ML20053E197

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IE Insp Rept 50-219/82-06 on 820317-0406.Noncompliance Noted:Failure to Submit Required LER & Failure to Implement Approved Procedures Properly
ML20053E197
Person / Time
Site: Oyster Creek
Issue date: 05/11/1982
From: Bettenhausen L, Pullani S, Rekito W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20053E187 List:
References
50-219-82-06, 50-219-82-6, NUDOCS 8206070688
Download: ML20053E197 (12)


See also: IR 05000219/1982006

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U.S. NUCLEAR REGULATORY COMMISSION

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OFFICE OF INSPECTION AND ENFORCEMENT

Region I

Report No.

50-219/82-06

Docket No.

50-219

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License No.

DPR-16

Priority

Category

C

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Licensee:

GPU Nuclear Corporation

P. O. Box 388

Forked River, New Jersey OS731

Facility Name:

Oyster Creek Nuclear Generating Station

Inspection at:

Forked River, New Jersey

,

Inspection conducted:

Marc

17-19, 31 and April 1, 2, 5, 6, 1982

Inspectiors:

C

d

W. A. Rekito Reactor Inspector

/ datg signed

L a-

s/n/n

S. V. -ftfilanf, Reactor Inspector

date signed

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date signed

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Approved by:

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L. H. ~8ettenhausen, Chief,

date signed

Test Program Section

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Inspection Summary:

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Inspection on March 17-19, 31 and Aoril 1, 2, 5, 6, 1982

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Areas Inspected:

Routine, unannounced inspection of licensee action on previous

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inspection findings; primary containment penetration leakage testing program;

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and witness of the primary containment integrated leakage rate test.

The

inspection involved 118 inspector-hours onsite by two region-based inspectors.

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Results:

Violations were identified in two areas:

(1)

Failure to make a required LER, (Paragraph 3.4) and

(2)

Failure to properly implement approved procedures (Paragraph 3.7,

3.8,4.6).

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DETAI_LS

1.

Persons Contacted

+M. Budaj, Manager, Saecial Projects

J. Carroll, Director Station Operations

P. Feidler, Vice President and Director

K. Fickeissen, Director, Plant Engineering

+S. Fuller, OPS QA Manager

K. Hutko, Test Engineer

+M. Laggart, Licensing Supervisor

  • +J. Molnar, Manager, Core Engineering

+T. Quintenz, Manager, Plant Engineer

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J. Sklar, Test Engineer

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+J. Sullivan Jr. , Plant Operations Director

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NRC Personnel

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+J. Thomas, Resident Inspector

+C. Cowgill, Senior Resident Inspector /

ottom)

The inspector also talked with and interviewed other licensee personnel

during the inspection.

They included members of the operating, technical,

and maintenance staffs.

  • denotes those present at the exit interview held March 19, 1982.

+ denotes those prescnt at the exit interview held April 6, 1982.

2.

Licensee Action on Previous Inspection Findings

(Closed) Unresolved Item (219/80-10-04):

Schedule for leakage rate

testing modifications. The licensee has planned and scheduled the

completion of applicable piping system modifications during the forthcoming

(1981) refueling outage. This schedule was committed to in a letter to

the NRC dated June 27, 1980. The NRC found this schedule for achieving

conformance with 10 CFR 50 Appendix J acceptable as documented in a

Safety Evaluation Report sent to the licensee on March 4,1982.

This

item is considered resolved.

(Closed) Unresolved Item (219/80-10-05):

Incomplete acceptance

criteria in the local leakage rate test procedure. On June 27, 1980

the licensee approved and implemented a special procedure 665.5.020,

Integrated Local Leak Rate Summary.

The inspector reviewed and verified

that this procedure included all applicable acceptance criteria, for

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local leak rate testing, from 10 CFR 50 Appendix J and the Technical

Specifications.

This item is resolved.

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(Closed) Unresolved Item (219/80-22-02): Maintaining electrical

penetrations pressurized with nitrogen.

The licensee had not conducted

the engineering evaluation to determine the applicable requirements

but stated that it would be done as priorities permit. During this

inspection the inspector examined a sampling of approximately 15

electrical penetrations and observed that all pressure indicators were

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reading above 10 psig.

Based on these observations and the licensee's

response to NRC Bulletin 77-06, which describe the need for a nitrogen

environment but no specific pressure, this item is closed.

(0 pen) Violatior[s (219/80-10-02, 81-05-10, 81-08-01) and Immediate

Action Letter 81-20:

Failure to meet Inservice Testing (IST) requirements

for safety related puips and valves.

