ML20054C547

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IE Insp Rept 50-334/82-01 on 820104-0216.Noncompliance Noted:Failure to Post Fire Watches for Nonfunctional Penetration & Administer Document Maint.Portions Withheld (Ref 10CFR73.21)
ML20054C547
Person / Time
Site: Beaver Valley
Issue date: 03/18/1982
From: Beckman D, Greenman E, Lazarus W, Reynolds S, Troskoski W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20054C544 List:
References
50-334-82-01, 50-334-82-1, NUDOCS 8204210307
Download: ML20054C547 (54)


See also: IR 05000334/1982001

Text

THE INFORMATION ON THIS PAGE IS

DCS Nos. 50-334 820114

820102

DEEMED TO BE APPROPRIATE FOR PUBLIC

'

820114

320106

DISCLOSURE PURSUANT TO 10 CFR 73.21.

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1

U.S. NUCLEAR REGULATORY COMMISSION

or' v,E OF INSPECTION AND ENFORCEMENT

Region I

Report No.

50-334/82-01

Docket No.

50-334

License No.

DPR-66

Priority

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Category

C

Licensee:

Duquesne Light Company

435 Sixth Avenue

The report details contain

Safeguards Info

Pittsburgh, Pennsylvania

(Pages 49-51)

Facility Name: Beaver Valley Power Station, Unit 1

Inspection at: Shippingport, Pennsylvania

Inspection cond c d: J uary 4 - February 16, 1982

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Inspectors:

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D AnB kmal, Senior Res' dent Inspector

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W. M.sTroskoski, Resident) Inspector

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W.'Jr1.azarus Reactor Inspector

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S. D. R ynolds, Rejetor Inspector

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Approved by:

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jvE. G. Greenman, Chief, Reactor Projects

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Section No. 2A, Projects Branch No. 2

Inspection Summary:

Inspection on January 4-February 16,1982 (Report No. 50-334/82-01).

Areas Inspected: Routine inspections by the resident inspectors (191 hours0.00221 days <br />0.0531 hours <br />3.158069e-4 weeks <br />7.26755e-5 months <br />) and two

region-based inspectors (26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />) of licensee action on previous inspection findings,

followup on NRC Performance Appraisal Section findings, plant operations, housekeeping,

fire protection, radiological controls, :,urveillance testing, maintenance, physical secur-

ity, radwaste system operation, in-office review of licensee event reports, onsite event

followup, refueling preparations, IE Bulletin followup, TMI lessons learned followup,

EPP drill observations, potential design deficiency review, piping NDE review,, and ar

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Results:

Violations:

None in seventeen areas.

Seven in two areas (Failure to

post fire watches for nonfunctional penetration, paragraph 3.e(3); Failure to

administer / document maintenance training, paragraph 2.b; ORC failed to review

violations required by TS, paragraph 2.b; Failure to establish and execute inspection

program for operating activities, paragraph 2.b; Failure to document bases for

10CFR50.59(b) safety evaluations, paragraph 2.b; QA Audit deficiencies, para

and, Inadequate ORC / Management Audit and ORC Training Audit, paragraph 2.b.) graph

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DETAILS

1.

Persons Contacted

D. Beron, Warehouse Supervisor, Stores Dept.

F. Bissert, Manager, Nuclear Support Services

J. Carey, Vice President, Nuclear Division

K. Grada, Superintendent of Licensing and Compliance

R. Hansen, Maintenance Supervisor

H. Harper, Security Assistant

T. Jones, Manager, Nuclear Operations

J. Kosmal, Radcon Supervisor

W. Lacey, Chief Engineer

V. Linnenbom, Radiochemist

J. Lukehart, Security Director

J. McGee, Director, Administrative Services

L. Schad, Operations Supervisor

J. Sieber, Manager, Nuclear Safety and Licensing

J. Vassello, Training Supervisor

H. Williams, Station Superintendent

J. Wenkous, Reactor Control Chemist

The inspectors also contacted other licensee employees and contractors

during this inspection.

2.

Licensee Action on Previously Identifiet Inspection Findings

a.

The NRC Outstanding Items (01) List was reviewed with responsible

licensee personnel.

Items selected by the inspectors were sub-

sequently reviewed through discussions with licensee personnel,

documentation review, and field inspection to determine whether

licensee actions specified in the OIs had been satisfactorily

completed. The overall status of previously identified inspection

findings was reviewed, and planned and completed licensee actions

were discussed for those items not reported below.

(Closed) Unresolved Item (79-12-02): Type C penetration ncn-

conscrvative test results.

In several Type C tests performed

using OST 1.47.4, Containment Isolation Valve Leakage Test, Type

C, the licensee recorded the leakage as zero, which is non-

conservative in that: 1) the rotameters used to measure leakage

are only accurate above a given minimum sensitivity, and 2)

the accuracy of leakage measurement using the " downstream

method" is not assured because no verification is done for leak

tightness of downstream boundries. The licensee comited to

revising the procedure to specify the use of the tests minimum

sensitivity when appropriate and to specify that additional veri-

fications be made when using the " downstream method."

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The inspector reviewed OST 1.47.4, Containment Isolation Valve

Leakage Test, Type C, Revision 39. This procedure includes a

note requiring that, if no indication of flow can be obtained

using the most sensitive rotameter then the minimum sensitivity

for the flow leakage shall be assigned as 0.01 SCFH, which

corresponds to the minimum sensitivity for the most accurate

rotameter used. Another note also specified that the make-up

air test method is to be used instead of the downstream method

for verifying test boundry leakage. The downstream method was

outlined and available for trouble-shooting only. The inspector

had no further questions at this time.

(Closed) UnresolvedItem(79-12-04): Type B containment leakage

test - nonconservative results. MSP 47.01, Type B Containment

Leakage Test - Electrical Penetrations, was detemined to be

inaccurate when computing leak rate by the Pressure Decay Method

in that temperature variations over the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> test period were

not measured nor compensated for in the calculations.

In addition,

pressure gauges used in the test were not calibrated. The inspector

reviewed Revision 2 to MSP 47.01 and determined that the use of

both calibrated test gauges and thermometers were specified for

conducting the test. The inspector also verified that the tempera-

ture compensation was included in leak rate calculations. The

inspector had no further questions on this item.

(Closed) Unresolved'cem(79-12-06): Airlock door bypass leakage.

During performance of the last containment integrated leak rate

test (CILRT), the airlock innet door equalizing solenoid valves

leaked by even though they had satisfactorily passed their local

leak rate test (LLRT).

In order to maintain containment integrity,

a manual isolation valve in the line 1-VS-153 must be kept closed.

The licensee comited to include this valve in the Type C LLRT

program and to incorporate checks of this valve position into a

periodic containment integrity verification.

The inspector reviewed surveillance test OST 1.47.1, Containment

Air Lock Test, Revision 22, perfomed on a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> basis to verify

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that detectable seal leakage is within containment integrity limits.

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To limit any leakage from the inner door equalizing solenoids, the

OST requires valve 1-VS-153 to be closed.

The inspector also re-

viewed surveillance test OST 1.47.30, Personnel Air Lock Isolation

Valve (1VS-153)TypeCLeakTest, Revision 42,andverifiedvalve

testing per the licensee's Type C leak rate test program. The

inspector had no further questions on this item.

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(Closed) UnresolvedItem(79-12-07):

Electrical penetration

surveillance.

During a field inspection of electrical penetra-

tions, the inspector noted that all pressure indicating gauges

were isolated and not indicating the status of the penetration

canisters o r 0-ring seals. When several of the isolation valves

were opened, two were found to be at zero pressure and two others

at 15 psig. Although these canisters are nomally pressurized

at or above 45 psig, no routine surveillance was performed to

verify proper pressurization. The licensee had commited to

issuing a routine surveillance to monitor the pressure.

TheinspectorreviewedMaintenanceSurveillanceProcedure(MSP)

47.01, Type B Containment Leakage Test - Electrical Penetrations,

Revision 2.

The MSP provides detection of local leakage from the

containment electrical penetrations by periodically testing their

pressure integrity and comparing test data to the overall contain-

ment integrated leakage rate acceptance criteria specified in

TS 4.6.1.2, Containment Leakage - Surveillance Requirements.

The MSP is perfomed during each refueling outage to meet the

requirement of 10CFR50, Appendix 1, Primary Reactor Containment

Leakage Testing for Water-Cooled Power Reactors. The inspector

had no further questions on this item.

(Closed) Unresolved Item (79-22-01): Licensee to evaluate cali-

bration program for MCB PR-NI. During a review of the Main Control

ector noted that the MCB

Board (MCB) instrumentation,theinsp(NI)meterswerereadingup

power range (PR) nuclear instrument

to 6% full power greater than the NI rack indicators. This

difference is attributed to the MCB indicators being driven by an

isolation amplifier that was not routinely recalibrated during

daily NI calorimetric calibrations. Calorimetric calibrations

result in adjustment of the circuit's principal summing and level

amplifier which provides signals to the NI rack indicators and

all protection functions. The meters' isolation amplifier receives

its signal from the summing and level amplifier and will deviate

from the NI rack indication if it is not adjusted after a summing

amplifier gain adjustment.

The inspector reviewed MSP 2.04, Power Range Neutron Flux Channel

(N-NI-42) Quarterly Calibration, Revision 13: This revision

includes adjusting the isolation amplifier signal to the main

control board instrumentation whenever a deviation greater than

plus or minus 1.5% exists between the NI rack indicators and MCB

meters during calorimetric calibration. The inspector had no

further questions on this item.

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(Closed) Unresolved Item (80-16-02):

Review licensee action

for NRC identified gouges on cold leg safety injection line.

During a tour of the containment building on June 4,1980, the

inspector noted several gouges on a 6 inch cold leg safety

injection line adjacent to vent valve SI-330. This was brought

to the attention of the QC Supervisor for evaluation and corrective

action. A NSQC General Inspection Report, dated June 25, 1980

identified the line as SI-73-1502-Ql, a 6 inch schedule 160 pipe

and reported a dial depth micrometer (No. 644, calibrated January

1,1980) measurement of gouge depth as a maximum wall penetration

of 0.011 inches. The condition was accepted as-is pending a

final Station Engineering evaluation of minimum wall thickness

acceptance criteria.

Engineering Memorandum (EM) 30086, approved December 21, 1981

compared the as-found wall thickness to Power Piping Code B.31.1

requirements applicable to BVPS-1.

Nominal wall thickness for

6 inch, schedule 160 pipe is 0.719 inches, minus 12.5% for

conservatism tolerance equals a minimum expected wall thickness

of 0.629 inches for standard pipe.

Subtracting the 0.011 inch

maximum 9 mge depth yields a wall thickness of 0.618 inches.

This exceeded the B31.1 acceptance criteria of 0.484 inches.

The inspector noted that the request for evaluation of minimum

wall thickness acceptance criteria was not forwarded to engineering

via EM 30086 until December 15, 1981.

b.

Followup on NRC Perfomance Appraisal

On October 19-30 and November 12-20, the NRC Performance Appraisal

Section (PAS) conducted a Performance Appraisal Inspection (50-334/

81-29) at Beaver Valley, Unit 1.

The following items were identified

as possible violations of NRC requirements and were reviewed by

the resident inspectors to determine the need for additional

enforcement action.

(Closed) Unresolved Item (81-29-02): ORC failed to review certain

documents containing violations of license requirements per TS 6.5.2.7.e.

That TS requires the Offsite Review Coonittee (ORC) to

review violations of applicable statutes, codes, regulations, orders,

TS, license requirements, or of internal procedures or instructions

having nuclear safety significance.

The PAS found that the ORC

did not review Nonconformance and Action Reports, incident reports,

and QA Surveillance Reports, all of which contain examples of such

violations. The PAS further found that the CRC may have relied

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upon Onsite Safety Committee minutes review to meet this require-

ment but that the information contained in the OSC minutes was

inadequate to pemit a thorough review.

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The inspector discussed this matter with the DLC Manager,

Nuclear Safety and Licensing, (ORC Chaiman) and reviewed

the following:

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ORCMinutes, Meeting #80(June 27,1980) through #101

December 22,1981).

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Operations Quality Control Nonconfomance and Corrective

Action Reports (NCARs), #234 (March 4, 1980) through-

  1. 275(December 3,1981).

BVPS Licensee Event Reports (LERs) 80-01 through 81-100.

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BVPS Incident Reports (not issued as Licensee Event Reports)

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Nos. 81-10 (January 12,1981) through 81-52 (April 2,1981).

Quality Assurance Department Outage Surveillance Reports,

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1980 Outage. All reports reviewed (about 250).

