ML20050B035

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IE Insp Rept 50-387/82-04 on 820127-0301.Noncompliance Noted:Improper Incorporation of Test Requirements in Preoperational Tests & Inadequate Control of Environ Condition for Activities Affecting Quality
ML20050B035
Person / Time
Site: Susquehanna 
Issue date: 03/03/1982
From: Mccabe E, Mccann J, Pullani S, Rhoads G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20050B029 List:
References
50-387-82-04, 50-387-82-4, NUDOCS 8204020521
Download: ML20050B035 (19)


See also: IR 05000387/1982004

Text

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U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

Region I

Report No. 50-387/82-04

Docket No. 50-387

,

Category

B

License No. C_PPR-101

Priority

--

Licensee:

Pennsylvania Power and Licht Cornany

2 North Ninth Street

Allentown. Pennsylvania 18101

Facility Name: Susquehanna Steam Electric Station

Inspection at: Salem Township, Pennsylvania

Inspection conducted: January 27 - March 1,1982

Inspectors:

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Gary W. Rhoads

date signed

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John FV M

date signed

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    • '

S. V.-Pullani

date signed

Approved by:

DAM

3l3181

Ebe C. McCabe, Chief, Reactor Projects

date signed

Section 2B, DPRP

Inspection Summary:

Inspection on January 27 - March 1,1982 (Report No. 50-387/82-04)

Routine resident (208 hr.) and regional inspection (48 hr.) of: Startup Test Program,

Startup Procedures Review; Preoperational Testing; Preoperational Implementation;

Bulletins and Circulars, Open Items; and Plant Status. Thirteen open items, four

bulletins, two circulars, and one Construction Deficiency Report were closed.

Five

violations were identified; two for improper incorporatica of test requirements in

preoperational tests, one for inadequate control of environmental condition for

activities affecting quality, and two for failure to follow approved procedures.

Six other items were opened during this inspection.

Region I Form 12

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(Rev. April 77)

0204020521 820315

PDR ADOCK 05000387

G

PDR

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DETAILS

1.

Persons Contacted

Pennsylvania Power and Light Company

L. Adams, Plant Supervisor of Operations

T. Clymer, Site QAE

F. Eisenhuth, Senior Coapliance Engineer

E. Gorski, Plant Quality Supervisor

J. Green, Operations Quality Assurance Supervisor

H. Keiser, Superintendent of Plant

C. Myers, Assistant Superintendent of Plant - Outages

R. Sheranko, Startup and Test Group Super isor

D. Thompson, Assistant Superintendent of Plant

Bechtel Corporation

N. Covington, Assistant ISG Supervisor

E. Figard, ISG Supervisor

M. Johnson, ISG QC Engineer

The inspectors also interviewed other PP&L employees, as well as employees

of Bechtel.

2.

Licensee Action on NRC Findings:

a.

(Closed) Unresolved Item (387/80-14-01) Station Quality Certification

Records.

FSAR Table 17.2-1 has been revised to commit to Regulatory Guide 1.58,

Revision 1 which endorses ANSI Standard N45.2.6-1973.

Quality Control Pro-

cedure (QCP) 10, Revision 0 " Training, Qualification, and Certification of

Inspection and Test Personnel" was reviewed for incorporation of the re-

vised Regulatory Guide. The qualification requirements specified in the

procedure met the minimum qualifications as defined in the ANSI Standard.

b.

(Closed) Unresolved Item (387/80-20-08) Core Spray System Drawing in FSAR.

FSAR Figure 6.3-4, Revision 25 was reviewed. All discrepancies previously

identified had been corrected by this revision.

c.

(0 pen) Unresolved Item (387/80-10-01) Acceptance Criteria For Battery Loading.

FSAR Tables 8.3-6A, B, C, D, Revision 19 and Table 8.3-7, Revision 23 were

reviewed to determine if the tables had been updated to show the load cycles

for the 125 VDC and 250 VDC batteries during a LOCA condition. The tables

had been updated, but it now appears that the initial load plac2d on both

the Division 1 and II 250 VDC batteries during preoperational test P88.1

does not meet the load spectrum as shown on FSAR Table 8.3-7.

d.

(Closed) Inspector rollowup Item (387/80-28-02) Comments on Primary Contain-

ment Instrument Gas Test.

Work authorizations WA-U-11179, WA-U-11452, ar.d WA-U-11957 were reviewed.

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From the review it was detennined the remaining relief valve had been satis-

factorily bench tested.

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2.

e.

(Closed) Inspector Followup Item (387/79-08-06) Environmental Oualification

c f Stem Mounted Limited Switches.