The licensee is still not conducting

insarvice tests and evaluating results in accordance with Section XI

of ASME B&PV Code. A licensee letter to NRC dated March 18, 1982

describes the delay of implementing these test activities beyond the

previously committed schedule for achieving total compliance with the

regulations. The inspector stated that delay of the stated corrective

action plan would be considered during the Licensee Performance Appraisal

for the recent assessment period.

Followup on these items and review

of the implemented test program will be included in a subsequent

inspection.

3.

Local Leak Rate Testing

3.1 Documents Reviewed

-- Procedure 665.5.003, Revision 3, Main Steam Isolation Valve Leak

Rate Test

-- Procedure 665.5.004, Revision 0, Feedwater Isolation Valve Leak

Rate Test

Procedure 66.5.006, Revision 3, Local Leak Rate Testing

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-- Procedure 665.5.020, Revision 0, Integrated Local Leak Rate

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Summary

-- Special Procedure 82-038, Revision 0, dated March 26, 1982,

Feedwater Check Valve Leak Rate Test with Leaking Maintenance

Valve.

-- Procedure 665.5.003.1, Revision 0, dated April 4, 1982, Leak

Testing MSIV's in Series (NS03A and NSO4A) or (NS038 and NSO48)

-- Records of Local Leak Rate Testing (LLRT) activities conducted

during recenc outage including test results, related repair and

retest documentation.

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Summary Technical Report for Reactor Building Containment Building

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Integrated Leak Rate Test - 1980, submittad to the NRC October 7,

1980.

NRC letter to licensee dated, M$rch 4, 1982, transmitting a

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Safety Evaluation Report regarding compliance with 10 CFR 50

Appendix J, Containment Leakage Testing at Oyster Creek.

Selected system operating procedures and drawings (P & ids)

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3.2 Scope of Review

The inspector reviewed the above documents to ascertain compliance

with regulatory requirements of 10 CFR 50 Appendix J and Oyster

Creek Technical Specifications..

The inspector also witnessed

selected LLRT activities and held discussions regarding the

relationship between LLRT failure results and the Primary Containment

Integrated Leak Rate Test (PCILRT) evaluation of "AS FOUND"

condition.

Further details and inspection findings are described

below.

3.3 Test Results

The inspector reviewed the LLRT Results Summary and discussed

analysis of test failures and status of test results with the

licensee.

Several significant problems were encountered. The

initial tests of two penetrations (Main Steam line A and Main

Steam drain to Condenser Hotvell) resulted in unacceptable leakage

past both redundant boundaries. The inspector explianed that the

overall primary containment system leakage improvements resulting

from repairs of these penetrations and others prior to the PCILRT

are expected to be added to the results of the PCILRT for determination

of the "AS IS" test result in accordance with 10 CFR 50 Appendix

J.

This requirement was acknowledged by the licensee. Preliminary

evalautions of LLRT results for this purpose appeared to be

adequate.

3.4 Reportability

The licensee submitted event reports (82-19 and 82-20) identifying

abnormal degradation of the primary containment for the two

penetrations with unacceptable leakage past both boundaries.

The

inspector inquired about li.ensee intentions to report other

valves with LLRT results exceeding their allowable TS limit of

11.9 SCFH necessitating repairs to reduce leakage.

In accordance

with Procedure 104, Control cf Nonconformances and Corrective

Action, the test engineer submitted a Deviation Report on February

26, 1982 identifying twelve Containment Isolation Valves whicn

were found to exceed their TS allowable leakage. This report was

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later evaluated by the Department Manager, Plant Operations

Manager, Safety Review Manager and Manager of Operations who

concluded that the occurance would be reported as part of the

PCILRT Technical Summary Report and not as an LER.

The inspector

acknowledged the need for this information in the Technical

Summary Report but stated that operation with unacceptable LLRT

results represented a reportable occurence as identified in

Regulatory Guide 1.16 paragraph C.2.a(2)(c).

The inspector

further explained that the intent of this requirement, during

outage periods when containment isolation is not required, could

be satisfied by an initial notification with a single LER supplement

following ccmpletion of all LLRT(s).

In addition to the recent LLRT failuras the inspector reviewed

the results of the LLRT program from the 1980 Refueling Outage

and determined that the LLRT failures were not properly reported.

Failure to submit an LER for containment isolation leak rate test

failures from the recent outage and the 1980 Refueling Outage

constitutes a violation of TS 6.9.2, Reportable Occurrences.

(219/82-06-01).

3.5 Test Witnessing

On March 18, 1982, the inspector witnessed a LLRT of Containment

Isolation Valves V-22-28 nd V-22-29.

