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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML20217C6191999-09-30030 September 1999 Application for Amend to License DPR-22,changing Tech Specs 3/4.17.B, Control Room Emergency Filtration Sys. Change Would Eliminate Unnecessary in-place Testing of HEPA & Activated Charcoal Filters Based on Sys Operating Time ML20203A3221999-01-28028 January 1999 Suppl 3 to 971125 LAR to License DPR-22 Re CST Low Level Hpci/Rcic Suction Transfer.Suppl Replaces TS Page 60d,to Include Approved Amend 103 Changes for Use by NRC in Issuing SER ML20206P1271998-12-31031 December 1998 LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4,deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR for SLCS ML20195C8911998-11-11011 November 1998 Supplemental Application for Amend to License DPR-22, Allowing Removal of One CST from Svc for Maint ML20154L9401998-10-12012 October 1998 Suppl 2 to LAR to License DPR-22,revising Statement on Normal Shift Length & Correcting Typos ML20154L8991998-10-0909 October 1998 Suppl 1 to LAR to License DPR-22,replacing Exhibits B & C of Original Submittal to Reflect Item 2 ML20153F0161998-09-25025 September 1998 Suppl 1 to LAR for Amend to License DPR-22, Replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Re Condensate Storage Tank Low Level Hpci/ RCIC Suction Transfer ML20249C5091998-06-19019 June 1998 Rev 2 to LAR Dtd 960726,requesting Changes to Ts,App a Sections 3.6.C & 3/4.17.B & Associated Bases.Proposed Changes Are to Establish TS Requirements That Are Consistent W/Analysis Inputs Used for Evaluation of MSLB Accident ML20216D2891998-03-25025 March 1998 Application for Amend to License DPR-22,providing Suppl 1 to 980313 Amend Request Re Plant Cycle 19 SLMCPR ML20216C9931998-03-19019 March 1998 Suppl Application for Amend to License DPR-22,requesting Consistent Wording Throughout TS & Providing Sound Basis for Frequency of Actions Required Each Shift ML20248L1951998-03-13013 March 1998 Application for Amend to License DPR-22,revising TS Re Safety Limit Minimum Critical Power Ratio ML20202H6861997-12-0404 December 1997 Rev 1 to Application for Amend to License DPR-22,increasing Plant Max Power Level from 1670 Mwt to 1775 Mwt ML20203A9531997-11-25025 November 1997 Application for Amend to License DPR-22,revising Tech Specs for Condensate Storage Tank Low Level Suction Transfer Setpoint for HPCI & RCIC Sys ML20210Q2881997-08-21021 August 1997 Suppl to 961125 Application for Amend to License DPR-22, Revising Page 6 of TS to Add Statement Re MCPR Values Applicable to Cycle 18 Only ML20141B9111997-06-19019 June 1997 Rev 2 to Application for Amend to License DPR-22,addressing Use of Containment Pressure for Assuring Adequate Net Positive Suction Head for ECCS Pumps Under worst-case Conditions ML20138F8661997-04-29029 April 1997 Application for Amend to License DPR-22,providing Suppl to 961125 Amend Request Re Safety Limit Minimum Critical Power Ratio ML20137W2141997-04-11011 April 1997 Rev 1 to Application for Amend to License DPR-22 Re Reactor Coolant Equivalent Radioiodine Concentration & Control Room Habitability ML20136B5361997-03-0404 March 1997 Application for Amend to License DPR-22,updating Design Basis Accident Containment Temp & Pressure Response ML20149M7221997-01-23023 January 1997 Application for Amend to License DPR-22,requesting Authorization for Changes to App A,Clarifying TS 3.5/4.5.C Re Min RHR & RHRSW Pump Requirements for Post Accident & Update of Design Basis Accident Containment & Temp Response ML20132C6361996-11-25025 November 1996 Application for Amend to License DPR-22,revising Section 2.1.A,SLMCPR Value & Deleting Sentence from Section 3.11.C of OLMCPR Re Limit Penalty for Single Recirculation Loop Operation ML20117A4281996-08-15015 August 1996 Application for