The licensee has submitted their environmental qualification report to NRC:

NRR for review. NRC:NRR has stated in the Safety Evaluation Report, Supple-

ment 2 that after review they will review the program ard report on its finding

in a future supplement.

f.

(Closed) Inspector Followup Item (387/81-24-06) Conduct of Operations.

See paragraph 4 on Circular 81-02.

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JClosed) Unresolved Item (387/80-28-03) Remote Snutdown Panel Design.

Based on the inspector's concern identified in this item,NRC:NRR is per-

forming a review of the remote shutdown panel

and has requested the licensee

to make some changes to the panel.

h.

(Closed) Unresolved Item (387/81-02-10) Resolution of Document Review.

Memoranda documanting resolution of coments made by the Station Nuclear

Engineer were reviewed.

During NRC Inspection 81-29 the inspectors had

reviewed recent licensing submissions to the NRC, and had verified existing

procedures for document review is being followed.

i.

(0 pen) Inspector Followup Item (387/80-32-06) Control Rod Drive Hydraulics

Preoperational Test.

On February 4,1982 Preoperational Test P55.1, Revision 2 was reviewed to

ensure proper resolution to NRC inspector comments were incorporated into

the test.

Comments concerning discrepancies between as-built descriptions

of the scram discharge instrument volumes and the FSAR Revision 28 descrip-

tion have not resulted in a change to the FSAR.

Comments concerning drive

water pressure valves did result in a change to the FSAR Section 4.6.1.1.2.4.1,

but were not included in changes to FSAR Section 4.6.1.1.2.5.1.

These

comments will be reviewed in a subsequent inspection.

On February 4,1982, the official Test Copy of P55 .. Revision 2 was re-

viewed.

It was noted that Acceptance Criteria 2(11) stated that total

cooling water flow for control rod drives (CRD) shall be between 37 g.p.m.

and 63 gallons per minute (9.p.m.) and indicated this was verified in para-

graph 7.3.7 of the preoperational test. The step had been signed off as

being verified by the System Test Engineer on January 26, 1982.

Section 7.3.7

was reviewed.

The section did not verify total CRD flow as indicated in the

acceptance criteria, bu+ established flow at 63 ! 2 g.p.m. with no exact

indication of flow being documented for final established flow.

10 CFR 50, Appendix B, Criterion XI states that a test program shall be

established in accordance with written test procedures which incorporate

the acceptance limits contained in applicable design documents.

PP&L Quality Assurance Manual Procedure SP-3, Re'tision 2 states that the

preoperational test program shall consist of approved procedures which assure

data from the test is evaluated against the design requirements to determine

acceptability of test results.

3.

Startup Administrative Manual Precedure AD7.5, Revision 10, states that

acceptance criteria will specify either minimum or maximum values, or

tolerances and that the acceptance criteria will identify steps of the test

procedure that verifies the stated ' criteria.

On February 5,1982 the inspector informed the Superintendent of Plant that

listing minimum and maximum valu~es for total cooling water flow in the

acceptance criteria, but verifying total cooling water flow with tolerances

which put total cooling water fic i above the maximum value stated in the

acceptance criteria was a violat in.

(387/82-04-01)

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(Closed) Inspector Followup Item (387/80-24-04) Main Steam - Nuclear Steam

Sunply Shutdown System Preoperational Test Comments.

On February 17, 1982 Technical Procedure TP2.17, Revision 0, and Preopera-

tional Test P83.1A, Revision I were reviewed. All previous inspector comments

have been resolved by these two documents.

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(0 pen) Inspector Followup Item (387/80-01-04) Emergency Service Water Pipe

Interferences.

As of February 18, 1982 the Bechtel Quality Assurance Request (QAR-F584)

remained open requesting resolution of the inspector :omments.

1.

(Closed) Inspector Followup Item (387/80-32-05) Steam Relief Valve Acoustic

Monitoring Testing.

On February 18, 1982 Test Change Notice (TCN) numoer 016 to Preoperational

Test P83.1B, Revision 2 was reviewed.

This TCN incorporated testing for the

acoustic monitoring system for the steam relief valves.

(0 pen) Inspector Followup Item (387/80-32-07) Reactor Recirculation System

m.

Preoperational Test Comments.

On February 16, 1982 the inspector reviewed Preoperational Test P64.1,

Revision 3 and the FSAR Sections 7.7.1.3.3.4.7 and 7.6.la to determine if

all previous inspector comments had been resolved.

Two of the previous

comments dealing with FSAR changes had not been incorporated into revisions

to the FSAR.

These comments dealt with a description of the speed limiters

and the RPS breaker trip logic.