The inspector found that the ORC meeting minutes only documented

review of NRC inspection findings and DLC responses, DLC QA Audit

findings, prompt (24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) Licensee Event Reports, several 30 day

Licensee Event Reports, and the running status of NRC and QA

audit corrective actions. No NCARs, Incident Reports, or Sur-

veillance Reports were listed. Neither were onsite contractor

nonconformance reports. The ORC Chairman advised the inspector

that, although individual ORC members receive and review such

documents as part of their non-comittee duties, no fomal system

for referral to the ORC was used. The chairman also stated that

such items were occasionally discussed in committee but apparently

were not documented in the minutes. The inspector further noted

that the QA Surveillance Reports were not distributed outside the

QA Department. The chaiman further advised that, although OSC

minutes are routinely reviewed by the ORC, they were not used as

the document of record for review of violations per TS 6.5.2.7.e.

Reviews- intended to satisfy that requirement were conducted by

use of the actual document (LER, NRC Inspection Report, etc.),

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generally presented by a committee member.

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Typical violations of the type subject to ORC review but not

documented in the comittee's minutes include:

High Radiation Area / Contamination Area procedure and TS

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violations documented in QA Surveillance No. 007, February

26, 1980.

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Safety Injection System modification Weld Data Sheets not

complied with and Weld Data Sheets completed prior to weld

completion; documented in QA Surveillance Nos. 024, March

17,1980; 068, April 2,1980; and, 070, April 3,1980.

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Chronically recurrent cases of weld rod control procedure

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violations documented in several dozen QA Surveillances.

Unplanned or unmonitored radioactive releases documented

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in Incident Reports 81-11, January 12,1981 and 81-14,

January 22, 1981.

Personnel errors and procedure violations documented in

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LERs 81-06, 81-21, 81-17, 81-18, 81-53, 81-66, and others.

Recurrent procedure violations: QC Hold Tags, installation

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of material without receipt inspection, cable routing errors,

safety related rigging procedures, and safety related snubber

fill procedures, documented in QC NCARs.

The inspector advised the ORC Chairman that TS 6.5.2.7.e does not

require review of all violations but that an appropriate sample

of all types of violations and/or documents identifying violations

must be reviewed in committee with the goal of evaluating both the

significance of the violation and the effectiveness of preventive

and corrective 6ctions.

Failure of the ORC to review documents such as described above

constitutes violation of TS 6.5.2.7.e.

(82-01-01).

(Closed) Unresolved Item (81-29-03): No inspection of operating

activities as required by the 0QA Program. The PAS found that,

while certain activities such as maintenance and modification,

were subject to inspection by the licensee and contractor quality

control organizations, operating activities were not subject to

any in process inspection. These uninspected activities included,

but were not limited to:

Routine plant evolutions such as plant startup, shutdown,

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and routine system operation.

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Reactor engineering activities.

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Operating Surveillance Testing.

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Equipment lubrication activities.

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Chemistry activities.

Equipment clearance (tagout) activities, other than independent

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system operability and equipment position verifications.

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10CFR50, Appendix B, Criterion X, requires that a program for

inspection of activities affecting quality be established and

executed to verify confirmance with the documented instructions,

procedures, and drawings for accomplishing the activity. The

BVPS FSAR, Section A.2, contains the same requirement. BVPS

FSAR, Section A.2.2.2, states that the OQA Program applies to

plant operations associated with safety related (Category I)

structures, systems, and components. The DLC Quality Assurance

Policy, issued by the President, DLC, as part of the BVPS 0QA

Manual, requires, in Section 10, that a program for the inspection

of activities affecting quality be established and provide for

inspections during operations.

Through discussions with licensee management, including the

Manager, Nuclear Operations, and review of the BVPS 00A Manual,

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the inspector found that no program for the inspection of

operating activities had been established or executed.

Although

0QA Manual Procedure OP-9, Technical Procedure for Control of

Operations and Maintenance, Revision 1, assigns responsibility

for periodic test and inspection (Section 9.5.4),ther procedure

addresses only tests and inspections for equipment and does not

address inspection of the operating activities above.

No imple-

menting procedures for such inspections were identified.

The licensee does, however, provide for redundant and independent

verification of certain operating and surveillance test activities

such as clearance tagouts, jumper and lifted lead placement / removal,

valve lineup verifications, switch lineup verifications, etc.

These verifications are accomplished by individuals performing the

operations activity and do not meet independence requirements of

Criterion X and the 00A Program.

Similarly, the example activities

above are variously subject to supervisory review of documentation

and results and/or supervisory observation of performance. Post

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perfonnance results review does not satisfy requirements for

activity inspection.

Supervisory observation may not provide the

required inspection independence and generally does not meet the

0QA program requirements for a formalized, documented inspection

activity.

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Failure to establish and execute an inspection program for opera-

ting activities such as provided above constitutes a violation of

10CFR50, Appendix B, Criterion X and the licensee's 0QA Program.

(82-01-02).

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(Closed)

UnresolvedItem(81-29-04): Changes made to the

facility via Temporary Operating Procedures (T0Ps) and Special

Operating Orders (S00s) without adequate reviews as required

by 10CFR50, Appendix B, or 10CFR50.59. The PAS identified four

examples of potential ncacompliance:

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(1) TOP 80-27, Filling the RWST from the Boron Recovery Tanks.

The TOP provided a temporary hose flowpath for transferring

water between the tanks. The flowpath used was different

than the system arrangement described in Sections 9.1 and

9.2 of the Final Safety Analysis Report. These sections

describe the expected operation of the Chemical and Volume

Control System (CVCS) and Boron Recovery System, including

the normal flow paths for processing Boron Recovery Tanks.

The Figures of FSAR Section 9 (Flow diagrams) provide the

normal flow paths, including makeup flowpaths to the Refueling

Water Storage Tank.

The inspector found that TOP 80-27 had been approved via Onsite

Safety Committee (OSC) poll on August 15, 1980, that the poll

had been reviewed in committee on August 25,1980(Minutes

No. BV-0SC-104-80), and that the minutes did include a safety

evaluation as required by 10CFR50.59. The minutes stated that

the poll had been reviewed and that "no changes to procedures

or equipment as described in the SAR result and that no un-

reviewed safety questions results." No basis for the above

determination was provided nor was the temporary hose flow

path addressed relative to the systems as described by the

FSAR.

10CFR50.59(a)(1) permits the licensee to make changes in the

facility and procedures as described in the safety analysis

report unless a change to technical specifications or an

unreviewed safety questioncare involved.

10CFR50.59(b)

requires that the licensee maintain records of these changes,

including a written safety evaluation which provides the bases

for the determination that the change does not involve an

unreviewed safety question.

Failure to document the bases for

the acceptability of TOP 80-27 constitutes a violation of

10CFR50.59(b). An additional example of further violation is

discussed below.

(82-01-03).

(2) TOP 81-27, Operating the Temporary Liquid Waste Demineralizer

(LW-I-2).

LW-I-2 was first installed and operated by TOP 80-33

(September 4,1980) to augment the capacity of the permanently

installed Liquid Radwaste System. The permanently installed

system was unable to process sufficient volume, resulting in

undesirable backlogs of unprocessed waste. The temporary

system, consisting of temporary filters, demineralizers and

plastic piping, had been installed as an " experiment" but

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had remained in use, with some modification, through 1981.

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TOP 81-27 was issued on July 17, 1981 to reflect the use

of a different style demineralizer. OSC Meeting Minutes

BV-0SC-84-81 (July 17,1981) documented review of the

original safety evaluation (T0P 80-33, Minutes BV-0SC-80-108

(September 4, 1980))and the committee's determinaticn that

the original evaluation remained valid. The inspector reviewed

the 80-33 safety evaluation, finding that it addressed con-

sideration of each of the items recomended by IE Circular

80-18,10CFR50.59 Evaluations for Changes to Radioactive

Waste Treatment Systems, and included the bases for the

comittee determination that no unreviewed safety question

nor technical specification change were involved.

During discussions with the DLC Chief Engineer, Station

Engineering Supervisor, and cognizant Operating Foreman, the

inspector learned that the system had not been fomally

designed but rather, had been assembled in place using

commercially available components and piping. The BVPS Opera-

tions Quality Assurance Program (FSAR Appendix A.2); QA

Procedure OP-4, Design Change Control, Revision 6; and the

BVPS 0QA Manual, Appendix B, Category I Systems, Structures

and Components, Revision 3, provide the requirements for

design change and modification control for safety related

systems. The Liquid Radwaste System is not considered a

safety related system by the BVPS QA Program and is therefore

not subject to the Quality Assurance Program controls.

Although application of fomal engineering and design change

controls to this installation were desirable, no violation

of NRC requirements was identified.

The extended use of a temporary system is similarly undesirable;

the licensee has experienced periodic problems with the in-

stallation. On July 14, 1981, Station Modification Request

(SMR) 404 was issued to DLC Engineering to install an improved

but again, interim system pending availability of a pemanent

system design. As of January 29, 1981, SMR 404 remained under

licensee review.

(3) TOP 81-31, River Water System Operation While Dredging Near

Intake. The TOP provided instructions for cross-connecting

the main River Water (RW) System with the Auxiliary River

Water (ARW) System during dredging operations at the main

intake structure to provide backup ccoling capability if

dredging silt fouled the main system. The inspector reviewed

FSAR Section 9.16; FSAR Question Response 2.30; BVPS Operating

Manual, Section 1.30, River Water System, and QA Manual,

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Appendix B, Revision 2, confirming that, although the

ARW System meets some of the design requirements of an

Engineering Safety Feature System (seismic design, single

failureanalysis,emergencypowersupplies,etc.)andis

capable of supporting a plant shutdown and cooldown on loss

of the main RW system, the ARW System is not considered QA

Category I (safety related). Additionally, the FSAR does

not describe extended operation of the ARW and RW systems

in a cross-connect mode during continued reactor operation.

TheinspectorreviewedOSCMinutesBV-0SC-93-81(August 7,

1981), finding that the OSC had determined that no unreviewed

safety question existed but provided no basis for that

detemination. Although the minutes noted that one ARW

header would be in service during dredging, no evaluation of

this alignment was provided. Failure to document the basis

for the detemination that an unreviewed safety question does

not exist is contrary to 10CFR50.59(b) and constitutes an

additional example of a violation.

(82-01-03).

(4) Special Operating Order (S00) 81-9, Pressurizer Relief Tank

Alarm Setpoints. Pressurizer Power Operated Relief Valve

seat leakage had caused abnomally high pressures and tempera-

tures in the Pressurizer Relief Tank. The licensee adjusted

the PRT high pressure alam and high temperature alarm setpoints

upward to reduce the frequency of alarm actuation and to reduce

the volume of water used to spray (quench) the tank each time

the alams actuated.

The inspector reviewed draft OSC Minutes BV-OSC-77-81 (June

25,1981) finding that S00 81-9 had been reviewed and found

not to involve an unreviewed safety question. The minutes

documented review of the setpoints relative to FSAR Section

4.2.2.3 and included consideration of the higher than nomal

tank temperatures and pressures. The minutes acknowledged

that such operation could result in PRT discharge to the

containment via the rupture disc on a design basis pressurizer

safety / relief valve actuation but noted that condition to be

an analyzed event. The DLC Chief Engineer also advised the

inspector that, although not documented in the meeting minutes,

he had consulted the pressurizer safety valve vendor and

determined that the abnomal operating conditions had no

adverse effect on safety valve operation. The inspector

also noted that, on July 17, 1981, misoperation of the PRT

spray system had resulted in PRT rupture disc failure and

discharge to the containment (Reference:

NRC Inspection

Report 50-334/81-18).

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The inspector also reviewed the procedures and data used

to reset the alanns finding that the PRT temperature and

pressure channels are not included in the licensee's safety

related calibration program, that the adjustments were made

on June 25, 1981 in accordance with generic Calibration

Procedures (CP515 and CP035) for the types of instruments

involved, and that the S00 provided the interim setpoint

information to plant operators.

Although the documented safety evaluation was considered

only marginally acceptable (discussions of safety valve

operation not included), no violation of NRC requirements

was identified.

(Closed) UnresolvedItem(81-29-05): Work Instructions not

included on Maintenance Work Requests (MWRs) required by Mainte-

nance Manual. The PAS found that minimal or no work instructions

had been provided on MWRs and that, in some cases, the scope of

work had changed but was not reflected on the MWR:

MWR 810190, Diesel Generator Lube Oil System. No written

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instructions were provided to repair an oil leak. A flange

was tightened to stop the leak.

MWR 810381, Channel 1 Loop RCS Flow. No written instructions

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were provided to replace the flow transducer. The instru-

ment was calibrated in accordance with MSP 6.26, referenced

on the MWR.

!!WR 810421, Loop Protection Tavg. No written instructions

--

were provided on the MWR to perform the maintenance in

accordance with Corrective Maintenance Procedure (CMP)

1-75-45 which was used to perfonn the work.