Amend to License DPR-22,requesting Authorization for Changes to App a of Plant License as Shown on Attachments Labeled Exhibits A,B & C ML20116D8161996-07-26026 July 1996 Application for Amend to License DPR-22,changing TS Sections 3.6.C Re Coolant Chemistry & 3/4.17.B Re CR Emergency Filtration Sys ML20116G8911996-07-26026 July 1996 Application for Amend to License DPR-22,proposing Increase Max Reactor Core Power Level by 6.3% to 1,775 Mwt from Current 1,670 Mwt.Request Also Changes TSs Based on Power Rerate Evaluations ML20100Q3761996-03-0101 March 1996 Application for Amend to License DPR-22,removing Surveillance Requirement Re Periodic Replacement of Containment Purge & Vent Valve Seat Seal ML20095J4271995-12-21021 December 1995 Application for Amend to License DPR-22,revising Main Steam Isolation & App J Leak Rate Test Requirements ML20095E7021995-12-11011 December 1995 Application for Amend to License DPR-22,removing SR 4.7.D.4 from Plant TS & Replaces Seat Seals for Drywell & Suppression Chamber Purge & Vent Valves Every Five Yrs ML20094M1941995-11-14014 November 1995 Suppl to 950815 LAR to License DPR-22,incorporating Requirements of Option B,Section Iii.A for Type a Testing (Primary Containment ILRT) Per Reg Guide 1.163 ML20091K6731995-08-18018 August 1995 Rev 2 to 940608 LAR to License DPR-22,re Section 3.7/4.7, SGTS ML20087J4211995-08-15015 August 1995 LAR to License DPR-22,revising Max Individual MSIV Leak Rate Acceptance Criteria of 11.5 Scfh to Overall Criteria That Encompasses Four Main Steam Lines Into One Limit of 46 Scfh ML20086D7981995-07-0505 July 1995 LAR to License DPR-22,revising TS to Extend Surveillance Test Intervals & Allowable out-of-svc Times for Selected Instrumentation ML20085N0921995-06-22022 June 1995 Application for Amend to License DPR-22,revising TS to Support Implementation of BWR Thermal Hydraulic Stability Solution ML20082N8691995-04-20020 April 1995 Rev 1 to 940608 LAR to License DPR-22,deleting 18 Month Surveillance Frequency Re Automatic Initiation of Test Specified in SR 4.7.B.2.b(3) & Modifying LCO for Spec 3.7.C.4 Re Secondary Containment ML20069J1011994-06-0808 June 1994 LAR to License DPR-22,revising TS Section 3.7/4.7, SGTS Re SR to Operate SGTS Monthly as Well as Revising Performance Requirements for SGTS Filters & Process Stream Electric Heaters ML20065B6581994-03-28028 March 1994 Revised Application for Amend to License DPR-22, Incorporating Improvement in Wording Originally Submitted for TS Section 6.7, Reporting Requirements, Re Identification of Approved Analytical Methods for COLR ML20065B6851994-03-28028 March 1994 Application for Amend to License DPR-22,changing TS Tables 3.2.4 & 4.2.1 Re SGTS Initiation Instrumentation ML20063C9821994-01-26026 January 1994 Application for Amend to License DPR-22,requesting Changes to Ts,To Require Valves Be Tested at Pressure Greater than or Equal to Calculated Peak Containment Internal Pressure Re Design Basis LOCA ML20062N8691994-01-0404 January 1994 Application for Amend to License DPR-22,revising TS Section 3.11, Reactor Fuel Assemblies by Removing Info Re Average Planar Linear Heat Generation Rate & Min Critical Power Ratio.Proposed Rev to Page 1 of 8 from COLR Encl ML20059E6011994-01-0303 January 1994 Application for Amend to License DPR-22,changing TS Surveillance Requirement 4.6.E.1.a to Require Valves to Be Tested Per Section XI Inservice Testing Requirements of ASME Boiler & Pressure Vessel Code ML20058G4311993-11-30030 November 1993 Application for Amend to License DPR-22,removing Chlorine Detection Requirements & Changing Control Room Ventilation Sys Requirments ML20056E1061993-08-10010 August 1993 LAR to Provide Clarification of Sampling & Analysis Requirements,Update Liquid Effluent Sampling & Analysis Requirements & to Correct Typographical Errors in TS