On February 17, 1982 two draft FSAR change

request forms were presented to the inspector which appeared to satisfy the

concerns.

This will be reviewed after L aroval of the draft change,

n.

(Closed) Inspector Followup Item (387/81-07-03) Control Rod Drive High Point

Vents.

On February 17, 1982 a PP&L internal letter PLI-13712 was reviewed.

This

letter stated the licensee's NPE group had evaluated the leaking vents and

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determined the problem encountered to be not reportable.

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(0 pen) Violation (387/80-16-03) Failure To Incoroorate Recirculation

System Flow Testing Into The Preonerational Test Precedure.

On February 18, 1982 Preoperational Test P64.1, Revision 3 was reviewed to

assure that integrated operation of the recirculation system motor generator

sets, recirculation pumps, jet pumps, and valves were incorporated in the

test.

PP&L internal letter, PLI-12299, was also reviewed requesting that

recirculation flows at greater than 45% pump speed be tested during the

startup phase. These changes appear to have fulfilled all immediate correc-

tive action to correct the Recirculation System Preoperational Test.

The licensee stated in its response to the NRC, PLA-559, that to avoid further

items of noncompliance the Test Revtew Board had been directed to insure

that FSAR requirements had been incorporated in the preoperational test.

This corrective step does not appear to have been sufficient since two items

of noncompliance in the present report period (387/82-04-01 ) and (387/82-04-

04) are partially due to FSAR requirements not being incorporated into Pre-

operational test. On February 19, 1982 the Superintendent of Plant was told

th1s item would be closed out based on further corrective action taken to

assure the Test Review Board is satisfying its responsibilities,

p.

(Closed) Inspector Followup Item (387/81-02-02) High Pressure Coolant In-

jection Preoperational Test Comments.

Preoperational lest PS2.1, Draft Revision 2, and FSAR Revision 19 were ob-

served. All inspector corments have been resolved.

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(0 pen) Inspector Followup Item (387 80-28-05) Temaorary Modifications In

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Containment Atmosphere Circulation System Durino

)reoperational Testing.

During NRC Inspection Report (387/80-28) in October, 1980 three Startup

Field Reports (SFR's) Numbers 1187, 1230, and 1531 were noted to be open

for resolution during preoperational testing of Containment Atmosphere

Circulation.

On February 18, 1982 the three SFR's were reviewed to determine if resolu-

tion to the identified problem could affect validity of the preoperaticnal

test. SFR 1230 which documented a problem with the circulation fans tripping

on overload during starting in fast speed resulted in the issuance of

Desion Change Package (DCP) Number 297, Revision 1, which will result in

qualified overloads of higher capacity being installed in the circuitry.

SFR's 1187 and 1531 document.ed discrepancies between wiring terminations

for the containment circulations fans control and alarm circuitry and the

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design drawing for this circuitry (drawing E-224, Sheet 1).

SFR 1187 was

resolved on August 13, 1980 stating the alarm circuit on E-224, Sheet 1,

would be revised to show circuitry as found in field.

SFR 1531 was issued

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on October 8,1980 to state that although E-224, Sheet 1, had been re-

vised (Revision 10) the circuitry as shown on the drawing still did not

correspond to what was in field. On November 10, 1980, the response from

Bechtel Project Engineering stated that they did not agree that E-224,

Sheet 1, was in error. Attached to the SFR was a memorandum of a tele-

phone call between a member of Bechtel Project Engineering and the Inte-

grated Startup Group Test Engineer for the containment atmosphere circula-

tion system stating that the alarm circuitry shown on drawing E-224, Sheet

1, Revision 10, is correct and no drawing change is needed.

On February 18, 1982 an inspection of the alarm circuitry for the contain-

ment circulation fan IV416A in panel 1B236 was conducted. The alarm cir-

cuitry had still not been changed to correct Ge installation to agree

with the SFR 1531 resolution. The temporary modification log was reviewed

and it was determined that a temporary modification was still in effect

for the configuration found in the panel.

Since the problem identified in SFR 1187 and 1531 still exists, this item

will remain open pending resolution.

On Fetruary 20, 1082 Startup Administrative Manual, A06.3, Revision 6,

"Startup Field Report" was reviewed.

Section 5.3.3 of the procedure states

that upon receipt of the SFR reply, work items resulting from the SFR

resolution agreeable to the ISG are added to the Startup Work List, and

if ISG disagrees with the resolution, a new SFR indicating the disagreement

is prepared and processed. No SFR had been written since the reply of

November 10, 1980 to indicate that ISG disagreed with the resolution, and

no Startup Work List item had been entered as of February 18, 1982.