MWR 810535, Number 2 Emergency Diesel Generator. There were

--

no written instructions on the MWR to replace the turbo-

charger in accordance with CMP 1-75-E08, which was used to

,

replace the turbo charger.

'

MWR 810566, Number 1 Emergency Diesel Generator. There

--

were no written instructions provided to repair the exhaust

bonnet for the electrical control panel.

MWR 811783, Containment Vacuum Pump. No written instructions

--

were provided to troubleshoot or repair bench board lights.

MWR 810949, Low Head Safety Injection Pump Recirculation

--

Pressure.

No written instructions were provided to replace

the pressure gauge.

y

.

13

The inspector reviewed:

BVPS QA Procedure OP-10, Maintenance and Modification

--

Planning, Revision 3;

BVPS QA Procedure OP-9, Technical Procedure Control for

--

Operations and Maintenance, Revision 3; and,

--

BVPS Maintenance Manual (MM), Chapter 1, Conduct of Maintenance,

Section A, General Rules for Implementation, Revision 14.

OP-10 provides requirements for work orders (Maintenance Work

Requests) and supplemental procedures or instructions for main-

tenance activities affecting quality. The OP requires that the

MWRs and/or supplemental procedures prescribe what is to be

accomplished and provide for a record of the quality achievements

andverifications(Section10.3.5). Any changes to the work order

or procedures must also be controlled, including review and approval

in the same manner as the original (Section 10.4.7).

MM Chapter 1, Section A, provides equivalent requirements.

Section

4.a.7 pemits instructions to be written in the " Additional Work

Instructions" section of the MWR for simple tasks requiring only

a few steps, otherwise Section 4.a.9 requires use of a written

procedure. Section 7.c requires that work shall be accomplished

as described in the instructions or procedures. Section 7.d requires

that any changes to instructions or procedures shall follow the

same approval process as the original procedures (except for on-

the-spot procedure revisions).

The inspector's review of the specific MWR examples identified no

actual problems resulting from the absence of work instructions

or procedure references. The work specified by these MWRs involved

troubleshooting / repairing.

In the case of sample repairs, the

repair was accomplished during the act of trouoleshooting.

Detailed

work instructions were inappropriate because the task was considered

to be within the skills nomally possessed by qualified maintenance

personnel.

In those cases where the troubleshooting identified a

more significant repair task, appropriate maintenance / calibration

procedures were subsequently referenced on the MWR and used in

the repair.

Discussions with the DLC Maintenance Supervisor

established that infomal oral comunications are normally used

to accomodate the inspector's concerns. However, the inspector's

review identified the following additional concerns:

(1) The Quality Control Department initially reviews MWRs and

detemines whether QC inspection coverage is required or de-

s t rable. A change in MWR scope does not appear subject to

additional QC review, particularly if a change in scope is

not documented on the MWR or is not subject to other specific

maintenance procedures.

_

.

.

14

(2) Similarly a change in scope may affect the post-maintenance

testing to be performed by the Operations Department. Failure

to document such changes do not pemit adequate Shift Super-

visor review upon closeout of the MWR.

(3) A change in work scope may also require a change in clearance

(tagout) boundaries. The licensee's procedures for MWR

control do not address such changes.

(4) The specific " additional work instructions" or reference

to supplemental procedures would nomally establish an authorized

scope of work and limit the worker's ability to extend the

scope of work without change control.

(5) None of the MWR examples included " additional work instructions"

or reference to supplement procedures or instructions (except

MWR 810381 which referenced a precedure for calibration of

thenewtransmitter).

The licensee acknowledged the inspector's concerns. The station

Maintenance Supervisor advised the inspector that procedure revisions

were in preparation at the close of this inspection and would be

issued by March 1, 1982. This matter will remain unresolved pend-

ing NRC:RI review of the procedures when implemented.

(82-01-07).

(Closed) UnresolvedItem(81-29-06): Vital Battery cells jumpered

without perfomance of 10CFR50.59 safety evaluation. On October

17, 1981, the number of cells in the No.1 bP.tery was reduced

from 60 (the number specified in the FSAR)to 58 in accordance

with MWR 817707 and Corrective Maintenance Procedure (CMP) 1-39DC-

Bat 1, 2, 3, 4-2E, Revision 1.

The cells had failed to meet the

voltage requirement of TS 4.8.2.3.2.b.1.

The remaining 58 cells

appeared to meet the minimum voltage requirements of TS but a written

safety evaluation had not been perfomed to establish that the

remaining battery capacity met FSAR and TS requirements.

During December,1981 - January,1982 the licensee was unable to

provide documentation of a written safety evaluation predating

the above change. The inspector reviewed OSC Minutes BV-0SC-68-79

(October 4, 1979) and -18-80 (January 30,1980) which documented

OSC review of Revision 0 and 1, respectively, of the jumper

installation CMP. The inspector found that the OSC had determined

no unreviewed safety questions existed but had failed to provide

the bases for that determination.No additional information was

available.

..

.

.

15

Although failure to provide a written safety evaluation per

10CFR50.59(b) is a violation of NRC requirements, a Notice of

Violation will not be issued. NRC Inspection 50-334/81-28

identified a similar violation for other jumper installations.

The licensee's response letter (dated February 8,1982) to

NRC:RI for that violation specifically addresses the corrective

and preventive actions regarding battery cell jumpers.

After the PAS finding, the licensee prepared a Safety Evaluation

Report, dated December 17, 1982, properly documenting the

determination that no unreviewed safety question exists for

jumpered battery cells. The safety evaluation addressed FSAR

and TS 4.8.2.3 capacity requirements and recommended a limit of

2 cells per battery be jumpered at any time. The safety evaluation

was reviewed by the OSC at Meeting BV-0SC-137-81 on December 31,

1981.

The minutes of this meeting were in preparation at the

end of this inspection.

The OSC also recommended that the Corrective Maintenance Pro-

cedures be revised to include the limit of two cells per battery

jumpered. The inspectors confirmed that the revised procedures

were approved on January 12, 1982 and were pending final typing

and distribution at the close of this inspection.

During this and prior inspections, the inspectors had discussed

TS 4.8.2.3.2.b.1 with licensee management, including the Chief

Engineer and Superintendent of Technical Services. The TS

requires that the voltage of each connected cell be greater than

2.02 volts under float charge and that the voltage has not decreased

more than 0.05 from the value observed during the original acceptance

test. The inspectors noted that IEEE Standard 484-1975, Installa-

tion of Large Lead Storage Batteries, considers an individual cell

acceptable if its voltage is within 0.4 volts of the average of

all cells. The licensee has experienced difficulty in maintaining

both original and replacement cells within 0.05 volts of their

original acceptance test values. The inspectors advised the

licensee that consideration of a TS change consistent with the

guidance of the IEEE Standard appeared appropriate.

(Closed) Unresolved Item (81-29-07): Audit program plan not

developed to assure coverage of applicable quality assurance pro-

gram.

10CFR50, Appendix B, Criteria XVIII requires the licensee

to establish a comprehensive system of planned and periodic audits

to verify compliance with all aspects of the quality assurance

program. ANSI N45.2.12, paragraph 3.3, Audit Planning, endorsed

by FSAR, Appendix A, Attachment to Table A.2, further requires

that the audit system be planned, documented, and conducted to

assure coverage of the applicable quality assurance program.

The audit system is to be periodically reviewed and revised as

necessary to assure that coverage and schedule reflect current

activities.

_ _ _ _ . .

_ _ _

.

.

16

QA Procedure OP-16, Revision 2, Section 16.4, Audit Planning,

provides guidance for scheduling audits that are planned, con-

ducted and reported in accordance with written procedures.

These procedures are to be revised, approved for use, and updated

as necessary. QA Procedure OP-16, does not provide for system

plans to assure coverage of all aspects of the quality assurance

program. QA Instruction 18.1.1, Revision 6, implements the QA

audit schedule requirements. The Senior QA Engineer is responsible

for assuring that audit responsibilities and obligations are met.

These responsibilities include detennining the areas to be audited

and the maintenance of audit schedule. The QA Manager approves

the audit schedules. The audit schedule is prepared annually

and reviewed quarterly by the QA Manager and lists all areas

requiring a QA audit. The audit schedule by itself does not

provide assurance that all aspects of the applicable QA program

have been covered, nor can it identify those areas that still

need coverage. The inspector held discussions with licensee QA

representatives to determine whether an alternate means existed

for assuring that all aspects of the program were covered by the

end of the year. None were identified.

Failure to develop an audit program system plan that can assure

coverage of all aspects of the QA program is a violation of

10CFR50, Appendix B, Criteria XVIII.

(82-01-04).

(Closed) Unresolved Item (81-29-08):

1980 0QA Program Manage-

ment Audit did not address all activities subject to 10CFR50,

Appencix B.

TS 6.5.2.8 requires that an audit of 0QA Program implementation be

performed under the cognizance of the Offsite Review Connittee (ORC)

at least once per 24 months. The audit must encompass the per-

formance of all activities required by the 0QA program to meet

the criteria of 10CFR50, Appendix B.

10CFR50, Appendix B,

Criterion II, and BVPS OQA Procedure OP-1, Revision 4, also

require a management review (biennially per OP-1) to assess the

status and adequacy of the 0QA Program.

The PAS found that the 1980 Management Audit, performed by a

contractor, was intended to satisfy both the 0QA Program and TS

requirements. That audit addressed only five of sixteen major

0QA procedures used to implement the eighteen criteria of 10CFR50,

Appendix B.

The PAS also found that, although the audit report

was submitted to the licensee in December,1980, the report was not

distributed to the Offsite Review Connittee until September 29,

1981.

.

.

17

The inspector reviewed the 1980 audit, the licensee's management

auditplan(Memo,C.N.Dunn,datedAugust 18,1978),the1977

and 1978 management audits, and applicable sections of the 0QA

Procedures (ops). The inspector found that the licensee's audit

plan provided for the audit of the implementation of four or five

0QA Procedures during each biennial audit.

(Note: The OP-1 audit

requirements were changed from annual to biennial in 1979). The

inspector confimed that each audit report documented confomance

with the audit plan.

Implementation of the audit plan would result

in complete coverage of all 0QA procedures over a five year period.

Perfomance of biennial cudits for only portions of the 0QA proce-

dures does not constitute an adequate management review pursuant

to 10CFR50, Appendix B, Criterion II nor an adequate ORC audit

pursuant to TS 6.5.2.8.d and is considered a violation.

(82-01-05).

An additional example of similar violation is discussed in Item

81-29-09 below.

The inspector found that the late distribution of the 1980 Audit

Report to the ORC was apparently the result of administrative

oversight. Cognizant managers of the audited areas had apparently

received distribution of the report upon its receipt from the

contractor and at least once again in mid-1981. The report had

not, however, been fomally distributed to and reviewed by the

ORC. The inspector did not review the adequacy or timeliness of

corrective actions or ORC audit followup.

(Closed) Unresolved Item (81-29-09): Operation training audit

inadequate in scope and depth. The QA Department under the cog-

nizance of the ORC, conducted audit BV-1-81-4 on March 24 - April

4, 1981, to comply with the requirements of TS paragraph 6.5.2.8.b,

for the annual audit of the performance, training and qualification

of the entire facility staff. The inspector reviewed this audit

and discussed its content and scope with the lead auditor. The

audit was conducted to cover: BVPS training; training for Con-

struction Department - Nuclear, Schneider, Incorporated, Sargent

Electric Company and Dick Corporation personnel under their

Program requirements, as related to BVPS Unit 1 modification

program; and, to meet the requirements of TS 6.5.2.8.b.

The

audit consisted mainly of training record reviews for the above

groups, requalification training of licensed operators and

radiation technician training. The audit did not address the

staff areas of: mechanical and electrical maintenance, instru-

ment and control, testing and plant perfomance, reactor control

chemistry, station engineering, or the technical advisory group.

Though the licensee was undergoing a reorganization during the

period of audit, the organization of the above plant groups

remained essentially unchanged.

_

,

.

18

The scope of the audit was insufficient in that it did not address

the qualifications of any staff group, other than licensed operators

and radiation technicians, nor did it address the performance of

any group to assure that personnel performing a specified job

function were trained and qualified to do those jobs.

Failure to audit the performance of any facility staff group,

and failure to audit the training and qualifications for some

facility staff groups (mentioned above) constitutes another

example of violation of TS 6.5.2.8.

(82-01-05).

(Closed) UnresolvedItem(81-29-10): QA audits did not include

observations of perfomance of operating and maintenance activities

for 1980 and 1981. The inspector reviewed the following QA audits

of maintenance and operations activities perfomed in 1980 and

1981:

BV-1-80-33, Operations

--

BV-1-80-15, Maintenance

--

--

BV-1-89-39, Maintenance

BV-1-81-10, Maintenance

--

BV-1-81-28, Operations

--

BV-1-81-30, Maintenance

--

Through this review and discussions with licensee QA personnel, the

inspector detemined that the QA audits of operations and mainte-

nance activities did not include documented observations of any

activities in either audit checklists or results.