The test was conducted in

accordance with approved procedure 665.5.006, following maintenance

performed to reduce leakage on valve V-22-29.

The results of the

test were unacceptable in that the test volume could not be

pressurized beyond 27 psig with the capacity of the test equipment.

The valve was again disassembled and disc-seating surface repaired.

A subsequent LLRT was found to be acceptable.

The inspector verified that the tests were cenducted in accordance

with the approvcd procedures and that the related maintenance and

work permit documentation was in accordance with the applicable

procedural requirements.

Additionally, the inspector observed

that the tcst instruments were properly calibrated and the test

personnel appeared to be suitably trained in their use.

No

unacceptable conditions were identified.

3.6 Feedwater Check Valve Testing

The licensee attempted to test all four feedwater check valves

with air.

However, excessive water leakage past the manual

isolation valve on the "A"

line prohibited a LLRT with air on

valve V-2-73. As an alternative, the licensee prepared Special

Procedure 82-038 and conducted a hydraulic leakage test on this

valve resulting in 0.

gpm leakage.

Additionally the outboard

valve (V-2-71) was tested with air and resulted in excessive

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leakage of 85 SCFH. The licensee evaluated this result and concluded

that the excessive leakage was not representative of the valve's

leak tightness due to use of the valve seat drain connection for

the test pressurization connection.

Based on the results of the water test conducted on redundant

valve V-2-73 and the previous commitment to perform necessary

piping modifications to achieve total conformance with 10 CFR 50

Appendix J during the next refueling outage, the condition was

considered acceptable.

3.7 Main Steam Isolation Valve Tests

Due to the method of testing inboard isolation valves, step 8.1.2

of Procedure 665.5.003 requires that the leak rate measured for

the outboard MSIV be added to the measured inboard valve leakage

to obtain a conservative value.

Likewise, the leak rate measured

for drain valves V-1-110 and V-1-111 must be added to the leak

rate measured for valves V-1-106 and V-1-107.

Review of LLRT

records (Data Sheets) revealed that this procedural calculation

requirement was not adhered to on three occasions:

February 28, 1982 - NS03B (IB MSIV) leakage reported as zero

while NSO4B (OB MSIV) reported as 11.49 SCFH

March 17, 1982

- Valves V-1-106, V-1-107 leakage reported

as zero while V-1-110, V-1-111 reported as

gross (could not measure.)

March 28, 1982

- NS03 A (IB MSIV) leakage reported as zero

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while NS04A (OB MSIV) reported as 22.9 SCFH.

During discussions with the responsible test engineers, they

stated that they were not aware of the procedural calculation

requirement and overlooked it.

As corrective action the ifcensee prepared a special procedure

665.5.003.1, Leak Testing MSIV's in Series (NS03A and NS04A) or

(N503B and NSO4B). On April 5, 1982 a satisfactory test was

performed on NS03A and NSO4A with a combined leakage of 4.57

SCFH. As of April 6,1982 the licensee had not yet corrected the

unacceptable test results of V-1-106, V-1-107 from March 17,

1982.

Improper calcula+. ion of test results on the occasions noted

represent an apparent failure to properly implemcnt approved

procedures. This example, along with the ones described in

paragraph 3.8, and 4.6 constitutes a violation of Technical Specification 6.8.1.

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3.8 Corrective Action for Test Failures

On March 28, 1982 MSIV-NSO4A was LLR tested, resulting in unacceptable

leakage of 22.9 SCFH. After recognizing some stem packing leakage,

the test engineer obtained maintenance personnel assistance to

tighten the packing. An immediate subsequent LLRT resulted in

acceptable leakage of 0.7158 SCFH.

procedure 105, Conduct of Maintenance, Section 4.1, states that

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all observed instances of failures, malfunctions, equipment

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deficiencies and deviations from acceptable performance which

require maintenance to correct shall be identified and documented

on a job order form which is used to initiate, track and document

maintenance activities performed by Oyster Creek personnel.

On March 28, when NSO4A failed, the LLRT and the packing was

tightened and no maintenance job order form was initiated. As of

April 6, 1982 the licensee could not provide the dccumented form.

During discussions with the responsible test engineer, he stated

that at the time of the occurrence he felt that a maintenance job

order form was not required to document the tightening of valve

packing.

Improper conduct of maintenance without required documentation on

this occasion represents failure to properly implement approved

procedures.

This example,-along with examples described in

parcgraph 3.7 and 4.6, constitute a violation of Technical Specification 6.8.1.

4.

Primary _ Containment Intearated Leak Rate Test (PCILRT)

4.1 General

On March 30 through April 4,1982, Oyster Creek Nuclear Generating

Station performed a PCILRT as required by TS 4.5.D.