PP8L's PSAR, Appendix D, Section 0.2.5, the PP&L 0A Manual Procedure 7.1

and 10 CFR 50, Appendix B, Criterion V require that activities affecting

quality will be accomplished in accordance with approved procedures. On

February 25, 1982, the Assistant Superintendent of Plant was told that the

failure to properly follow the Startup Administrative Manual Procedure

AD.6.3, Revision 6 for processing the resolution to an SFR was a violation

against 10 CFR 50, Appendix B, Criterion V.

(387/81-04-02)

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(Closed) Inspector Followup Item (387/81-28-02) Sources of Acceptance

Criteria.

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The inspector verified that sources of acceptance criteria are identified

on several of the startup test procedur,es previously reviewed by the in-

spector. Licensee personnel stated that the sources of acceptance

criteria will be identified on all future startup test procedures,

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(Closed) Inspector Followup Item (387/81-28-03) Transient Tests on Reactor

Level Instruments.

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The licensee personnel stated that the transient tests on reactor level

instrumeats are included in startup test procedures ST-25, Revision 0, Main

Steam Isolation Valves and ST-27, Revision 0, Turbine Trip and Load Rejection.

The inspector reviewed these procedures and verified the above.

t.

(Closed) Construction Deficiency Report (387/80-00-15)

See Section 4 on Bulletin 80-21.

3.

Plant Tours

The inspector conducted periodic tours of accessible areas of the plant during

normal and backshift hours. The inspector observed work in progress, testing,

housekeeping, cleanliness controls, and storage and protection of components

and systems.

Findings:

ESW and RHR Instrumentation Access Pit

a.

On February 1,1982 the inspector found wate r in the two concrete access

pits containing 'B' division Emergency Service Water and Residual Heat Re-

Each pit contains a

moval (RHR) Service Water Piping and Instrumentation.

section of discharge piping with a flow orifice, heat tracing, a flow trans-

mitter and associated wiring and terminal boxes. The 'B' division Emergency

Service Water pit was filled to about 5 feet, submerging all but the tops

of the terminal boxes. The 'B' division RHR service water pit was filled to

about 2b feet, partially submerging the heat trace and flow transmitter.

The two ' A' division access pits, which are located adjacent to the flooded

'B' division pits, contained about an inch of water.

The lowest equipment

in these pits is about 6 inches from the bottom and was not covered.

The four pits form a row located on the south side of the emergency service

There is normally a concrete cover with a manhole over

water pump house.

each pit, but the covers were removed for installation of missile shields.

There were temporary covers of corrogated roofing material over the ' A'

division pits, but the covers on the flooded 'B' division had been removed.

There was also a plastic tent type structure over the entire area, but the

inspector found snow on the ground under the tent.

The inspector infonned the licensee of the problem and on February 2,1982

the pits were pumped dry with a portable pump and sand bags were placed on

the bottom inside walls of the tent type enclosure.

Licensee representatives

told the inspector that the cause for the flooding has not bean completely

determined, but that it appeared to be primarily due to surface run-off into

the top of the pit. The possibility of leakage around piping and conduit,

or through the walls, is still being evaluated.

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System turn over from the constructive organization is accomplished separately

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from the turnover of the facilities or areas in which the equipment is located.

The work on the missile shields was under the jurisdiction c' the Bechtel

construction organization, but the equipment inside the pit was turned over

to the licensee. Procedures do not adequately specify requirement for

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protecting turned over equipment within an area or facility from work activities

of the construction group. As a result, the pits were allowed to fill with

water to the extent that vital equipment was submerged.

Appendix B, Criterion II of 10 CFR 50 requires activities affecting quality

to be accomplished under suitably controlled conditions.

Controlled con-

ditions include suitable environmental conditions for accomplishing the

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activi ty.

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10 CFR 50, Aopendix B, Criterion V requires that activities affecting quality

shall be prescribed and accomplished by documented instructions appropriate

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to the circumstances.

The Susquehanna PSAR, Appendix D, Section D.P.5 requires activities affecting

quality be prescribed by documented instructions, procedures or drawings

appropriate to the circumstances.

On February 5,1982 the inspector told the Superintendent of Plant that the

failure to have adequate procedures which establish sufficient environmental

controls to prevent flooding of safety-related equipment is a violation.

(387/82-04-03)

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b.

Reactor Vessel Head

On February 11, 1982, the inspector witnessed the reactor vessel head being

put in place on the reactor vessel in Unit 1.

The inspector noted that the

work was being accomplished by an approved procedure, and that qualified

personnel were performing the job.

The inspector also visually inspected

selected head closure studs for both the reactor vessel head and the con-

tainment head.

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No unacceptable items were noted.