Section for License DPR-22 ML20045G6061993-07-0707 July 1993 Application for Amend to License DPR-22,revising Requirements for Monitoring RCS Leakage,Per NRC Guidance Provided in GL 88-01,Suppl 1 & NUREG-1433, BWR/4 Improved Sts ML20128M7101993-02-12012 February 1993 Application for Amend to License DPR-22,changing Ts,To Increase Minimum Core Spray Pump Flow to More Conservatively Account for ECCS Bypass Leakage Paths ML1129708521982-07-0202 July 1982 to 760907 Application for Amend to License DPR-22,changing Tech Spec to Allow Plant to Remain at Substantial Power Level W/One Recirculation Pump in Operation & Equalizer Valve Closed ML1129708171981-03-19019 March 1981 Application for Amend to License DPR-22 Revising Tech Specs App a Re Reactor Protector Sys,Submitted as Revision 1 to 810206 Amend Request ML1129708131981-02-0606 February 1981 Application for Amend to Ol.Changes to Tech Specs Requested Per Encl Exhibits A,B,C & D ML20024G4151978-08-16016 August 1978 Application for Amend to License DPR-22,revising Tech Specs by Raising Permissible Setpoint of Eight Safety/Relief Valves Installed at Plant to 1,108 Psig ML20127H2001978-08-10010 August 1978 Application for Amend to License DPR-22 to Authorize Use of Partial Drilled Model for Plant ML20024G3731978-03-21021 March 1978 Application for Amend to License DPR-22,changing Tech Specs Re Partial Drilled Model for Analyzing Retrofit Fuel Design Scheduled for Fall 1978 Refueling Outage ML20024G3931978-03-20020 March 1978 Application for Amend to License DPR-22,clarifying Sections of Interim Radioactive Effluent Tech Specs ML20024G3991978-03-20020 March 1978 Suppl 1 to 770902 Application for Amend to License DPR-22, Changing Tech Specs to Permit Containment ILRT to Be Terminated in Less than 24 H 1999-09-30
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML20217H1841999-10-12012 October 1999 Amend 106 to License DPR-22 Revising TS Reactor Pressure Vessel P-T Limit Curves,Deleting Completed RPV Sample SRs & Deleting Requirement to Withdraw Specimen at Next Refueling Outage ML20217C6191999-09-30030 September 1999 Application for Amend to License DPR-22,changing Tech Specs 3/4.17.B, Control Room Emergency Filtration Sys. Change Would Eliminate Unnecessary in-place Testing of HEPA & Activated Charcoal Filters Based on Sys Operating Time ML20205C1451999-03-19019 March 1999 Amend 105 to License DPR-22,revising TSs for CST Low Level Suction Transfer Setpoint for HPCI & RCIC Sys to Allow Removing 1 CST from Svc for Maint ML20203A3221999-01-28028 January 1999 Suppl 3 to 971125 LAR to License DPR-22 Re CST Low Level Hpci/Rcic Suction Transfer.Suppl Replaces TS Page 60d,to Include Approved Amend 103 Changes for Use by NRC in Issuing SER ML20202H6421999-01-22022 January 1999 Errata to Amends 103 & 104 to License DPR-22.Typographical Errors Made to TS Pages ML20206P1271998-12-31031 December 1998 LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4,deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR for SLCS ML20198M8021998-12-24024 December 1998 Amend 104 to License DPR-22,revising TS So That Either 8 or 12 H Shifts Considered Normal & 40 H Considered Nominal Week & Changing Wording for Surveillances Required Once Per Shift to Once Per 12 H ML20198M3621998-12-23023 December 1998 Amend 103 to License DPR-22,extending STIs & Allowable out- of-service Times for Instrumentation in Eccs,Rod Block, Isolation Group 4,Isolation Group 5,RB Ventilation & Standby Gas Treatment,Rpt & ARI & Scs Isolation Sys ML20195C8911998-11-11011 November 1998 Supplemental Application for Amend to License DPR-22, Allowing Removal of One CST from Svc for Maint ML20154L9401998-10-12012 October 1998 Suppl 2 to LAR to License DPR-22,revising Statement on Normal Shift Length & Correcting Typos ML20154L8991998-10-0909 October 1998 Suppl 1 