ANSI N18.7-1972, Administrative Controls for Nuclear Power Plants,

Section 4.4 requires audits to include observations of operations

and maintenance activities in addition to reviews of procedures

and records and interviews. ANSI N18.7-1972 is endorsed by the

BVPS FSAR, Appendix A.2, 00A Program, Section A.2.2, via Endorse-

ment of NRC Regulatory Guide 1.33-1972.

Quality Assurance Procedure OP-16, Audits, Revision 2, does not

include requirements for such observations during audits. Failure

to establish and implement procedure requirements for audit observa-

tions of such activities is a violation of 10CFR50, Appendix B,

Criterion XVIII; the BVPS FSAR, Appendix A.2 and ANSI N18.7-1972

as endorsed by Regulatory Guide 1.33.

(82-01-0 4).

.

.

19

(Closed) UnresolvedItem(81-29-11):

Personnel conducting audit

of Plant Operations did not have training or experience in nuclear

plant operations. The inspector reviewed the personnel folders

of the auditors who performed Quality Assurance (QA) audit

BV-1-81-28, Operations, during September 21 - October 7, 1981.

Prior to this audit, the team leader had performed 11 other audits

in 1981, none of which involved operations. This individual met

the audit team leader qualification requirements specified in QA

Instruction (QAI)

2.1.3, Training and Qualification of Auditors,

Revision.4, issued March 16, 1979. He also participated in a

continuing auditor training program as specified in QAI 2.1.2,

Training of QA Personnel, Revision 5, issued February 23, 1981.

However, this individual has had no previous experience in nuclear

plant operations nor other specialized training. The other audit

team member had received approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> of operations

related training between 1976 and 1981; however, he too had

no previous experience in plant operations. Neither QAI 2.1.2

nor QAI 2.1.3 require specialized training or experience to

establish that the auditors' qualifications are commensurate with

the special nature of the activities to be audited.

ANSI N45.2.12-1974 as endorsed by the BVPS FSAR, Attachment to

Appendix A-2, requires that QA personnel or technical specialists

be selected for an auditing assignment based on experience or train-

ing which establish that their qualifications are comensurate with

the complexity or

special nature of the activities being audited.

Although both individuals participating in audit BV-1-81-28 were

_

qualified auditors, neither had plant operation experience nor

specialized training in this area. Failure to provide require-

ments for selection of auditors or use of technical specialists

having qualifications commensurate with the complexity or special

'

nature of activities to be audited is a violation of ANSI Standard

N45.2.12. _(82-01-04).

(0 pen) Unresolved Item (81-29-12): Written training, reh &ing,

and replacement training program for all unlicensed personnai not

provided and fully implemented.

(0 pen) UnresolvedItem(81-29-13):

Key personnel not provided BVPS plant specific training as required

by BVPS FSAR Section 12.2.

The PAS found that established training programs did not appear

to meet all requirements of the licer.see's OQA program and Technical

Specifications and that existing programs specified in the BVPS

Training Manual had not been fully implemented. Additionally,

key personnel reassigned to CVPS from other DLC facilities had not

been provided plant specific training.

.

.

.

20

The review of these two items was in progress at the end of this

inspection. The inspector had reviewed the applicable regulatory

requirements and was reviewing a sample of facility staff member

training records for compliance with the licensee's existing

programs and license requirements.

Items 81-29-12 and -13 will

remain unresolved pending completion of the inspector's review.

During the review, the inspector found that BVPS Maintenance

Department required reading assignments had not been p(MM) contains

roperly

performed. Chapter 1 of the BVPS Maintenance Manual

administrative procedures for the control of maintenance activities.

Chapter 1. Section A.5.b, Revision 14, requires electricicans,

mechanics, and meter and control repairmen (instrument technicans)

to read pertinent sections of Chapter 1.

The table below shows

inspection results for a sample of 5 individuals whose records

were reviewed:

MM Section

N

Q

H

J

W

Y

Z

0

Legend

Electr. A

C

C

I

C

X

C = Complete

Electr. B

C

C

I

C

X

I = Training

incomplete or

Mech. A

X

X

C

C

C

I

C

C

not documented

X = Not required

Mech. B

X

X

I

I

C

I

C

I

for job classi

fication

Tech. A

C

X

C

C

C

I

C

C

  • = Training in-

complete but

Tech. B

I

X

I

I

I

I

I

C

identified by

DLC internal

memo dated

4/16/81

Section N - Relay Testing

Section Q - Motor Repair

Section H - Cleaning & Maintaining Cleanliness

Section J - Housekeeping

Section 0 - Calibration Program

Section W - Maintenance Procedure Control

Section Y - Control & Maintenance of Respiratory Equipment

Section Z - General Work Practices

Each individual is rated as a "first class" craft worker normally

assigned to safety related maintenance activities. Of the 40 re-

quired reading assignments sampled, only 20 had been recorded as

complete.

.

21

10CFR50, Appendix B, Criterion II, requires that the OAQ program

provide for indoctrination and training of personnel performing

activities affecting quality as necessary to assure that suitable

proficiency is achieved and maintained. The BVPS FSAR, Appendix

A.2.2.2, states that indoctrination and training measures assure

that all responsible individuals are aware of quality policies,

procedures and manuals and have an adequate understanding of these

requirements. QA Procedure OP-14, Indoctrination and Training,

Section 14.4.1, Revision 3, requires that station personnel shall

be trained, as appropriate, to achieve special skills required in

the performance of equipment protection, process, and test pro-

cedures and that retraining will be provided as necessary to main-

tain adequate proficiency.

The BVPS MM, Chapter 1, Section A.5.b, General Rules for Implemen-

tation, Revision 14, requires individuals to receive indoctrina-

tion on specific sections of the manual (as represented in the

above table) and to document completion of the training. Failure

to complete and document this training constitutes a violation.

(82-01-06).

(Closed) UnresolvedItem(81-29-14):

Training records not stored

in accordance with QA Program requirements and ANSI N45.2.9. The

PAS found that training records were improperly stored at the Nuclear

Division Training Center (the Johnson Street School) and that de-

partmental training records maintained by managers and supervisors

were not subject to QA record requirements.

The inspector reviewed records at the Johnson Street School and in

various station departments with respect to Technical Specification 6.10.2; QA Procedure OP-15, QA Records, Revision 1; and ANSI

N45.2.9-1974Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.9-1974" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Requirements for the Collection, Storage, and Main-

tenance of Quality Assurance Records for Nuclear Power Plants.

Discussions were held through the inspection with Nuclear Division

supervisors including the Manager, Nuclear Support Services, and

the Nuclear Division Director, Adininistrative Services.

The inspector determined that the licensee had established an on-

going QA records review and upgrade program, already addressing plant

drawings, technical manuals, maintenance work requests, and various

procedure records; establishment of satelite record centers; and,

division-wide categorization and indexing of QA records.

Each

activity resulted from prior licensee identification of records

program deficiencies or record discrepancies. Corrective actions

for each problem were either in progress or in planning.

,

- , - -

'

22

The inspector found that single copy training records at the

Johnson Street School and in BVPS-1 station departments were

not stored or maintained in accordance with the above require-

ments but that the licensee had initiated corrective actions

similar to the others above. Other areas requiring similar

licensee attention identified by the inspector were: station

incident reports, operating procedure and valve lineup records,

radwaste and transportation records, and certain maintenance

records. By the end of this inspection the licensee had begun

addressing each of these items as part of the overall effort.

The Nuclear Division Director, Administrative Services advised

the inspector that:

1) a fire loading / rating survey had been

completed for the Johnson Street School records room; 2) engineer-

ing action was in progress to upgrade that facility to meet ANSI

N45.2.9Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.9" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. requirements; 3) the use of computerized duplicate

training records was being evaluated; and 4) an expected date of

completion of actions for the Johnson Street facility would be

provided to the inspector by about March 15, 1982. The Nuclear

Division Director, Administrative Services further advised that

a general review of in-plant and divisional records would be

performed to ensure that all single copy records were properly

stored; the expected date of completion would also be provided

by about March 15, 1982. The acceptability of the licensee's

actions in this matter will remain unresolved (82-01-08).

Unresolved Item 81-29-14 will be closed.

(Closed) Unresolved Item (81-29-15): Appropriate acceptance

criteria not available for activities affecting quality.

PAS

review of Welding Manual Procedure No.1.4, Welding Electrode

Control, and NSQC 8.1, Storeroom Quality Control, found that

certain activities affecting quality were not governed by appro-

priate acceptance criteria.

(1) QA Procedure OP-12, Control of Measuring and Test Equipment,

Revision 3, requires the calibration of instruments and

measuring devices used in activities affecting quality,

regardless of the owner or user. Welding Manual Procedure

No.1.4, Welding Electrode Control, Revision 1, requires

that ovens used to store covered electrodes be maintained

0

at 250-300 F. During the PE> inspection the inspector observed

I

that thermometers used to determine the temperature of the

weld electrode oven in the Maintenance Department had not

been calibrated.

The licensee has since calibrated the thermometer and has

scheduled it for periodic recalibration in accordance with

their administrative controls. The inspector had no further

questions on this item.

.

.

.

23

(2) General Stores (GS) Procedure 204.0, Storage Functions,

Revision 2, requires that temperature and humidity be

controlled within specified limits for the Level A storage

room. The inspector noted that the temperature and humidity

recording instruments had not been calibrated. A sampling

review of purchase requisitions by the inspector failed to

identify any piece of equipment that required Level A storage.

Although the licensee had stored electronic instruments and

parts in this storage area, the inspector verified that this

equipment did not require this level of storage. The licensee

has since initiated a calibration program for the storeroom

instrumentation. As Level A storage was apparently not required

up to this time and the licensee has instituted a routine

calibration program for those instruments, the inspector had

no further questions on this matter.

(3) The temperature and humidity limits discussed in GS 204.0

are not specified by the procedure. Through discussions

with Stores personnel, the inspector determined that these

limits had not been established at the time of the PAS. inspection.

The licensee has since issued a memorandum that specifies

appropriate limits, subject to change as required to meet

special material storage requirements. As there has apparently

never been equipment stored in the Level A storage room that

required these special temperature and humidity controls,

the inspector had no further questions at this time.

(Closed) Unresolved Item (81-29-16): The PAS identified the

following items related to storage and inspection of materials:

(1) Bags of cement were stored within 10-15 feet of reactor

plant equipment such as pumps, motors, valves, and spare

parts in the warehouse. Several cement bags had been punctured.

A plastic tarp used for covering one skid of cement was not

in place.

The tarp was immediately lowered over the exposed

cement bags to contain any dust. The inspector had no

further questions on this item.

(2) Openings in four Limitorque valve operators did not have

covers or seals to prevent foreign material from entering

the valve operators.The PAS inspector further noted that

attached vendor instructions directed that desiccant be

added if the operators were not immediately installed.

Discussions with storeroom personnel confirmed that instruc-

tions from Engineering specifying storage and maintenance

requirements were not available and that stores personnel

__

.

.

24

had not been instructed to look for vendor storage require-

ments.

During this inspection, the inspector confirmed that the

open valve parts had been covered and that requirements for

installation inspections and cleaning would assure proper

cleanliness levels if and when the valves are used in reactor

plant systems. When the licensee disassembled the valve

operator to add disiccant, three packs were found inside the

operator, apparently added by the vendor before shipping.

The licensee's overall program receipt and storage of equip-

ment and material will be inspected in the near future as

part of the prescribed inspection program. The inspector

had no further questions on this item.

(0 pen) Unresolved Item (81-29-01): Bases for 10CFR50.59(b) deter-

minations not documented by Onsite Safety Committee (OSC) for

procedure changes. The PAS found that the committee did not

make written evaluations of procedures or changes to procedures

to document the bases for their detennination that no unreviewed

safety question existed.

The inspector reviewed a sample of 50 procedure changes documented

in OSC Meeting Minutes BV-0SC-71-81 (June 10,1981) through

BV-0SC-131-81 (December 17,1981), including changes to operating

procedures, surveillance procedures, calibration procedures, and

system descriptions. The inspector also reviewed Section 12.5,

Procedures, of the BVPS FSAR and selected other sections discussing

test and inspection procedures. The inspector found that none of

the fifty procedure changes sampled appeared to constitute a change

to the procedure as described by the FSAR. This item remains

open pending additional NRC:RI management review.

-

- _

1

.

.

25

3.

Plant Operations

a.

General

The facility was shutdown for all of the inspection.