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4.

IE Bulletin and Circular Followup

IE Bulletins and Circulars listed below were reviewed to verify the following:

(a) Bulletins and circulars received by PP&L corporate management were for-

warded to appropriate individuals with.n the organization, including

station management, for information, review and/or corrective actions as

required.

(b) PP&L bulletin responses were submitted to the fiRC within the specified

time period.

(c) Licensee reviews and evaluations of bulletins and circulars are complete

and accurate, as supported by other facility records and by inspector

observations of installed plant equipment.

(d) Corrective actions specified in licensee bulletin responses or internal

circular evaluation memoranda have been completed and/or responsibilities

have been assigned for completion.

Bulletin 80-21, " Valve Yokes Supplied by Malcolm Foundary Company, Inc."

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The licensee replaced all of the defective valve yokes in Unit 1.

Six de-

fective yokes from Unit 2, and 2 yokes in spare valves still need replace-

ment.

These are being tracked by the licensee under Bechtel Noncompliance

Report 5980, and are scheduled for completion by October,1982.

This bulletin is closed.

-- Circular 80-02, " Nuclear Plant Staff Work Hours."

Administrative Procedure AD-QA-300, Revision 0, " Conduct of Operations" was

reviewed to detemine if concerns of the circular had been addressed.

Section

6.1.3 of the procedure complies with the guidelines established in the cir-

cular for licensed operators. However, it did not address these guidelines

for non-licensed operators or other personnel who perform safety-related

functions (e.g.: health physicists, I&C technicians, and key maintenance

personnel) .

This circular remains open pending resolution of this discrepancy.

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Circular 80-18, "10 CFR 50.59 Safety Evaluations for Changes to Radioactive

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Waste Treatment Systems."

This circular had been previously discussed in NRC Inspection Report 80-32

and was left open pending a review of a licensee procedure which addressed

proposed changes to the plant would require a safety evaluation.

On February

4,1982 Nuclear Department Instruction, NDI-QA-14.2.2, Revision 0, " Safety

Evaluations" was reviewed.

This procedure discusses which changes to the

facility must be evaluated and what the scope of the evaluation should be.

This circular is closed.

-- Circular 81-02, " Performance of NRC Licensed Individuals While On Duty."

Administrative Procedures AD-QA-300, Revision 0 " Conduct of Operations" and

AD-QA-303, Revision 0, "Shif t Routine" were reviewed. These two procedures

incorporated the concerns of the circular.

This circular is closed.

-- Bulletin 79-28, "NAMCO Model EA180 Limit Switches."

On February 17, 1981, Bechtel Nonconformance Report (NCR) 8162 was reviewed.

The NCR stated all Unit One NAMC0 switches applicable to the bulletin had

been repaired under PPSL Work Authorizations WA-U-12395 and WA-U-12399.

These work authorizations were reviewed and found to have performed the

su99ested repairs for all Unit One valves listed in the Bechtel NCR.

This bulletin is closed.

-- Bulletin 79-08, " Events Relative to Boiling Water Reactors Identified During

TMI Incident."

The licensee's commitments to NUREG 0737 and 0694 has been reviewed by NRC:

NRR and has been reviewed as documented in the Safety Evaluation Reonrt.

Future inspections to verify commitments made by the licensee base

1 NUREG

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0737 and 0694 will be completed by Regional Inspections.

Since bulletin 79-08 information was essentially restated in one of the two

NUREGS, this bulletin is closed.

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Bulletin 79-09, " Failures of G.E. Type AK-2 Circuit Breaker in Safety

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Related Systems.

This bulletin had previously been discussed in NRC Inspection Report

(387/81-25). On February 19, 1982 various AK-2 circuit breakers were in-

spected in the following 125 volt D.C. distribution panels:

-- 10-612

1D-632

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-- 10-642

No undervoltage devices as described in the bulletin were found in the

breakers.

This bulletin is closed.

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5

Preoperational Test Witnessing

Portions of the following preoperational testing were observed to verify that:

The approved test procedure was the current revision-being followed.

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-- Qualified personnel were performing the test.

-- Test precautions and prerequisities were followed.

-- Test and measuring equipment met procedure requirements and was properly

calibrated.

Quality control hold and witness requirements were met.

--

Test results were properly documented.

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-- Test procedures are technically adequate.

-- Test results are acceptable.

Criteria for interruption and continuation of testing are adhered to.

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(a) Containment Atmosphere Control System

The approved procedure was reviewed prior to the scheduled testing on

January 27, 1982. The procedure did not verify the maximum design closure

time for containment vent and purge valves. The closing time requirements

are listed in FSAR Table 6.2-12, and in Technical Specification Table

3.6.3-1.