to LAR to License DPR-22,replacing Exhibits B & C of Original Submittal to Reflect Item 2 ML20153F0161998-09-25025 September 1998 Suppl 1 to LAR for Amend to License DPR-22, Replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Re Condensate Storage Tank Low Level Hpci/ RCIC Suction Transfer ML20151T0931998-08-28028 August 1998 Amend 101 to License DPR-22,consisting of Changes to TS in Response to Revised Application & Suppl & Adding Two License Conditions to App C of License ML20249C5091998-06-19019 June 1998 Rev 2 to LAR Dtd 960726,requesting Changes to Ts,App a Sections 3.6.C & 3/4.17.B & Associated Bases.Proposed Changes Are to Establish TS Requirements That Are Consistent W/Analysis Inputs Used for Evaluation of MSLB Accident ML20217E9351998-04-20020 April 1998 Amend 100 to License DPR-22,revising MCPR Safety Limits for Operating Cycle 19 Based on Cycle Specific Analysis of Current Mixed Core of General Electric (GE) 10,11,four GE12 Lead Use Assemblies & Eight ATRIUM-9B Fuel Parameters ML20216D2891998-03-25025 March 1998 Application for Amend to License DPR-22,providing Suppl 1 to 980313 Amend Request Re Plant Cycle 19 SLMCPR ML20216C9931998-03-19019 March 1998 Suppl Application for Amend to License DPR-22,requesting Consistent Wording Throughout TS & Providing Sound Basis for Frequency of Actions Required Each Shift ML20248L1951998-03-13013 March 1998 Application for Amend to License DPR-22,revising TS Re Safety Limit Minimum Critical Power Ratio ML20202H6861997-12-0404 December 1997 Rev 1 to Application for Amend to License DPR-22,increasing Plant Max Power Level from 1670 Mwt to 1775 Mwt ML20203A9531997-11-25025 November 1997 Application for Amend to License DPR-22,revising Tech Specs for Condensate Storage Tank Low Level Suction Transfer Setpoint for HPCI & RCIC Sys ML20210Q2881997-08-21021 August 1997 Suppl to 961125 Application for Amend to License DPR-22, Revising Page 6 of TS to Add Statement Re MCPR Values Applicable to Cycle 18 Only ML20151M0141997-07-25025 July 1997 Amend 98 to License DPR-22,authorizing Licensee to Change TS Bases & USAR to Reflect Reliance on Containment Pressure to Compensate for Potential Deficiency in NPSH for ECCS Pumps Following DBA ML20141B9111997-06-19019 June 1997 Rev 2 to Application for Amend to License DPR-22,addressing Use of Containment Pressure for Assuring Adequate Net Positive Suction Head for ECCS Pumps Under worst-case Conditions ML20138F8661997-04-29029 April 1997 Application for Amend to License DPR-22,providing Suppl to 961125 Amend Request Re Safety Limit Minimum Critical Power Ratio ML20137W2141997-04-11011 April 1997 Rev 1 to Application for Amend to License DPR-22 Re Reactor Coolant Equivalent Radioiodine Concentration & Control Room Habitability ML20136B5361997-03-0404 March 1997 Application for Amend to License DPR-22,updating Design Basis Accident Containment Temp & Pressure Response ML20149M7221997-01-23023 January 1997 Application for Amend to License DPR-22,requesting Authorization for Changes to App A,Clarifying TS 3.5/4.5.C Re Min RHR & RHRSW Pump Requirements for Post Accident & Update of Design Basis Accident Containment & Temp Response ML20132C6361996-11-25025 November 1996 Application for Amend to License DPR-22,revising Section 2.1.A,SLMCPR Value & Deleting Sentence from Section 3.11.C of OLMCPR Re Limit Penalty for Single Recirculation Loop Operation ML20117A4281996-08-15015 August 1996 Application for Amend to License DPR-22,requesting Authorization for Changes to App a of Plant License as Shown on Attachments Labeled Exhibits A,B & C ML20116G8911996-07-26026 July 1996 Application for Amend to License DPR-22,proposing Increase Max Reactor Core Power Level by 6.3% to 1,775 Mwt from Current 1,670 Mwt.Request Also Changes TSs Based on Power Rerate Evaluations ML20116D8161996-07-26026 