Inspections

and plant tours were conducted during day and night shifts with

respect to outage activities and maintenance of safe shutdown

conditions. Acceptance criteria for those inspections included:

--

BVPS FSAR Appendix A, Technical Specifications

BVPS Operations Manual, Chapter 48, Conduct of Operations

--

--

OM 1.48.5 Section D Jumpers and Lifted Leads

OM 1.48.6, Clearance Procedure 3

--

OM 1.48.8, Records

--

OM 1.48.9, Rules of Practice

--

BVPS Operations Manual, Chapter 55A, Periodic Checks -

--

Operating Surveillance Tests

BVPS Maintenance Manual, Chapter 1, Conduct of Maintenance,

--

Section J, Housekeeping

BVPS Radcon Manual, various sections

--

10CFR50.54(k), Control Room Manning Requirements

--

--

Inspector Judgement

--

BVPS Physical Security Plan

Findings resulting from these inspections are discussed in

paragraph 31 below.

b.

Areas Inspected

Primary Auxiliary Building, including High Radiation Areas

--

and Loose Surface Contamination Areas

--

Service Building

Main Steam Valve Room

--

Purge Duct Room

--

--

East / West Cable Vaults

--

Emergency Diesel Generator Rooms

Containment Building, including High Radiation Areas

--

Penetration Areas

--

Safeguards Areas

--

,

Various Switchgear Rooms, Cable Spreading Room

l

--

Protected Area

l

--

l

The inspectors also toured the Control Room regularly to review

logs and records and conduct discussions with operators concerning

l

reasons for selected lighted annunciators and knowledge of recent

'

changes to procedures, facility configuration and plant conditions.

,

!

,

_

_

_

.

.

26

c.

During daily Control Room tours the inspectors made the following

observations:

(1)

Instrument and recorder traces for systems required during

shutdown were observed for abnomalities. Systems included:

--

Residual Heat Removal (RHR) System

Chemical and Volume Control System (CVCS)

--

Fuel Pool Cooling and Purification System

--

Supplementary Leak Collection and Release (SLCRS) System

--

Liquid (LW) and Gaseous (GW) Radioactive Waste Systems

--

--

Fire Protection Systems

NuclearInstrument(NI) System

--

--

ProcessandAreaRadiationMonitors(RMs)

Offsite and Onsite Electrical Power Systems

--

(2) Proper Control Room and shift manning were confimed. Control

of personnel access was confimed to be in accordance with the

BVPS OM, Section 1.48.

(3) The inspectors verified operator adherence to approved operating

procedures for partial RCS draindown per BVPS OM Section 1.6.4.N.

Draining RCS to Centerline of Hot Leg Loops for Maintenance,

Revision 3.

These inspections activities are further discussed

in paragraph 5 of this report.

(4) The following licensee logs and documents were reviewed daily

on a rotating basis during the inspection to obtain infomation

on plant conditions, determine compliance with regulatory re-

quirements and assess the effectiveness of the communications

provided by the documents:

Nuclear Shift Supervisors Logs

--

Nuclear Control Operator Logs

--

Equipment Clearance Logs

--

--

Caution Tag Log

Special Operating Orders

--

Waste Handling Systems 7 Day Running Logs

--

--

Chemistry Log Sheets

Nuclear Shift Operating Foreman Logs

--

Radcon Foreman Logs

--

--

EquipmentOutofService(00S) Logs

--

Temporary Operating Procedures & Log

Temporary Logs Sheets (for special surveillance or

--

operations)

--

Nuclear (auxiliary) Operator Logs

  • Note:

Each of these logs was reviewed for the entire inspection

period. All other logs were reviewed at least weekly.

_ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . . _ _ _ . .

.

.

27

(5) The inspectors observed Control Room instrumentation,

controls, and indicators to verify that ongoing operations

and maintenance of shutdown conditions were in conformance

with Technical Specification (TS) Limiting Conditions for

Operations (LCOs). Portions of the below TS LCOs confirmable

from the Control Room were observed on the dates shown:

TS

Title

Date

3.1.1. 2

Reactivity Control System,

January 6, 1982

0

Tevg less than 200 F

January 14,1982

February 2,1982

3.1.2.3

Reactivity Control System,

January 7,1982

Charging Pump - Shutdown

February 2,1982

February 4,1982

3.4.1.3

Reactor Coolant System -

January 8,1982

Shutdown

January 11,1982

January 13,1982

January 19,1982

February 4,1982

3.8.2.2

Electrical Power System -

January 11,1982

A.C. Distribution - Shutdown

January 14,1982

January 19,1982

3.8.1.2

Electrical Power System -

January 13,1982

Shutdown

January 28,1982

January 29,1982

February 2,1982

3.1. 2.1

Reactivity Control System,

January 14,1982

Boration System

January 22,1982

February 2,1982

3.1.2.7

Reactivity Control System,

January 18,1982

Borated Water Sources - Shutdown

January 22,1982

February 2, 1982

3.1.2.5

Reactivity Control System, Boric

January 22,1982

Acid Transfer Pump

February 2,1982

. _ - _ _ - _ _ _ _ _ . _ _ _ _ _ _

.

.

28

(6) The inspectors reviewed completed surveillance tests to

verify that:

the tests were completed as scheduled; test

results were reviewed by responsible supervisors, and that

corrective actions were initiated for test identified

deficiencies:

OST 1.43.1 - TS Required Area and Process Monitors

--

Channel Functional Test, Revision 5, performed

January 6, 1982, following corrective action on

RM-RW-100 per MWR 816045.

OST 1.43.2 - Area and Process Monitors Channel

--

Functional Check, Revision 16, completed January 6,

1982 to return RM-VS-105 to service.

--

OST 1.39.lD - Weekly Battery Check - Battery No. 4,

Revision 7, performed January 21, 1982.

OST 1.20.1, Spent Fuel Pool Level Verification,

--

Revision 0, perfomed January 21, 1982.

OST 1.49.2, Shutdown Margin Calculations, Revision 11,

--

perfomed January 6,13, and 22,1982.

OST 1.20.2, FC-P-1A Fuel Pool Pump Operability Test,

--

Revision 7, initiated January ll,1982 and put on hold

for review after the pump failed to meet the differential

pressure acceptance criteria.

MSP 21.06, P-495 1C Steamline Pressure Protection (Loop

--

3) Channel III Test, Revision 3, perfomed December

24, 1981.

MSP 13.09, L-100A RWST Level Loop Channel III Test,

--

Revision 2, perfomed December 24, 1981.

--

MSP 10.02, RHR Automatic Isolation and Pressure Interlock

Test, Channel II, Revision 3, performed January 1, 1982.

MSP 2.10, Nuclear Instrument Source Range N-32

--

Calibration, Revision 4, performed December 29, 1981.

OST 1.7.3, Boric Acid Transfer Pump Operational Test,

--

Revision 21, performed January 22, 1982.

--

OST 1.39.lE, Weekly Station Batter Check, Battery No. 5,

Revision 8, performed January 22, 1982.

-.

-

.

_

_ _-

.

0

29

--

OST 1.7.8, Boric Acid Storage Tanks and RWST Level

and Temperature Verifications, Revision 6, perfomed

January 22, 1982.

OST 1.32.1, Chemical Waste Sump, pH Monitor Operability

--

Check, Revision 5, and OM Change Notice 82-12, performed

January 14 and 22,1982.

OST 1.16.2, Supplementary Leak Collection and Release

--

Exhaust Fan and Remote Damper Component Test (Train B),

Revision 8, performed January 6, 1982.

OST 1.48.1, Mode 5 and 6 ESF Train Operability, Revision

--

5, performed January 6 and 13,1982 for Train "B."

OST 1.36.7, Offsite to Onsite Power Distribution System

--

Breaker Alignment Verification, Revision 18, perfomed

January 9, 1982 for Mode 5 conditions.

OST 1.36.9, AC Power Source Breaker Alignment Verification

-

--

During Shutdown, Revision 1, performed January 9, 1982.

OST 1.11.10, Boron Injection Flow Path Power Operated

--

Valve Exercise, Revision 30, perfomed January 12, 1982.

OST 1.7.3, Boric Acid Transfer Pump Operational Test,

--

Revision 21, perfomed January 29, 1982, OMCN 82-03,

January 5,1982.

OST 1.1.10, Cold Shutdown Valve Exercise, Revision 29,

--

performed January 28, 1982.

OST 1.7.8, Boric Acid Storage Tanks and RWST Level and

--

Temperature Verification, Revision 17, performed January

28, 1982.

OST 1.33.3, Fire Protection System Drain Test, Revision

--

33, performed January 23, 1982.

OST 1.39.1A, Weekly Battery Check - Battery No. 1,

--

Revision 7, performed February 8,1982.

--

OST 1.39.1B, Weekly Battery Check - Battery No. 2,

Revision 7, perfomed February 8,1982.

_

.

30

OST 1.49.2, Shutdown Margin Calculation, Revision ll,

--

perfonned February 9 and 10,1982.

OST 1.16.5, Fuel Building Ventilation System Verifica-

--

tion - Fuel Storage, Revision 7, performed February 10,

1982.

OST 1.36.2 - Diesel Generator No. 2 Monthly Test,

--

Revision 25, perfomed February 4,1982.

d.

The following activities were inspected during tours of the plant

areas listed in paragraph 3.b:

(1) Safety related tagouts (below) were verified to be properly

posted with equipment properly positioned and redundant equip-

mentoperable(ifrequired):

--

"A" Emergency Diesel Generator, Equipment Clearance Tag

No. 473726 and 466270, placed January 6, 1982.

Pressurizer Heaters, Equipment Clearance Tag No. 466277,

--

observed January 18, 1982.

"C" Component Cooling Water Pump, Equipment Clearance

--

Tag No. 466140 and 466214, observed January 8, 1982.

M0V-RC-557 A&B, Equipment Clearance No. 466315 and

--

444316, placed February 11, 1982.

(2) The inspectors independently verified plant conditions and

equipment status required for confomance with the following

TS LCOs during inspection tours outside the Control Room:

--

TS 3.4.1.3 - Reactor Coolant Systems - Shutdown

TS 3.8.1.2 - Electrical Power Systems - Shutdown

--

--

TS 3.8.2.2 - Electrical Power Systems - AC Distribution

TS 3.4.2 - Reactor Coolant Systems - Safety Valves

--

TS 3.7.15 - Fire Barrier Penetrations

--

TS 3.7.14.4 - Fire Hose Stations

--

(3) General plant / equipment conditions including operability

and verification of standby equipment, pipe hanger / seismic

restraint settings and oil levels, and instrumentation and

recorders functional.

(4) The inspectors verified that Maintenance Work Requests (MWRs)

had been initiated for equipment in need of maintenance and

that proper priorities had been assigned to the repairs.

Examples include:

.

.

31

MWR 816045, completed January 6,1982 to repair

--

RM-RW-100

MWR 820046, completed January 6, 1982 to repair

--

MOV-RH-758

MWR 820045, completed January 6,1982 to repair

--

FCV-CH-ll4

MWR 817917, observed maintenance activities on

--

January 29, 1982 to rebuild PCV-MS-106A

(5) Toured areas were observed for fire hazards, availability

and operability of fire fighting equipment and emergency

equipment, and general condition of fire alarms and actuating

controls. The inspectors verified that observed ignition

sources were being controlled in accordance with BVPS OM

Section 1.56.

(6) The following ongoing activities outside the Control Room

were observed to confinn that they were conducted in

accordance with applicable administrative controls:

Rebuild Steam Dump Valve TCV-MS-106A6 per:

(i)MWR817918

--

for mechanical work; and, (ii) MWR 817917 for actuator

work. The inspector verified proper equipment clearance

per Clearance No. 479124.

Completion of OST 1.39.lC, Weekly Battery Check - Battery

--

3, Revision 7, performed January 21, 1982.

(7) Plant housekeeping conditions and cleanliness were observed

to confirm that:

--

Critical clean areas are controlled.

Excess materials and materials are returned to storage

--

areas.

Combustible materials and debris are promptly removed

--

from the facility.

(8) The inspectors observed implementation of the Physical Security

Plan, including:

Proper manning of the security organization.

--

Security personnel were capable of performing their

--

assigned functions.

--

Protected Area barriers were not degraded.

Isolations Zones were clear.

--

Persons and packages were properly checked prior to

--

Protected Area entry.

.

.

32

Vehicles are properly authorized, searched and

--

escorted or controlled within the Protected Area.

'

Persons within the Protected and Vital areas display

i

--

photo identification badges and are properly escorted

if required.

Communications checks were conducted and proper com-

--

munications devices were available.

Compensatory measures were employed when required by

--

security equipment failure or impairment and were

effective.

Security access controls to vital areas are properly

--

implemented.

Response force composed of specified amed individuals

--

available and responded in a timely manner on January

19, 1982.