The inspector asked the Test Engineer if the valve closing times

were measured as part of a different procedure and found that they were

not. The inspector told the Test Engineer that containment isolation valve

design closing times must be verified, and that the preoperational test

procedure appeared to be inadequate.

On January 28, 1982 the inspectors looked at the rest of the preoperational

test procedures involving containment isolation valves to see if closing

times were measured.

Containment isolation valve closing times were not

measured in preoperational tests P25.1, Primary Containment Instrument

Gas, and P34.2, Reactor Building Chill Water.

In test P64.1, Reactor Cir-

culation System, the valves were timed, but no acceptance criterion was

listed. Test P50.1, Reactor Core Isolation Cooling, required valve 1F088

to close in less than 5 seconds, however, FSAR Table 6.2-12 requires a 3

second closing time.

Valve 1F088 actually closed well within the 3 second

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limit during testing.

In test PS2.1, High Pressure Coolant Injection, valves

IF100 and IF042 were not timed.

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Appendix B, Criterion XI of 10 CFR 50 requires preoperational testing of

structures, systems and components to demonstrate that they will perform

satisfactorily in service. The tests must be performed in accordance with

written test procedures which incorporate the requirements and acceptance

limits contained in applicable design documents.

Quality Assurance Procedure SP-3, Control of Testing and Inspection Activities,

Part 5.4.12 requires the preoperational test program to assure that licensing

commi t i. :nt - and design specifications are reflected in the completed installa-

tions.

The Se quehanna FSAR, Section 14.2.12.1 (P59.1) states that the closure

times specified in the FSAR for containment isolation valves are to be veri-

fied in the various system preoperational tests.

Failure to properly verify closure times of the containment isolation valves

identified above is a violation.

(387/82-04-04)

This violation was discussed with the Assistant Station Superintendent on

January 28, 1982. He informed the inspectors that the Integrated Startup

Group (ISG) had also initiated a review of other preoperational tests to

determine the extent of the problem. On January 29, 1982, the Assistant

Station Superintendent informed the inspectors that a new preoperational

test would be issued for the purpose of testing containment isolation valve

closure times, and that the appropriate change to the FSAR would be submitted.

The inspectors reviewed the draft Technical Specifications for the Susque-

hanna Steam Electric Station, Unit 1.

Section 3.6.3 states limiting condi-

tion for operation for primary containment isolation valves, and states

that the isolation valves listed in table 3.6.3-1 must be demonstrated oper-

able with isolation time less than or equal to those listed on table 3.6.3-1.

Since the valve timing would have to be performed to meet this requirement

prior to entering operational condition 3 (Hot Shutdown) the violation for

not performing time testing in the preoperational tests is not considered

as having large safety significance.

On February 4,1982 preoperational testing was observed. No unacceptable

items were identified.

b.

Core Spray

On the evening of February 10, 1982 portions of Section 8.3.1 of Preopera-

tional Test P55.1, Revision 2 were witnessed.

No discrepancies or unacceptable items were noted.

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6.

Preoperational Implementation

a.

Temporary Modifications

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On February 5, 1982 ' two position switch was observed connected to ter-

minals 1 and 2 in terminal box TB0144 in the Reactor Core Isolation System

(RCIC) Room. The switch had no temporary modification tag attached to it.

The temporary modification log was reviewed, but no entry could be found for

putting this switch into the terminal box.

The Integrated Startup Test Engineer for the RCIC System stated the switch

was placed in the system to be used as a local safety trip during initial

testing.

10 CFR 50, Appendix B, Criterion V states that activities affecting quality

shall be prescribed by approved procedures.

PP&L Quality Assurance Manual Procedure SP-9, Revision 1, Section 5.3 states

that temporary modifications shall be controlled and documented in accordance

with approved procedures.

PP&L Startup Administrative Manual Procedure AD6.8, Revision 4, Sections 5.3

a'id 5.4 states that an orange tag is used for field identification of temporary

modifications, and that temporary modifications are documented on the Temporary

Modification Log.

On February 5,1982 the Superintendent of Plant was notified that since the

switch had not been entered into the temporary modification log, nor had a

orange temporary modification tag been placed on the switch, this was a

violation of 10 CFR 50, Appendix B, Criterion V.

(387/82-04-05)

b.

Controlled Drawings

On February 12, 1982 controlled drawing stick file number 87 and 127 were

reviewed.

It was noted that stick file 127 drawing E-137, sheet 9 was re-

vision 2 of the drawing while stick file 87 had revision 3 to the drawing.