July 1996 Application for Amend to License DPR-22,changing TS Sections 3.6.C Re Coolant Chemistry & 3/4.17.B Re CR Emergency Filtration Sys ML20101Q1141996-04-0909 April 1996 Amend 96 to License DPR-22,modifying TS Section 4.7,SR for Primary Containment Automatic Isolation Valves ML20101N1601996-04-0303 April 1996 Amend 95 to License DPR-22 Modifying TS to Revise Main Sliv Leak Rate Test Acceptance Criterion,Operability Test Interval for Drywell Spray Header & Nozzles from 5 to 10 Yrs & TS 3/4.7.a.2 ML20100Q3761996-03-0101 March 1996 Application for Amend to License DPR-22,removing Surveillance Requirement Re Periodic Replacement of Containment Purge & Vent Valve Seat Seal ML20095J4271995-12-21021 December 1995 Application for Amend to License DPR-22,revising Main Steam Isolation & App J Leak Rate Test Requirements ML20095E7021995-12-11011 December 1995 Application for Amend to License DPR-22,removing SR 4.7.D.4 from Plant TS & Replaces Seat Seals for Drywell & Suppression Chamber Purge & Vent Valves Every Five Yrs ML20094M1941995-11-14014 November 1995 Suppl to 950815 LAR to License DPR-22,incorporating Requirements of Option B,Section Iii.A for Type a Testing (Primary Containment ILRT) Per Reg Guide 1.163 ML20093F0341995-10-0202 October 1995 Amend 94 to License DPR-22,revising Tech Specs 3.7/4.7 Which Pertain to SGTS & Secondary Containment ML20091K6731995-08-18018 August 1995 Rev 2 to 940608 LAR to License DPR-22,re Section 3.7/4.7, SGTS ML20087J4211995-08-15015 August 1995 LAR to License DPR-22,revising Max Individual MSIV Leak Rate Acceptance Criteria of 11.5 Scfh to Overall Criteria That Encompasses Four Main Steam Lines Into One Limit of 46 Scfh ML20086J8101995-07-12012 July 1995 Amend 93 to License DPR-22,increasing Min Core Spray Pump Flow to More Conservatively Account for ECCS Bypass Leakage Sections of Ts.Changes to TS Encl ML20086D7981995-07-0505 July 1995 LAR to License DPR-22,revising TS to Extend Surveillance Test Intervals & Allowable out-of-svc Times for Selected Instrumentation ML20085N0921995-06-22022 June 1995 Application for Amend to License DPR-22,revising TS to Support Implementation of BWR Thermal Hydraulic Stability Solution ML20082N8691995-04-20020 April 1995 Rev 1 to 940608 LAR to License DPR-22,deleting 18 Month Surveillance Frequency Re Automatic Initiation of Test Specified in SR 4.7.B.2.b(3) & Modifying LCO for Spec 3.7.C.4 Re Secondary Containment ML20072U0691994-09-0909 September 1994 Amend 91 to License DPR-22 Changing TS Tables 3.2.4 & 4.2.1 Such That Initiating Parameter for Secondary Containment Isolation & Standby Treatment Sys Would Be Revised from Low Reactor Water Level to low-low Reactor Water Level ML20072S6751994-09-0707 September 1994 Amend 90 to License DPR-22,involving Several Improvements to Radiological Effluents Portion of Plant TSs ML20072K5201994-08-25025 August 1994 Amend 89 to License DPR-22,deletes Requirement for Cl Detection Sys from Following Portions of Ts:Section 3.2.I, 3/4.17.A,Tables 3.2.9 & 4.2.1 & Bases 3.2 & 3.17.A ML20071F4451994-06-30030 June 1994 Amend 88 to License DPR-22,modifying Section 3.11,Reactor Fuel Assemblies,By Removal of Info Re Analytical Method to Determine APLHGR & Adding Ref to COLR ML20069J1011994-06-0808 June 1994 LAR to License DPR-22,revising TS Section 3.7/4.7, SGTS Re SR to Operate SGTS Monthly as Well as Revising Performance Requirements for SGTS Filters & Process Stream Electric Heaters ML20065L4331994-04-15015 April 1994 Amend 87 to License DPR-22 Re Changes to TS 3.6.D, Primary Sys Boundary Coolant Leakage, & Corresponding Surveillance Requirements 1999-09-30
[Table view] |
Text
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- UNITED STATES NUCLEAR REGULATORY COMMISSION
^
i NORTHERN STATES POWER COMPANY MONTICELLO NUCLEAR GENERATING PLANT DOCKET NO. 50-263.
