operation of the Monticello Nuclear Generating Plant in accordance with the proposed licence amendment request does not involve any sionificant hazards considerations as defined by NRC regulations in 10 CFR Part 50, Section 50.92. i Environmental Assessment: '
Northern States Power has evaluated the proposed changes and determined that ,
- 1. The changes do not involve a significant hazards consideration, <
- 2. The changes do not involve a significant change in the types or
~
significant increase in the amounts of any effluents that may be released offsite, or
- 3. The changes do not involve a significant increase in individual or.
cumulative occupational radiation exposure. ;
Accordingly, the proposed changen meet the eligibility criterion for _;
categorical exclusion set forth in 10 CFR Tart 51 Section 51.22(c)(9).
Therefore, pursuant to 10 CFR Part 51 Section 51.22(b), an environmental assessment of the proposed changes is not required.
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Exhibit B Monticello Nuclear Generating Plant ,
License Amendment Reaueet Dated January 26, 1994 l Technical Specification Pages Marked Up ,
with Proposed Wording Changes Exhibit B consists of the existing Technical Specification pages marked up.
with the proposed changes. Existing pages affected by this change are listed ;
below:
Pace ..
159 160 184 i
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