On February 16, 1982 the inspector reviewed the Audit Verification Sheet for

stick file 127. The audit was begun on January 30, 1982 and completed on

February 15, 1982. The audit verification sheet noted that drawing E-137

sheet 9 was the wrong revision, and en updated version had been requested.

No unacceptable items were identified.

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14.

7.

Startup Test Program Review

The inspector reviewed the licensee startup test program against the commit-

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ment in FSAR and the requirements of Regulatory Guide 1.68, Revision 1.

Based

on the above review, the inspector had several questions on how the licensee

complies with the requirements of certain paragraphs of R.G.1.68, Revision 1,

Appendix A and discussed them with the licensee personnel.

Some of these ques-

tions were satisfactorily resolved by the detailed explanation presented by

the licensee personnel. The remaining questions, described below, need further

actions by the licensee for their resolution:

R.G.1.68, Revision 1, Appendix A, Paragraph 5.n requires collection of

baseline data for reactor coolant system loose parts monitoring system

during the power ascention test phase. This test is not included in any

of the Startup Test Procedure abstracts in FSAR Section 14.2.12. 2. The

licensee personnel stated that this test will be included as a subtest of

one of the presently scheduled startup tests.

This is an insnector followup item.

(387/82-04-06)

R.G.1.68, Revision 1, Appendix A, Paragraph 5.e.e requires demonstration

of the primary containment inerting and purge system operation in accordance

with design, during the power ascension test phase. This test is not in-

cluded in any of the startup test procedure abstracts in FSAR Section 14.2.

12.2.

The licensee personnel stated that a new subtest procedure (ST 37.2)

will be written and incorporated into an existing test procedure (ST 37,

Gaseous Radwaste System) and the new subtest will be scheduled to be per-

formed following the Plant Warranty Run.

This is an inspector followup item.

(387/82-04-07)

R.G.1.68, Revision 1, Appendix A, Sections 4 and 5 require low power

tests and power ascention tests to be performed at definite power plateaus

( 5%, 25%, 50%, 75%, 100%) or at definite power ranges,

The startup test

program as described in FSAR Section 14.2 indicates that these tests to

be performed at certain Test Conditions (TC-0,H,1,2,3,4,5, and 6). These

test conditions generally do not correspond to definite power plateaus

required by R.G.1.68, but vary over wide range of power levels. This is

especially true for TC-1,2, and 3.

The licensee personnel explained that a

new startup test procedure (ST-99) will be written to specify various power

plateaus or ranges for each test as required by RG 1.68.

This is an inspector followup item.

(387/82-04-08)

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8.

Startup Test Procedure Review

The following preliminary issues of startup test procedures were reviewed for

compliance with NRC requirements and licensee commitments:

a.

ST-4, Revision 0, Full Core Shutf7wn Margin.

b.

ST-15, Revision 0, High Pressure Coolant Injection.

c.

ST-25, Revision 0, Main Steam Isolation Valves,

d.

ST-27, Revision 0, Turbine Trip and Generator Load Rejection,

e.

ST-28, Revision 0, Shutdown From Outside The Control Room.

Based on the above review, the inspector had several questions 2nd discussed

them with licensee personnel. These questions were satisfactorily resolved

by the answers presented by the licensee personnel which were further verified

by the inspector by review of pertinent records except that one question needs

further licensee action for its resolution. The following is a brief outline

of these questions and their resolution:

a.

ST-15, Revision 0, High Pressure Coolant Injection

FSAR Section 14.".7 commits to R.G.1.68, Revision 1, which requires

demonstration of auto start of HPCI system under simulated accident

'

conditions and injection into the reactor coolant system during power

ascension test phase (see R.G.1.68, Appendix A, Paragraph 5.k).

The

'

inspector questioned the validity of simulating the accident conditions

by using the MANUAL INITIATION push button rather than by tripping the

accident condition primary sensors (reactor low level switches and dry-

well high pressure switches). The licensee stated that the circuitry

for HPCI auto initiation from the primary sensors is in parallel with

the MANUAL INITIATION push button and will be tested during preoperation

testing, and therefore is not repeated during startup testing. The

inspector verified this by review of HPCI Preoperational Test P52.1, Revision 2.

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b.

ST-25, Revision 0, Main Steam Isolation Valves

The insoector pointed out that R.G.1.6R Revisinn 1 Anoendix A Para-

graphs 4.m

5.u, and 5.m.m require testin,g of MSIV's,at less than, 5%

power (Low Power Test) and at 25%, 50%, and 100% po;.er (Power Ascension

s.