REQUEST FOR AMENDMENT TO OPERATING LICENSE DPR-22 LICENSE AMENDMENT REQUEST DATED July 7.1993 Northern States Power Company, a Minnesota corporation, requests authorization l
for changes to Appendix A of the Monticello operating License as shown on the attachments labeled Exhibits A, B, and C.
Exhibit A describes.the proposed changes, describes the reasons for the changes, and contains a Safety Evaluation, a Determination of Significant Hazards Consideration and an Environmental Assessment.
Exhibit B contains current Technical Specification pages marked up with the proposed changes.. Exhibit C is a copy of the Monticello Technical Specifications incorporating the proposed changes.
This letter contains no restricted or other defense information.
k NORTHE STATES POWER C PANY By '
_d foger O Ariderson Director
-Licensing and Management Issues
[
On this M day o M79.8 before me a notary public in and for said County, pdsongfly appeare'd ' Roger 0 Anderson, Director Licensing and Management Issues, and being first duly sworn acknowledged that he is authorized to execute this document on behalf of Northern States Power Company, that he knows the contents thereof, and that to the best of his knowledge, information, and belief the statements made in it are true and that it is not interposed for delay.
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MONTICELID NUCLEAR GENERATING PLANT License Amendment Request Dated July 7,1993 i
Evaluation of Proposed Changes to the Technical Specifications for Operating License DPR-22 Pursuant to 10 CFR Part 50, Sections 50.59 and 50.90, the holders of' Operating i
License DPR-22 hereby propose the following changes to the Monticello Technical Specifications:
t Par.e Section Current Specification 126 3.6.D.5 At least one of the leakage measurement instruments associated with each sump shall be operable and the drywell particulate radioactivity monitoring system shall be operable or a sample of the containment atmosphere shall be.
taken and analyzed at least every four hours. Otherwise, initiate an orderly shutdown of the reactor and reduce reactor water temperature to less than 212'F within'24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
.fronosed Channe 3.6.D.5 Any time irradiated fuel is in the reactor vessel and reactor water temperature is above 212*F, at least one of the leakage measurement instruments associated with each sump shall be operable.
If no leak rate measurement instruments associated with a sump are operable, then:
a.
Perform manual leak rate measurements once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and restore a measurement instrument to operable status within 30 days.
b.
Otherwise, initiate an orderly shutdown of the reactor and reduce reactor water temperature to less than 212'F within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
3.6.u.6 Any time irradiated fuel is in the reactor vessel and reactor water temperature is above 212 F, the drywell-particulate radioactivity monitoring system shall'be operable.
If the drywell particulate radioactivity monitoring system is not operable, then; a.
Analyze grab samples of the primary containment atmosphere once per-12 hours.
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Otherwise, initiate an orderly shutdown of the reactor and reduce reactor water temperature to less than 212 F within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Reason for Proposed Change Staff position number three of Generic Letter 88-01, Supplement 1 provides for an alternative means to quantitatively measure reactor coolant system leakage via manually pumping the sump or measuring differences in sump level for a period of 30 days while restoring the drain sump monitoring system. The alternative staff position is-reflected in the revised wording of Limiting Condition for-Operation requirement 3.6.D.5.a.
The proposed' change reduces the burden placed on plant operations personnel to record indications of potential. coolant oystem leakage and reduces the potential for unnecessary plant shutdowns by allowing manual determination of coolant system leakage-consistent with NRC Staff positions stated in Generic' Letter i
88-01, Supplement 1.
Requirement 3.6.D.6 incorporates Limiting Conditions for Operation for the drywell particulate radioactivity.
monitoring system which were previously contained.in-requirement 3.6.D.S.
' Requirement 3.6 D.6-revises the grab sample analyses frequency to once every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> during drywe11' radioactive particulate monitor inoperability-to be consistent with standard technical specification i
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requirements contained in NUREG-1433, BWR/4 Improved Standard Tech Specs.
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Eggg Section Current Specification 126 4.6.D.1 Any time irradiated fuel is in the reactor vessel and coolant temperature is above 212 F, the following.
surveillance program shall be carried out:
a.
Unidentified and Identified Leakage rates shall be recorded at least once every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> using primary containment floor and equipment drain sump monitoring equipment, b.
Primary containment atmospheric particulate radioactivity shall be recorded at least once every 4
- hours, c.