The test was

performed in accordance with Procedure 666.5.007, Revision 5,

dated July 29, 1981.

The inspector reviewed the test procedure,

witnessed preparations and various portions of the test.

Further

details and inspection findings are described below.

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4.2 Procedure Review

The inspector reviewed the PCILRT Procedure along with the documects

listed in paragraph 3.1 for technical adequacy and to ascertain

compliance with Technical Specifications and commitments for

compliance with 10 CFR 50, Appendix J.

The inspector also discussed

various aspects of the PCILRT with the licensee's representative,

including guidance asailable in industry standard ANSI /ANS 56.8-

1981. With the exception of the item described below the inspector

identified no unacceptable conditions.

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Section 5.9.3 of the procedure provides an equation for correcting

the calculated leakage rate for liquid volume changes in the

containment.

The inspector identified an error and questioned

the validity of this equation.

The licensee agreed that the

equation was in error and committed to correcting it prior to

calculating the final official leak rate.

Recognizing that this

correction would have a very minor effect on the test results,

the inspector considered the licensee's committment acceptable.

However, the matter is unresolved pending NRC review of the

licensee's corrective action.

(219/82-06-02)

4.3 Instrumentation

The inspector reviewed the calibration records for resistance

temperature detectors, dewpoint instrumencs, pressure detectors

and verification test flowmeters. Their calibration prior to the

PCILRT were found to meet applicable accuracy requirements and

were traceable to the National Bureau of Standards.

The inspector

also verified that the instrument system specified in the test

procedure satisfied the instrument selection guide of ANSI /ANS

56.8-1981.

The inspector observed operation of the automatic

data collection system during conduct of the test.

The inspector

had no further questions regarding instrumentation.

4.4

Inspection Tours

The inspector conducted inspection tours independently and with

licensee personnel both before and during the PCILRT. During

these tours, test boundaries were surveyed for evidence of leakage

and, on a sampling basis, selected valves were verified to be in

correct positions according to procedure requirements.

During these tours no significant leakage was identified. However,

on April 2, 1982 the station air system inside the Reactor Building

was found to be pressurized.

This system was used as the test

pressurization source. After the start of the test, it had been

isolated and vented to prevent any possible air addition to the

containment past test boundary valves V-6-135 and V-6-136.

Subsequent to this, at approximately 4:00 am, the system vent was

closed with tne belief that the system would remain depressurized.

At approximately 1:30 pm, the sytem was again depressurized

(vented). After evaluation of the test data trending, the licensee

concluded that having the service air system pressurized during

this short time period had no measurable effect on the test

results. This event was documented in the test Abnormal Event

log.

The licensee stated that prior to the next PCILRT this

system would be modified to provide local isolation and venting

of that penetration.

No violations were identified as a result

of this problem.

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4.5 PCILRT Chronology

March 30


Completed the drywell inspection

March 30

1945

Commenced pressurizing the containment

March 31

Experienced problems with the drywell


recirculation fan motors drawing high

amperage and breakers tripping.

0430

Performed LLRT on drywell airlock which

revealed outer door leakage.

0615

Commenced depressurizing the containment

due to problems with drywell recirculation

fans

1430

Ccmpleted depressurization of the containment

Containment entry made and drywell


recirculation fans re-adjusted to lowest

speed setting.

April 1

0315

Commenced pressurizing the containment

again

1300

Completed pressurization at test pressure

(Pt) of 37.37 psia

1630

Began temperature stabilization period


Conducted leak surveys

2200

Temperature stabilization Complete.

Started 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> test period data collection

April 2


Continued inspections for leaks and

test data collection

0130

Dewcell instruments appeared to be

unstable. Approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> later

returned to normal stable condition

1200

Prelimary calculations indicate leak

rate will be acceptable

1800

Radiological problems discovered in

Reactor Building

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2225

Completed 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> test period data

collection

2255

Commenced 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> verification test with

an indicated leakage rate of 3.95 SCFM

April 3

0530

Dewcell readings unstable again and

test to be continued

1740

Completed the verification test and

commenced depressurization of the containment

4.6 Conduct of Test and Procedural Control

During performance of the test, the inspector identified several

concerns regarding adherence to the test procedure and proper

procedural control as described below.

Step 7.3 of the test procedure requires completion of the test

valve lineup verification (checkoff sheets) and step 7.3.16

requires verification that instrument racks are aligned per

Procedure 410, Placing Instrument Racks RK-01, 2, 3 and 4 in

Service. On March 31, the inspector identified that valve V-38-

1021 had not been verified to be open on the valve checkoff sheet

and the normal instrument alignment verification per Procedure

410 had not been started even though the test pressurization had

started the previous day, March 30.