Tests) and that the tests as described in ST-25 generally satisfy these

requirements except that the Power Ascension Tests at 25% and 50% pov:er

are grouped as a single test to be performed between 5% and 75%. The

licensee personnel explained that there will be two separate tests

(near 25% and 50% power) as shown on the draft Power Ascention Test Pro-

gram Schedule. The inspector verified this by review of the above

schedule.

c.

ST-27, Revision 0, Turbine Trip and Generator Load Rejection

The inspector pointed out that Section 27.2.2, Initial Status, of ST-27

dots not specify the Recirculation Flow Control Systems mode (AUT0/

MASTER MANUAL) during the performance of this test and the selection of

the mode will influence the test results.

The licensee personnel ex-

plained that the MASTER MANUAL mode will be selected as shown on FSAR

Figure 14.2.5, Sheet 1, and will be specified in G0-00-003, Operating

Procedure for Power Ascension, Revision D, which will be used to arrive

at the initial conditions for ST-27. The inspector verified this by re-

view of the above operating procedure,

d.

ST-28, Revision 0, Shutdown From Outside the Control Room

The inspector pointed out that R.G.1.68.2 (Initial Startup Test Program

to Demonstrate Remote Shutdown Capability for Water-Cooled Nuclear

Power Plants), Revision 1, which the licensee is committed to, requires

maintaining stable hot standby condition for at least 30 minutes during

this test and that the test as described in ST-28 does not reflect this

requirement.

The licensee personnel explained that the decay heat from

the fresh reactor core is not sufficient to overcome the losses from

the reactor coolant system and, therefore, the above requirement cannot

be achieved in practice.

The inspector stated that the test abstract in FSAR Section 14.2.12.2

for ST-28 describes the initiation of this test with a reactor scram

from outside the Control Room where as the test as described'in the

detailed test procedure (ST-28, Revision 0) describes the initiation of

the test with a reactor scram from the Control Room. The licensee

personnel explained that FSAR Section 14.2.12.2 will be corrected to

agree with ST'-28, Revision 0.

This is an inspector followup item.

(387/82-04-09)

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9.

Quality Assurance Survbillance Activities

Operational Policy Statement (OPS) Number 7, Revision 0, states in Section

5.3 that Nuclear Quality Ass' rance (NQA) will establish a Surveillance Program

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to verify by observation that activities are performed in specified manners.

It also states that Functional Unit Procedures will be established to detail

and implement this surveillance program.

On February 25, 1982 the Operations Quality Assurance Supervisor was questioned

as to status of functional unit procedures for the surveillance program. He

stated a Surveillance Program Procedure was in draft

and being reviewed.

,

The Operational Quality Assurance Program must in effect at least 90 days

'

prior to receiving an operating license; and therefore the Surveillance Pro-

gram mutt be in effect by that time. The approved program will be reviewed

during a subsequent inspection.

(387/81-04-10)

10.

Emergency Planning Meeting

On the arening of February 24, 1982, at the request of the Secretary of the

Nescopeck Borough Council the inspector and the Director of the Division of

Emergency Plans and Operational Support attended a meeting organized by the

Berwick Corough Council with other Columbia County Municipalities and town-

ships. The meeting was organized to listen to a presentation made by repre-

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sentatives of the licensee on Emergency Planning.

11.

Traversing In-Core Probe System Electrical Power Supplies

On January 27, 1982 representatives from PP&L told the NRC Resident Inspector

that power supplies to the traversing In-Core Probe System (TIPS) contain-

ment isolation ball valve, and to tne back-up shear valve were not installed

as safety-related. Since the ball valve is considered the containment isolation

valve, a PP&L Quality Assurance Action Request (Number 82-011) had been initiated

on January 26, 1982 requesting the PP&L Nuclear Plant Engineering (NPE) Group

to evaluate this problem. On January 27, 1982 the NPE Group responded stating

that the power supplies to both the ball valve and the shear valve should be

safety grade.

PP&L Nonconformance Report Number 82-058 was written to document

the problem.

The problem was then discussed with the General Electric (G.E.) Operations

.

Manager at the Susquehanna Site who stated that all G.E. BWR's would have the

same electrical set-up since G.E. did not consider the TIPS System as safety-

related.

i

FSAR Table 3.2-1 states that TIPS piping and isolation valves are Safety Class

f

2 and Seismic Category I, but does not discuss the power supplies for the valves.

With the present configuration, it can not be assured that the ball valve or

the shear valve will be capable of operation when a containment isolation signal

is generated.

The resolution to this problem will be further addressed by the NRC and will be

reviewed during a subsequent inspection.

(387/82-04-11)

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12.

Exit Interviews

At periodic intervals during the course of this inspection, meetings were held

with facility management to discuss the inspection and findings identified.

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