Drywell pressure and temperature shall be recorded at least once every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Proposed Change Any time irradiated fuel is in the reactor vessel and coolant temperature is above 212*F, the following-surveillance program shall be carried out:
a.
Unidentified and Identified Leakage rates shall be recorded once per shift:not to exceed 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> using-primary containment floor and equipment drain sump monitoring equipment.
Reason for Proposed Change Staff position number one of Generic Letter 88-01, Supplement 1, endorses a frequency of once per shift not to-exceed 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> for monitoring reactor coolant system leakage. The revised frequency for Surveillance Requirement 4.6.D.1.a and the deletion of requirements 4.6.D.l.b and 4.6.D.l.c reduces the burden placed on plant operations personnel to record indications of potential coolant system leakage consistent with NRC staff guidance provided in Generic Letter 88-01, Supplement 1, and NUREG-1433, BWR/4 Improved Standard Tech Specs.
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n Current Specification 126 4.6 D.2 b.
Primary. containment sump leakage measurement system -
3' performance of a sensor check at least once per 4
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hours and a channel calibration test at least once per cycle.
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Proposed Channe j
b.
Primary containment sump leakage measurement system -
performance of a sensor check at least once per shift not to exceed 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and a channel calibration. test at least once per cycle.
Reasens for Proposed Chance i
Surveillance requirement 4.6.D.2.b has been revised,to
-J require a sump _ leakage measurement system sensor check to be performed once per shift not to exceed twelve hours..
The e
proposed change reduces the burden placed on plant operations personnel to record indications of potential coolant system leakage consistent with NRC staff guidance provided in NUREG-1433, BWR/4 Improved Standard Tech Specs.
Safety Evaluation:
r Requirements governing reactor coolant system leakage detection were added to t
the plant Technical Specifications on December 10, 1982 via License Amendment
[
14 and 17.
License Amendment 14 was issued as part of the corrective actions and justification for returning the Monticello Nuclear Plant to' power
,l following a Confirmatory Action Letter issued by.the Commission on October'19,
- i 1982.
The October 19, 1982 Confirmatory Action Letter was issued regarding proposed corrective actions.for crack indications found in welds on the
+
Monticello Nuclear Plant recirculation system.
Since that time, the Monticello Nuclear Plant has either replaced piping susceptible to Intergranular Stress Corrosion Cracking (ICSCC) in the recirculation system, the residual heat removal system, and the core spray system with materials resistant to ICSCC, or protected the piping with a cladding of resistant veld metal. To further reduce susceptibility to IGSCC, a Hydrogen Water Chemistry System was placed in operation in 1988. As a result of these modifications, the potential for IGSCC ( and therefore the safety: significance of the leak detection system) has been greatly reduced.
In 1988, the Nuclear Regulatory Commission issued Generic Letter 88-01, "NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping." This Generic t
Letter provided revised Staff Positions to minimize and control intergranular stress corrosion cracking (IGSCC) in BWR piping systems made of austenitic-stainless steel.that is four inches or larger in nominal diameter and contains reactor coolant at a temperature.above 2000F.
Generic Letter 88-01 required confirmation that plant Technical Specifications related to leakage detection s
A-4 a
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would conform to the staff position on leak detection included in the Generic Letter.
In our response to Generic Letter 88-31 dated July 28, 1988, we confirmed that our plant Technical Specifications conformed to the NRC staff position on leak detection as incorporated via License Amendments 14 and 17 to the Monticello Operating License. This License Amendment Request does not change the reactor coolant system leakage limits specified in Generic Letter 88-01.
Subsequent to the above correspondence, the NRC has issued Supplement 1 to Generic Letter 88-01 and NUREG-1433, BWR/4 Improved Standard Tech Specs.
In these documents the NRC has provided revised guidance for monitoring reactor coolant system leakage which ensures means are available for detecting reactor coolant system leakage while reducing unnecessary hardship on plant operators and the potential for undesirable plant transients due to unnecessary plant shutdowns.
This License Amendment Request incorporates the applicable revised guidance.
The revised Limiting Conditions for Operation requirements for inoperability of a sump leak rate measurement instrument and the drywell particulate radioactivity monitoring system are acceptable based on the multiple forms of leakage detection that are still available.