Explosives Detector Alam checked prior to returning to

--

service on January 13, 1982.

--

Vital Area controls for outage activities are also

discussed in paragraph 14 of this report.

(9) Shift turnovers of the following work groups / departments

were periodically observed to ensure continuity of infoma-

tion between shifts:

Group

Date

Operations

January 6, 7, 11, 14, 18, 21,

and 26, 1982

Health Physics

January 8,13, 22 and 28,1982

Security

February 11, 1982

Test Group

January 21, 1982

(10) The following radiological control activities were observed

on day and night shifts:

(a) Portions of the following licensee perfomed surveys

were observed for confomance with BVPS Radcon Manual

requirements:

Survey of Blender Cubicle High Radiation Area

--

in the Primary Auxiliary Building (discussed

further in paragraph 3.i(3).

Survey conducted during Type C local leak rate

--

test on penetration 20 inside containment and the

Primary Auxiliary Building on January 21, 1982.

--

Survey of Steam Generator Drain Tank Building during

decontamination efforts (discussed in paragraph 6.b).

Survey of Solid Waste Areas conducted as part of

--

TOP 82-07 and subsequent decontamination (discussed

furtherinparagraph6.d).

_

_

-

__

_

._

_.

.

.

33

(b) Radiation protection instruments below were inspected

during plant tours to verify operability and adherence

to calibration frequency requirements.

(c) The following Radiation Work Permits and Radiation

Access Control Permits were reviewed for completeness.

The permit (s) denoted by asterisk were reviewed in the

'

field to verify that the permit requirements were being

followed:

RWP B009351, Repair Line on LW-TK-7B, January 19,

--

1982.

RWP B009359, Decontaminate Outside Area, January

--

19, 1982.

RWP B009133, Dewatering Demineralizers, January

--

8, 1982.

PACP 81-11-H, Inspection and Surveillance, January

--

14, 1982.

RWP B009122, Clean / Repair / Test Motor Operators,

--

January 1,1982 for SI-850A.

--

RWP B009299, Install Hydrogen Recombiner System

at735'S/G(Maint), January 14, 1982.

RWP B009501 Decon LW-P-1A8B Cubicle, February 4,

--

1982.

RWP B009501, Decon Solid Waste Area, February 8,

--

1982.

(d) The inspector audited the licensee's Jumper and Lifted

Lead controls on January 15 and 19,1982 in accordance

with BVPS OM Section 1.48.5 to ensure no conflicts with

Technical Specifications, that the licensee is actively

pursuing correction of conditions requiring the jumpers

or lifted leads, and that the installation and removal

were proper. The following sample was audited:

--

2021, Area Ventillation, to allow VS-C-1B1 to run

with V S-E-4B out-of-service, placed March 4,1978.

2122 and 2123, Gaseous Waste System, to disable

--

Alam A-2-1, placed February 3,1979.

2766, Miscellaneous Safety Related System, to disable

--

alam A6-51, placed October 12, 1981.

(e) The inspector witnessed selected portions of the below

radioactive releases to verify conformance with approved

procedures, that required release approvals have been

obtained, that required sampling was accomplished, and

that effluent release instrumentation was operable:

RWDA 01736, Steam Generator Drain Tank 7A, discharged

--

to Unit 2 Blowdown, observed February 1, 1982.

.

.

34

(f) The following records of liquid and gaseous radioactive

releases were also reviewed to assure that approvals

were obtained, sampling was accomplished,fand release

limits satisfied:

RWDA (Liquid) 1724, Steam Generator Drain Tank 7B,

--

December 20, 1981.

RWDA 1724, Steam Generator Drain Tank 7A, January

--

1, 1982.

RWDA 1727, Laundry, January 1,1982.

--

RWDA (Gaseous) 0560, Gas Decay Tank 1A, January

--

3, 1982.

RWDA 0559, Gas Decay Tank 1C, January 2, 1982.

--

RWDA 0553, Containment Purge, December 30, 1981,

--

(Reviewed by OSC meeting 136-81).

(g) The inspector observed solid radioactive waste disposal

activities to verify implementation of administrative

controls.

Spent resin transferred to lined waste cask for

--

offsite disposal on February 7 - 10, 1982.

(h) The inspector observed portions of on-going maintenance

activities to verify that:

These activities did not violate TS Limiting

--

Conditions of Operation.

Required administrative approvals and tagouts

--

were obtained prior to initiating work.

Approved procedures were being used or the

--

activity was within the " skills of the track."

c

QC reviewed the proposed work to define any desired

--

hold points.

Activities observed included:

Rebuilding Steam Dump Valve TCV-MS-106A6 per

--

(i) MWR 817918 for mechanical work, and

(ii) MWR 817917 for work on the valve actuator.

Instrument Calibration of Rod Area Monitor RM-215A

--

per MSP 43.08, Containment Particulate Calibration,

Revision 3, performed February 11, 1982.

_ _ _ _

_

_ _

__

-

-

---

35

e.

Findings

(1) Fire Barrier Penetrations Inoperable

Technical Specification 3.7.1.5 requires all penetration fire

barriers protecting safety related areas to be functional at

all times. The Action Statement of TS 3.7.15 requires that,

with penetration fire barrier nonfunctional, a continuous

fire watch must be established on at least one side of the

affected penetration within one hour.

During this inspection,

three examples of violation of TS 3.7.1.5 were identified.

(a)

TOP 82-6 (pection of temporary cable installations per

During ins

paragraph 6c, this report) the inspectors

found that the temporary 480 volt pcwer supply passed

through the wall between the AE and DF Vital Switchgear

Rooms via a standard conduit penetration. The fire

barrier packing for the penetration had apparently been

removed for the cable installation but not replaced. No

fire watch was present. The inspectors found the condition

at about 10:50 a.m. on January 28, imediately notified

the Control Room, and observed repacking of the pene-

tration with acceptable fire stop material at about

11:10 a.m.

Inspector discussions with the cognizant

Electrical Maintenance Foreman and review of operator

logs established that the cable had been run through the

penetration at or before 9:00 p.m. on January 27,

apparently without proper replacement of the fire stop

material or fire watch.

(b) During a February 5,1982 tour of the PAB Safeguards

Area, the inspectors found an 8" conduit penetration

  1. WCV-735'-111 between the West Cable Vault and the

Auxiliary Feedpump Room open and not stuffed with fire

retardant material. No fire watch was posted as required

by TS 3.7.15.

The inspectors imediately notified the

Nuclear Shift Supervisor and witnessed repacking of the

penetration with fire retardant batting.

(c) Additionally, the inspectors noted that similar finding

was documented in the Nuclear Shift Supervisor's log

for 8:25 p.m., February 5.

A Nuclear Shift Operating

Foreman on plant tour found welding cables passing through

a fire barrier penetration between the AE and DF Vital

Switchgear Rooms without fire retardant stuffing or a

fire watch.

The licensee was unable to establish the date and/or time

the penetrations of examples 2) and 3) were unpacked to make

them inoperable or whether fire watches had been posted at

any time during the inoperability.

Failure to comply with TS 3.7.15 constitutes a violation.

(82-01-09).

..

_

-

_-

. _ _

.

.

.

36

(2) Security Picture Badge Procedures

During a February 5, 1982 tour of the #1 and #2 Emergency

Diesel Generator Rooms, the inspectors observed two

construction workers not wearing their security picture

badges as required by the BVPS Physical Security Plan. The

individuals, inside the #1 EDG Room Vital Area, had left

the badges en their coats when the coats were removed. When

addressed by the inspectors, both individuals put the badges

on as required.

This matter was discussed with the DLC Security Supervisor

and Security Assistant on February 5-6.

Based on no recent

-

similar observations, the inspectors considered the above

apparent violation of security plan requirements to be an

isolated case and advised the licensee representatives that

any future observations of improperly displayed security

badges would be considered as violations. The licensee was

ensuring that construction craft workers were made aware of

the need to properly wear badges via contractor safety meetings

and communications. The inspectors noted that about 1000

construction contractor personnel are onsite to support the

current outage and that prior observations showed no widespread

abuse of badge requirements.

(3) High Radiation Barrier Unlocked

At 2:45 p.m., January 28, 1982, during a plant tour, the

inspectors found the radiation barrier door to the CVCS

blender cubicle unlocked and ajar about 8 inches. The

door is a fence-type gate properly posted as a High Radiation

Area and Contamination Area /RWP required for entry. The

inspectors immediately notified the cognizant Radcon Foremtn

who responded to the scene, insured no personnel were within

the cubicle, and relocked the gate.

The inspectors and licensee reviewed survey data, Radiation

Access Control Pemit logs, Radiation Work Permit Logs, Instru-

ment Issue Logs, and Radiation Area key logs, confiming that

only two parties had entered the area since it was last

verified locked at about 11:30 a.m., January 28. Neither of

the two parties (an operator and a housekeeping crew) recalled

finding or leaving the gate unlocked. The inspectors con-

fimed that both parties were properly authorized entry and

both were equipped with required radiation survey meters.

Survey data showed that general area radiation levels within

the cubicle were less than about 60 mrem /hr. except at and

below grating level. At grating level, localized fields were

about 100 mrem /hr; below grating level, maximum fields were

600 mrem /hr. or less.

'

.

_

-

_

.

. _ _

.

.

37

TS 6.12.1.a and BVPS Radcon Manual, Radcon Procedure 9.2,

Radiation Area Control

Issue 1, Revision 2, require entry

to high radiation areas of more than 100 mrem /hr. but less

than 1000 mrem /hr. be controlled via RWP and barricades.

Locked barricades are only required if the radiation intensity

is greater than 1000 mrem /hr. The licensee locks the lower

intensity cubicles to provide additional positive entry control

beyond that required by TS. Based on the above and the

isolated nature of this finding, no violation of NRC require-

ments was identified.

4.

In Office Review of Licensee Event Reports (LERs)

The inspector reviewed LERs submitted to the NRC:RI office to verify

that the details of the event were clearly reported, including the

accuracy of the description of cause and adequacy of corrective actions.

The inspector determined whether further information was required from

the licensee, whether generic implications were indicated, and whether

the event warranted onsite followup. The following LERs were reviewed:

  • --

LER 81-103/03L

Over Current Trip of IDF Emergency Bus due

to ground from 1C Component Cooling Water

Pump Motor.

LER 81-104/03L

Loss of Core Cooling Monitor due to power

--

supply failure.

LER 81-105/03L

Hydrogen Recombiner Pre-heater discharge air

--

temperature failed surveillance test.

LER 81-106/03L

Drift of 7 Main Steam Safety Valve Setpoints.

--

LER 82-01/03L

Supplementary Leak Collection and Release

--

System Train A failed surveillance test.

No unacceptable conditions were identified.

LER 81-103/03L was submitted by the licensee after the 1C Component

Cooling Water Pump Motor Bearings overheated and caught fire. A

resulting electrical ground caused an over current trip of the IDF

emergency bus.

Prior onsite inspector followup of this event is dis-

cussed in NRC Inspection Report No. 50-334/81-31.

LER 81-106/03L was submitted by the licensee after 7 of 15 Main Steam

Safety Valves experienced setpoint drift. Prior onsite inspector

followup of this event is discussed in NRC Inspection Report No.

50-334/81-31.

Denotes those reports selected for onsite followup as discussed belcw.

.

.

38

5.

Immediate Action Letter Followup - Operation With RCS Partially Drained

References:

--

(1)

Imediate Action Letter (IAL) 81-14, March 9,1981.

(2) Duquesne Light Company letter to the Nuclear Regulatory

Commission, January 6, 1982.

(3) Nuclear Regulatory Commission, Region I, letter to Duquesne

Light Company, January 8, 1982.

In March,1981, while the RCS was partially drained to mid-loop level,

inaccurate level indication and Residual Heat Removal Pump air binding

resulted in a partial loss of core flow. Licensee commitments to ensure

adequate Residual Heat Removal (RHR) system capability while in partially

drained conditions were documented in IAL 81-14.

Proposed changes to

those commitments based on a licensee evaluation of the event were

forwarded to the NRC in reference (2) for review and concurrence.

Clarifications of those comitments are contained in reference (3).

The licensee proposal and clarifications included redundant remote

level indications in the Control Room, requirements for instrument

checkout and periodic verification, data logging and parameter limits,

and actions for abnonnal conditions. On January 8 and 11 the inspector

reviewed implementation of the licensee commitments after the RCS had

been partially drained.

Operating Manual Change Notice (OMCN) issued

to support those commitments and reviewed by the inspector were:

OMCN 82-04 to BVPS OM Section 1.6.4 issued, January 7,1982.

OMCN 82-09 to BVPS OM Section 1.10.4, issued January 8, 1982.

OMCN 82-08 to BVPS OM Section 1.10.4, issued January 8, 1982.