The licensee responded to this by immediately verifying valve V-

38-1021 open and initiating a sampling verification of instrument

alignment.

Later, the licensee conducted an alignment verification

for all containment instrumentation per Procedure 410. This was

completed on April 5, with no discrepancies noted.

Section 4.9 of the test procedure requires that personnel performing

the test shall sign the cover page to document that the precautions

have been read and understood. On March 31, the inspector identified

that no personnel had as yet signed the cover page although test

pressurization started on March 30.

The test director explained

that further training of personnel would be done later that day.

On April 1, the inspector noted that test engineers had satisfied

this requirement.

On April 5, the inspector noted that the

operations staff supporting the test had also signed the cover

page.

Section 4.2 of the test procedure requires that the control room

operator log the reactor vessel flange temperature hourly during

the test. On April 2, the inspector noted that the day shift

reactor operator was not logging the flange temperature as required

and was not aware of the procedural requirement to do so.

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Procedure 107, Procedure Control, requires that " Temporary Change"

revisions to procedures be documented on a Station Controlled

Distribution Document Request (Form 103-1) and that the GSS/GOS

will ensure that this form is completed when he approves the

revision. On March 31 the inspector noted that four " Temporary

Change" revisions had been executed in the working copy of Test

Procedure 666.5.007 on March 28, 29, and 30 without being documented

on Form 103-1.

The test director responded to this by documenting

these revisions on the required Forms 103-1.

Procedure 107, Procedure Control, and TS 6.8.3 permit " Temporary

Change" revisions to procedures provided they do not change the

intent of the original procedure. The inspector questioned the

justification for one " Temporary Change" revision which deleted

the requirement to vent the Instrument Air System Piping inside

the drywell and, as such, changed the scope of the test boundaries,

the intent of the test procedure, and possibly violated the

requirements of 10 CFR 50 Appendix J.

The licensee later determined

that the initial " Temporary Change" revision was not justified

and that the system was required to be vented. On April 5 a

" Temporary Change" revision was executed to delete the original

" Temporary Change" revision.

In addition, the licensee documented

this system alignment error in the test Abnormal Events Log. The

licensee plans to correct (adjust) the results of the PCILRT by

adding the results of a LLRT for the Instrument Air System

penetration which was incorrectly omitted from the boundaries of

the test.

The inspector considered the corrective action acceptab'.e.

At the end of the test the inspector noted that a total of twelve

" Temporary Change" revisions were executed.

The inspector commented

that this appeared to be excessive, not in agreement with the

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intent of Procedure 107, and that most could have been handled by

the normal review and approval cycle prior to the start of the

test.

The specific problems identified above represent an apparent

failure to properly ir:1cment approved procedures. These examples,

along with the ones described in paragraph 3.7 and 3.8, collectively

constitute a violation of Technical Specification 6.8.1 and

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6.S.3. (219/82-06-03).

4.7 PCILRT Results

The licensee evaluated the test results for the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period

starting at 22:25 hours on April 1 and ending 22:25 hours on

April 2, 1982.

The calculated leakage rate at the 95% upper

confidence level was 0.273 weignt reccent per day.

The test

acceptance criterion is 0.375 weight percent per day.

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The inspector noted that the above calculated leakage rate of

0.273 is not corrected for the change in containment free volume

due to water accumulation in the sump or addition of LLRT results

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for the Instrument Air System penetration. Additionally, this

value represents the Conta; ament System "AS LEFT" overall leakage.

An evaluation of any leakage improvement resulting from repairs

performed prior to the PCILRT is needed to determine the Containment

System "AS FOUND" overall leakage.

Both values are expected to

be reported in the Technical Summary Report.

The inspector independentiv calculated several mass values and

the leakage rate, using raw data from the test. The results were

identical to and verified, the accuracy of the licensee's leak

rate calculations.

5.

Facility Tours

The inspector made several tours of the facility including the Reactor

Building and the Control Room.

During these tours, the inspector observed operations and activities

in progress, implementation of radiological controls, general condition

of safety related equipment, component tagging and system operations

to support the PCILRT.

6.

Unresolved Item

Items about which more information is required to determine acceptability

are considered unresolved.

Paragraph 4.2 contains an unresolved item.

7.

Exit Interview

The inspector met with licensee representatives (see detail 1 for

attendees) on March 19, 1982 and at the end of the inspection on April

6, 1982.

The inspector summarized the scope and findings of the

inspection at those times.

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