Determination of the coolant system leakage during periods when the sump leakage rate measurement instrument is inoperable, can be accomplished by manually pumping the sump or by observation of the sump level change, using indications that are readily available to the operating staff. These instruments have an accuracy which is suitable for detecting changes in reactor coolant system leakage consistent with specified leakage limits. The 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> interval for manual leak rate determination or grab sample analysis provides periodic information that is adequate to detect leakage. The 30 day completion time for restoration of the sump leakage measurement instrument or the drywell particulate radioactivity monitoring system recognizes that at least one other form of leakage detection is available.
The level of safety provided to the public is maintained with extension of the i
frequency for recording the coolant system leakage rates and performance of sump leakage measurement system sensor check to once per shift not to exceed 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, and deletion of the surveillance requirement to record drywell particulate radioactivity and drywell pressure and temperature.
Alarms are provided to alert the operator to conditions indicative of a potential coolant system leak via the drywell particulate radioactivity monitoring system as well as alarms to notify the operator of conditions approaching the Technical Specification leakage limits. The drywell particulate radioactivity and drywell pressure and temperature indications provide corroboration of the primary indication of potential breaches in reactor coolant system integrity, the sump leakage measurement instruments. The established operating limits for reactor coolant system leakage as monitored by the sump leakage measurement instruments are well below the rates predicted for critical crack growth and instability.
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Determination of Sinnificant Hazards Consideration:
The proposed changes to the Operating License have been evaluated to determine whether they constitute a significant hazards consideration as required by 10 CFR Part 50, Section 50.91 using the standards provided in Section 50.92.
This analysis is provided below:
1.
The proposed amendment will not involve a sirnificant increase in the probability or conseauences of an accident oreviousiv evaluated.
The proposed changes incorporate the guidance of Generic Letter 88-01, Supplement 1, and.NUREG-1433, BWR/4 Improved Standard Tech Specs, into the Technical Specifications governing reactor coolant system leakage monitoring.
Piping susceptible to Intergranular Stress Corrosion Cracking (IGSCC) in the recirculation system, the residual heat removal system, and the core spray system has been replaced with material resistant to ICSCC, or protected with a cladding or resistant weld metal.
To further reduce susceptibility to IGSCC, a Hydrogen Water Chemistry System was placed in operation in 1988. The above actions taken to minimize the potential for crack initiation in conjunction with the leakage rates allowed by the Technical Specifications and the multiple leakage indication systems available, maintains a high level'of confidence in the ability to monitor reactor coolant system integrity, thus the proposed changes will not significantly affect the probability or consequences of an accident previously evaluated.
2.
The proposed amendment will not create the possibility of a new or different kind of accident from any accident previousiv analyzed.
There are no new failure modes or mechanisms associated with the proposed changes. The proposed changes do not involve.any equipment modifications or changes in operational limits. Only the means and frequency for confirming compliance with the limits are affected. The operating limits are established well below the rates predicted for critical crack growth and instability.
Indications remain available to the operators to provide an early warning of a significant reactor coolant pressure boundary leak.
It is therefore concluded that the proposed changes do not create the possibility of a new or different kind of accident from any previously evaluated, and the accident analyses presented in the Updated Safety Analysis Report will remain bounding.
3.
The proposed amendment will not involve a significant reduction in the c
margin of safety.
The proposed changes do not involve any modification in operational limits. Alarm functions to alert the operator of reactor coolant system leakage, and operator monitoring of key parameters is maintained at a level to assure early detection of any significant leakage.
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therefore concluded that the proposed changes will not result in any.
reduction in the plant's margin of safety,
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Based on the analysis'above, and: pursuant to 10 CFR Part.50, Section 50,59, Northern States Power _ company has determined that operation of the Monticello
- Nuclear Generating Plant in accordance with the proposed license amendment request does not involve any significant hazards considerations.as defined by:
NRC regulation in 10 CFR Part 50, Section 50.92, Environmental Assessment Northern States Power has evaluated the proposed changes'and determined that:
1.
The change does not involve a significant hazards consideration.
f.
2 The changes do not involve a significant change in the type or significant increase in the amounts of any effluent that may be released offsite, or 3.
The changes do not involve a significant increase in individual or cumulative occupational radiation exposure.
Accordingly, the proposed changes met the eligibility criterion-for categorical exclusion set forth in 10 CFR-Part 51, Section'51.22(b), an environmental. assessment of the proposed changes is not required.
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