OMCN 82-10 to BVPS OM Section 1.10.4, issued January 8,1982.

OMCN 82-05 to BVPS OM Section 1.10.4, issued January 8, 1982.

OMCN 82-06 to BVPS OM Section 1.10.4, issued January 8, 1982.

OMCN 82-07 to BVPS OM Section 1.54.3, issued January 8,1982.

The inspector also observed control board system alignments and

indications, held discussions with operations personnel, and

reviewed data to confirm licensee compliance with their commitments.

These items will receive continued review by the inspector during

routine inspection activities.

6.

Onsite Event Followup

a.

Automatic Actuation of Safety Injection System

A safety injection signal inadvertently actuated at 5:07

.m.,

January 4, 1982. MaintenanceSurveillanceProcedure(MSP 1.04,

Solid State Protection System, Train "A," Revision 16, was being

used as a guide to return the Solid State Protection System to

l

-

.

.

39

normal after replacing a fuse (replaced MB0-15 fuse with Buss-

man ABC-15 as specified by EM 41393) per MWR 800775. The safety

injection signal resulted from resetting the system out cf the

sequence specified in MSP 1.04.

Duringtheincident,thereactorwasinColdShutdown(Mode 5)

with two Reactor Coolant Pumps (RCP) and two Residual Heat Removal

(RHR) loops in operation. No actual water injection into the

Reactor Coolant System occurred due to Mode 5 (Cold Shutdown)

system lineups (pumps in pull-to-lock). However, the signal did

isolate the charging pump makeup flow path and the RCPs' No.1

Seal leakoff path (Containment Isolation Phase A). The two operating

RCPs were tripped to prevent possible damage, leaving the two

Residual Heat Removal loops in operation, meeting Technical Speci-

fication requirements (one loop in operation, and one lcop operable

in Moh 5). After the Safety Injection signal was confirmed to be

spurious, normal system alignments were reestablished.

The inspector discussed corrective actions taken by the licensee

with the Instrument and Control Supervisor. Actions taken included

revising MSP 1.04 for clarity and discussion of the event and the

importance of adhering to procedures during a safety meeting with

all Meter and Control Repainnen. The inspector had no further

questions on this item.

b.

Liquid Radwaste Piping Rupture

On January 19, 1982, about 3:30 a.m., water was observed leaking

down an exterior wall of the Steam Generator Drain Tank Building.

A recirculation line between Steam Generator Drain Tanks (LW-TK-

7A & -78) had ruptured, spilling about 300-500 gallons of water

on the roof, walls, and ground around the building. The line was

immediately isolated and the spillage stopped. Survey results

indicated maximum contamination in the surrounding earth of about

12,000 cpm as measured by an RM14/HP210 frisker. Liquid activity

from takn and spilled water samples was about 6E-5 uCi/cc. Most of

the spilled water had frozen on the walls and earth due to extremely

cold weather. The snow and ice surrounding the tank was drumed

and disposed of as liquid radwaste.

Post decontamination surveys

showed no contamination above the licensee's adninistrative limits

(450 uuCi/100 .m+2).

The line apparently ruptured due to freezing. The inspector observed

the failed line and portions of repair activities per MWR 820164.

The cause of freezing appears to be deficient temporary electric

.

heat tracing and damaged piping insulation, both of which were

also repaired.

.

40

J

The inspector became aware of the event about 8:00 a.m.

January

19, during a routine log review.

10CFR50.72, Notification of

Significant Events, requires prompt telephone notification to

NRC of any accidental radioactive release within one hour of

occurrence. The inspector reviewed this event relative to

10CFR50.72 and the licensee's reporting procedures of BVPS OM

Section 1.48.9.D.

At the time of discovery, the area affected

by the spill was apparently well defined in the snow around the

tank.

Discussions with licensee witnesses confimed that no

spillage to stonn drains was observed (abo iater confirmed by

sample) . The onduty Shift Supervisor considered the event to be

a " spill" rather than a " release" based on the absence of a path-

way to the environment. This appears appropriate based on the

BVPS FSAR which defines the restricted area (in the context of

10CFR20) as the company owned property at the Beaver Valley and

Shippingport sites.

The inspector questioned whether the absence of a release had

actually been confirmed within the one hour reporting time of

10CFR50.72. While not actually confimed by sample, the inspector

concluded that the licensee's assessment was reasonable. The

inspector, however, advised the Station Superintendent that a

notification to NRC per 10CFR50.72 would have been prudent based

en the circumstances. The Station Superintendent acknowledged

the inspector's concern and, on February 2,1982, issued Memo

NDlSSl:482 to Operations Department Supervisors emphasizing the need

for both internal (DLC) and external (NRC and other) notifications

for potentially reportable or sensitive matters.

The inspectors had no further questions on this matter; no

unacceptable conditions were identified.

c.

4160 VAC Cable Failure and Partial Loss of Offsite Power

While in Cold Shutdown, a 4160 VAC feeder cable failed at 2:15 p.m.,

January 27, 1982, resulting in arcing and smoldering insulation in

a switchgear room cable tray, and caused loss of 4160 VAC supply

to two of four (the A" and "B") main electrical busses and the

"A" Train (lAE) Emergency Bus. The "A" Train Emergency Diesel

Generator (EDG) is out-of-service for modification. The smoldering

insulation was immediately extinguished with portable equipment.

The "B" Train busses and EDG remained operable throughout the

event. The Reactor Coolant System (RCS) was partially drained.

_

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41

"B" Train safety systems were aligned for " priority train service"

and remained operable. The inspector confimed that Technical

Specifications for boration flowpath, onsite and offsite electrical

systems, residual heat removal, and reactivity control systems

were satisfied, including Action Statements as applicable. Power

was lost to the standby Residual Heat Removal (RHR) loop, RH_R

flow control valves, temporary Reactor Coolant System Level Instru-

ments, and miscellaneous instrumentation and controls.

Core flow

and level were maintained using local control and monitoring. The

cable fire, in the Service Building switchgear room, did nr

avolve

radiation or contamination.

Power was partially restored (to 480 VAC busses) via a temporary

cable about 9:15 p.m., January 27, restoring most of the instru-

ment and control functions. The "A" 4160 VAC Bus was reenergized

by a second temporary cable connection about 4:00 a.m., January

28.

Inspector review of the temporary cable connections is further

discussed below.

On January 28, the inspectors reviewed the sequence of events,

inspected the damaged cable trays, and reviewed the licensee's

response to the event. At the time of the incident, the "A"

and

"B" 4160 VAC busses were being powered via backfeed from the Main

Transformer through the 1C Unit Station Service (USS) Transfomers.

The fault, apparently a phase-to-phase short, occurred in the feeder

cables between the 1C USS Transformer and the "A" 4160 VAC Bus.

Inspector review of Sequence of Events computer printouts and

discussions with onduty operators established that the electrical

fault protection equipment operated as designed. The operators

properly responded to the event in accordance with the Abnormal

Procedures of the BVPS Operating Manual, Sections 1.36-1.39.

Power was lost to RHR flow control valves and temporary RCS level

to manually adjust RHR flow if needed (y dispatched to containment

instruments. Operators were immediatel

valves failed as-is) and

to monitor the local RCS level standpipe. Both temporary RCS

level instruments were powered from the "A/AE" busses via Instru-

ment Bus 3 and were deenergized. The instruments use Channel 3

Steam Generator level transmitters circuitry, temporarily repiped

to indicate RCS loop level. The Channel 3 instruments, powered

from the same Instrument Bus, were selected because they are the

only channels equipped with Control Rod recorders. The

inspectors confirmed that both RCS level and flow were properly

controlled and monitored through the event.

On the evening of January 27, 1982 the licensee issued and im-

plemented two Temporary Operating Procedures (TOPS) to provide

temporary power supplies to the "A" Train electrical busses.

TOP 82-5, Temporary Supply of Power to MCCl-E9, provided for

temporary cross connection of the 480 VAC emergency busses.

TOP 82-6, 4160 VAC Temporary Station Service Supply to AE

Emergency Bus, provided a similar cross connection for the 1A

4160 VAC bus. On January 28, the inspectors walked down each of

the installations to verify their confomance with the requirements

of the TOPS and good installation practice. The inspectors found

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42

that the temporary cables were of the specified size, properly

supported, and routed to avoid jeopardizing safety-related cables

in adjacent conduit and cable trays.

The inspector noted, however, that the temporary 480 volt power

supply passed through the wall between the 1 AE and 1 DF Vital

Switchgear Rooms via a standard conduit penetration. The fire

barrier packing for the penetration had apparently been removed

for the cable installation but not replaced. The matter is further

discussed in paragraph 3e(1) of this report.

On January 28, 1982, the inspectors discussed the licensee's safety

evaluation for the two TOPS with the DLC Chief Engineer, confirming

that conson mode failures, cable separation, and circuit protec-

tion were properly addressed by the procedures and the Onsite

Safety Committee's (OSC) review. On February 4, 1982, the

inspectors reviewed the draft safety evaluation included in the

draft OSC Meeting Minutes BV-0SC-5-82. The inspectors had no

further questions on this matter.

At the close of this inspection, temporary cables continued to

supply the "A" 4160 VAC normal and emergency busses. The 480

VAC temporary cross connect remained installed but deenergized.

Preparations for repair of the failed 4160 VAC cable were in

progress.

On January 27, 28, and 30, the inspectors observed the failed

cables and damaged cable trays.

Two cables appeared to be the source

of the failure (phase to phase and/or phase to ground). The cables

failed about midway between wooden supports and did not appear

to be in contact with each other at the point of failure.

Failure damage included evidence of heavy arcing with burnt cable

insulation and melted cable shield and conductors on both cables.

Evidence of arcing from the cables to the tray was also observed.

The cables are located in a horizontal covered tray about 20 feet

above floor level in the Service Building switchgear room. To the

extent permitted by the damage, the inspectors observed no

evidence of pre-failure damage or tampering. On February 2, 1982,

the licensee issued Engineering Memoranda (EM) 44398 and 20928

for repair of the damaged cables and 1C transformer respectively.

EM 44398 also provided for analysis of the failed cable by the

cable vendoc. At the close of this inspection the failure causes

for the cable and the potential for similar failures of other

cable had not been established, pending vendor analysis. This

matter will remain unresolved pending review of the licensee's

l

actions.

(82-01-10).

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d.

Spent Resin Spill

Approximately 1/2 gallon of spent resin was spilled in the Solid

Waste Area on February 5,1982. No personnel internal or external

contamination or offsite release occurred.

Temporary Operating Procedure (T0P) 82-07 Resin Removal and Trans-

fer of CH-I-1A, -1B, and -38, was in progress at the time of the

spill. The procedure involved 'he transfer of spent resin in slurry

form from the ion exchangers to a shipping line within a cask atop

a flatbed truck for offsite disposal.

Through discussions with licensee personnel, the inspectors deter-

mined that the spill occurred after the initial transfer was

essentially complete.

Involved personnel interviewed by the

inspectors stated that when the transfer pump reached shutoff

head due to backpressure from the full line, a residual amount

of resin remained in the transfer hose coupled to the liner. The

hose was disconnected and the residual resin drained into a poly

bag. The bag slipped out of the operator's hand, spilling resin

onto the outside of the cask, the bed, and tires. The inspector

reviewed TOP 82-07 and associated RWP 9516 package to evaluate the

licensee's preparations and preventive measures for coping with

possible spills. The inspector found the licensee preparations

generally acceptable including:

a confinement structure around

the SWA door and trailer; radiation barriers and postings; sealing

of storm sewers; butiding of floor dikes; placement of spill kits;

temporary ventilation and radiation monitors; and radtech coverage.

These efforts were successful in containing the actual spill until

decontamination was complete.

The inspector noted that TOP 81-07 did not provide guidance for

handling abnonnal conditions encountered during the transfer such

as unexpectedly high radiation levels or line plugging. Additional

improvements in the transfer rig such as isolation capability at

the cask end of the hose were also identified as desirable. The

DLC Radcon Supervisor acknowledged the inspectors'consnents and

stated that the procedure would be revised to include stop-work

provisions for abnormal conditions and transfer rig improvements

prior to its next use. These provisions would be included in the

licensee's programmatic procedures to ensure that they are con-

sidered for any similar evolution. This matter will remain un-

resolved ending NRC:RI review of the licensee's actions.

'

(82-01-11.

The inspector reviewed , pre- and post-spill survey and sample data.

Continuous air monitor samples varied from E-9 to E-10 uCi/m1,

,

and showed no increase of airborne activity above initial area

'

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44

background during the spill. Contact readings on the resin-filled

bag showed 15 R/hr.

Resin on the truck was reading approx-

imately 3-4 R/hr. at 6 inches, with a general area reading of

40-100 mR/H. Transfer and spill. response activities up to cask-

top decontamination and cask lid" installation resulted in personnel

exposures within the As Low As Re~asonably Achievable (ALARA) guide-

lines for RWP 9' 6.

Decontamination efforts perfomed under RWP

9501 (General Decontamination) were also accomplished with minimum

personnel dose.

When operations to seal the cask resumed, an additional written

ALARA review was not performed. Continuous health physics coverage

was, however, provided. The Radcon Foreman who surveyed the lid

area of the cask where some of the resin had spilled, was equipped

with two high range extremity dosimeters (one for each hand), a

low range dosimeter for whole body exposure control, and a TLD

badge. After assessing the situation, the foreman decided to per-

sonally complete the RWP 9516 work by manually cleaning the lid

sealing area of resin. The individual's low range pocket dosimeter

was periodically read during the work to control whole body exposure

and indicated a total exposure of 425 mrem. The individual's

thermoluminescent dosimeter (TLD), processed after the job showed

a total 1130 mrem whole body exposure for the calendar quarter,

900 mrem attributable to this activity. A calibration check of the

pocket dosimeter showed the instrument to be defective. The total

exposure for this individual is within the limits prescribed by

10CFR20, but did exceed the licensee's administrative guidelines

of 1000 mrem / quarter.

The high range dosimeters showed a total extremity dose of 4320

mrem gamma for the right hand and 3480 mrem gamma for the left

hand. These values were also within the 10CFR20 limits of 18 3/4

rcm per quarter.

The inspector discussed this event with Radcon Supervisor and

expressed his concet.' that work had been allowed to continue after

radiological conditions had substantially changed without parform-

ing an additional ALARA review. Though the Radiological Control

Manual Chapter 3 Radcon Procedure 8.1, Radiological Work Permit,

Revision 1, states that Radcon should initiate an ALARA review of

,

I

a dose of greater than 200 mR for an individual or 1000 mR for a

l

work party is expected, none is required. The inspector further

noted that Radcon Procedure 8.1 contains provisions for terminating

an RWP if warranted by changes in radiological status, as detemined

by Radcon personnel. The licensee acknowledged the inspector's

,

l

comments, stating that future jobs would be carefully monitored to

prevent recurrence.

'

,

The inspector observed portions a the decontamination of the

Solid Waste Area and cask truck, ,; ifying that radiological con-

l

trols were properly implemented.

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45

7.

Refueling Preparations - New Fuel Receipt

The inspector reviewed procedure NSQC 10.2, " Fuel Assembly and Shipping

Container Receipt Inspection," Revision 1, July 8,1980, to verify that

a technically adequate, approved procedure was used for the receipt,

inspection and storage of new fuel. No inadequacies were identified.

The inspector reviewed the Fuel Assembly Receiving and Inspection Reports

(NSQC 10.2, Attachment 6.1) for the 52 fuel assemblies received in

shipments DLCF-1 through DLCF-5, to verify that the receipt, inspection

and storage of the new fuel was accomplished in accordance with pro-

cedure NSQC 10.2.

No unacceptable conditions were identified by the

receipt inspectors. The inspector had no further questions in this area.

8.

IE Bulletin Followup

Licensee responses to IE Bulletins were inspected for timely submittal,

adequate corrective action, and dissemination to onsite management as

discussed below.

IE Bulletin 80-05:

Vacuum Condition Resulting in Damage to Chemical

and Volume Control System (CVCS) Holdup Tanks. The inspector reviewed

this bulletin and the licensee's response (DLC letter of June 16, 1980)

which adequately addressed the concerns to the bulletin for the Pressur-

izer Relief Tank, Primary Drains Transfer Tanks 1

and 2, Coolant

Recovery Tanks 4A and 4B, and the Volume Control Tank. The inspector

noted, however, that there were several other tanks which had not been

evaluated to detennine if they could be subjected to potentially dam-

aging vacuum conditions. The licensee agreed to extend the evaluation

to the tanks in question. The licensee's action in this regard will

be reviewed in a subsequent inspection.

IE Bulletin 80-18: Maintenance of Minimum Flow Through Centrifugal

Charging Pumps Following Secondary Side High Energy Line Rupture.

The inspector reviewed the licensee's response to this bulletin (DLC

letter of September 24,1980) and Emergency Operating Procedure E-0,

verifying that the bulletin had been received and evaluated, the

required modification made to prevent automatic closure of the coolant

charging pump (CCP) miniflow isolation valves on safety injection actua-

tion, and that emergency procedures had been modified to provide operator

guidance on opening and closing the CCP miniflow isolation valves. The

inspector had no further questions in this area.

IE Bulletin 80-23: Failure of Valves Manufactured by VALCOR Engineering

Corporation. The inspector reviewed the licensee's response to this

bulletin (DLC letter of December 15, 1980) which stated that no Valcon

solenoid valves were in use at Beaver Valley, Unit 1.

The inspector

reviewed the licensee's records documenting their review, consisting of:

.

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46

a memo itsting all safety-related solenoid valves and the manufacturers,

a memo of a phone contact with a Stone and Webster representative,

(Stone and Webster had been listed in the bulletin as receiving some of

the valves from Valcor), a memo of a phone contact with the W. J. Wooley,

Co. (airlock supplier), and a memo referencing a check of spare parts.

This documentation supports the licensee's conclusion that none of these

valves are used at the site. The inspector had no further questions in

this area.

9.

Review of TMI Action Plan Requirements

The inspector reviewed licensee implementation of TMI Action Plan Items

identified in NUREG 0737, Clarification of TMI Action Plan Requirements,

published November 1980, with respect to the licensee letters identified

below, the guidance of NUREG 0737, and other applicable documents as

referenced by NUREG 0737.

Item II.E.4.1, Dedicated Hydrogen Penetrations. The licensee's response

to NUREG 0378 guidance (DLC letter of January 26,1980), describes the

installation of the Hydrogen Recombiners at the site. A review of this

response, the licensee's FSAR Sections 6.5 and 14.3.4.4, and the BVPS

Operating Manual, Section 1.46, confimed that the licensee's installa-

tion meets the requirements of 10CFR50.44,10CFR50 General Design Criteria 54 and 56, and the NRR position as clarified in NUREG 0737, Item II.E.4.1.

Inspector walkdown of the penetration piping confimed the installation

to be as described by the licensee's submittals. The inspector had no

further questions in this area.

Item II.E.4.2.5a & b - Containment Isolation Dependability (Actuation

Setpoint). The licensee's submittal to NRC dated December 31, 1980

provided the bases for no reduction or modification to the containment

pressure setpoint for initiation of containment isolation. The submittal

discusses the facility's subatmospheric containment design and the con-

siderations for maintaining the existing setpoint. The inspector reviewed

BVPS Operating Manual Section 1.16 and 1.47, finding the infomation

contained in the letter to be consistent with existing system descrip-

tions and operating procedures. This item was reviewed by NRC:NRR and

found acceptable (NRC letter, Varga to Carey, dated December 11,1981).

Item II.E.4.2.7: Containment Purge and Vent Valves Close on High

Radiation. This requirement has been detemined not to be applicable

to Beaver Valley, Unit 1 because of the subatmospheric containment

design and was deleted by a letter from the NRC to the licensee dated

April 29,1981. Subatmospheric containment designs do not pemit open-

ing purge and exhaust valves except in Cold Shutdown or Refueling con-

ditions.

Containment purge and exhaust valves are equipped with high

radiation isolation signals for these conditions.

Containment vacuum

pump lines are separately equipped with isolation signals.

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47

10.

Emergency Preparedness Exercise - Personnel Accountability Drill.

On February 12, 1982 the inspectors witnessed portions of the licensee's

accountability drill, performed to meet the requirements of the BVPS

Emergency Preparedness Plan, Section 6.7.5 and NUREG 0654, Section J.

The drill was conducted separately from the full scale NRC/ FEMA drill

of February 17, 1982 to minimize the impact of the current outage on

both exercises. About 1000 additional non-DLC employees are currently

onsite for the refueling / modification outage and were not included in

the accountability drill.

Inspector drill observations were made from the Primary Assembly Area

(Men's Locker Room), the Control Room, the Central Alarm Station, and

the Nuclear Division administration building, with respect to:

--

EPP/ Implementing Procedure (IP) 7.2, Administration of EPP Drills

and Exercises, Issue 6, Revision 3;

EPP/IP 3.1.3, Administration Building Evacuation, Issue 6, Revision

--

4; and

EPP/IP 3.2, Personnel Accountability, Issue 6, Revision 4.

--

The drill was to include limited participation by BVPS Unit 2 con-

struction personnel (emergency / accountability coordinators).

Partici-

I

pation was less than expected due to a misunderstanding of drill

'

announcements and poor PA system performance. Unit 2 activities were

observed by the BVPS Unit 2 resident inspector.

The inspectors attended the licensee's post drill critique, confiming

thaj licensee observer findings were consistent with the inspectors'.

The licensee met the accountability goal of 30 minutes specified by

NUREG 0654. The inspectors' findings will be included in NRC:RI

Inspection Report 50-334/82-04 for the full scale emergency response

exercise.

11.

Containment Hydrogen Recombiner Design Deficiencies

On December 15, 1981, Rockwell International, manufacturer of the

BVPS-1 recombiners, notified NRC:HQ and the licensee of deficiencies

in recombiner heater lead wire insulation. The vendor's evaluation

concluded that nomal testing combined with actual post-LOCA operation

would result in failures after ten years in nomal service. The

BVPS-1 recombiners were delivered in 1974

The vendor will provide

the licensee instructions for correction of the deficiencies.

The inspector confirmed that the licensee had received the vendor's

notification and had initiated Station Modification Request (SMR) 543,

dated February 3,1982, to accomplish the vendor's recomendations.

The SMR notes that action must be completed prior to 1984. The

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1

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_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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48

inspector also confinned that the modification requirements had been

entered into the BVPS Commitment Action Control System, responsibility

assigned for completion, and a required completion date of December

30, 1983 established.

12.

Safety Injection Actuation Design

Because of a recent design error found at the Maine Yankee Nuclear

Pcwer Station which would have prevented actuation of the Safety

Injection System for certain single active components failures, the

inspector reviewed the design of the Westinghouse safeguards actuation

circuitry for BVPS-1 with the Westinghouse Site Representative. This

review verified that a similar design error does not exist in this

circuitry. The inspector had no further questions in this area.

13.

Review of NDE Techniques for Plant Modification Piping

On February 2-3, 1982, a region based inspector reviewed licensee and

licensee contractor actions taken in response to Schneider Power

Corporation Nonconformance Report (NCR) 288, regarding use of DLC Radio-

graphic Procedure RT2 for radiography of USAS/ ANSI B31.10 (1967) pipe

welds. Procedure RT2 has been used on examination of field pipe welds

used for safety realted modifications in progress at BVPS-1.

NCR 288, dated December 23, 1981, indicated that the determination of

sensitivity in B31.1 (which references ASME SCI) is different than that

required in RT2. The penetrameter requirements are more severe in B31.1.

The licensee conducted a series of radiographic tests utilizing the same

techniques used for the affected pipe welds on pipes of similar wall

thickness with the B31.1 and RT2 (SCIII) penetrameters. The inspector

reviewed the radiographs and Radiographic Interpretation Reports dated

January 27, 1982 for 6" x 0.432", 10" x 0.365", 3" x 0.360", 6" x 0.134",

and 6" x 0.240" tests. The radiographic techniques used are capable

of meeting the sensitivity levels required by both B31.1 and RT2. The

quality of the weld joints is therefore acceptable to B31.1. A review

of the assignment of allowable stresses in ASME SCIII and B31.1 indicates

that a higher allowable stress for SA106C is permitted in SCIII Table

J-1.1 (19.4 KSI 0 650 F) than is permitted for B31.1 (17.5 KSI O 650 F)

indicating further conservatism for B31.1 fabrication when compared with

SCIII.

(The higher allowable stress is permitted with the lower radio-

l

graphic sensitivity).

The inspector reviewed DLC Memo DLCQA-3459 dated January 29, 1982 on

,

the evaluation of the sample radiographs finding the licensee's evalua-

l

tion and actions acceptable.

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52

15.

Review of Periodic Reports

The inspector reviewed the BVPS Monthly Operating Reports for October-

December,1981 to verify that information required to be reported by

NRC requirements had been included. No inadequacies were identified.

16.

Unresolved Items

Unresolved items are matters about which more information is required

to determine whether they are acceptable, items of noncompliance or

deviations. Two unresolved items were identified and are discussed

in paragraphs 6.c and 6.d of this report.

17.

Exit Interview

Meetings were held with senior facility management periodically during

the course of this inspection to discuss the inspection scope and

findings. A summary of inspection findings was also provided to the

licensee at the conclusion of the report period.

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