ML20045F538

From kanterella
Jump to navigation Jump to search
Insp Rept 50-458/93-19 on 930425-0605.No Violations Noted. Major Areas Inspected:Onsite Response to Events,Operational Safety Verification,Maint & Surveillance Observations & Water Level Instrumentation Errors
ML20045F538
Person / Time
Site: River Bend Entergy icon.png
Issue date: 07/02/1993
From: Gagliardo J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20045F533 List:
References
50-458-93-19, NUDOCS 9307080009
Download: ML20045F538 (18)


See also: IR 05000458/1993019

Text

.

_

_

_ . _ -

.

.

_

_

,

.

.

,

APPENDIX

1

!

'

U.S. NUCLEAR REGULATORY COMMISSION

.

!

REGION IV

!

Inspection Report:

50-458/93-19

l

r

Operating License:

NPF-47

Licensee:

Gulf States Utilities

'

P.O. Box 220

.

St. Francisville, Louisiana 70775-0220

Facility Name:

River Bend Station

Inspection At:

St. Francisville, Louisiana

1

Inspection Conducted: April 25 through June 5, 1993

i

Inspectors:

W. F. Smith, Senior Resident Inspector

."

D. P. Loveless, Resident Inspector

lE. T. Baker, Senior Project Manager,

j

9 ear Reactor Regulation, Project Directorate IV-2

l

61

h

?2 );

,

1

Approved:(

/ /

o'

{.E(pagi24rdo, Chief,ProjectSectionC

D'at(

i

Inspection Summary

,

Areas Inspected:

Routine, unannounced inspection of onsite response to

events, operational safety verification, maintenance and surveillance

I

observations, water level instrumentation errors during and after

depressurization transients, followup on corrective actions for violations,

and other followup.

l

Results:

The inspectors found that the licensee's activities in determining and

1

correcting the causes of air leakage into the service water system were

appropriate (Section 2.1).

,

The licensee's identification of logic system functional test

r

discrepancies demonstrated excellent attention to detail (Section 2.2).

j

,

!

The licensee's corrective actions and analyses regarding the heat

!

capacity temperature limit for the suppression pool following a control

room fire with a loss of offsite power were_ appropriate _(Section 2.3).

j

During control room observations, the inspectors noted an increase in

l

operator formality and the controls over nonoperator visitors. The

9307080009 930702

PDR

ADDCK 05000458

G

PDR

.

. --

- - -

_

.-

_ _.

. . _ . -

__

.

-_

..

-

-.

.

- . _ .

-

'

.

s

!

-2-

)

!

startup on May 31 and the shutdown on June 1, 1993, were conducted in a-

deliberate and careful manner (Section 3.2).

The conduct of the pressure test of Reactor Recirculation Pump B seal to

troubleshoot the' failure was poorly planned resulting in ineffective

communications that were established (Section 4.1).

Work instructions to assure proper assembly of recirculation pump seals

'

appeared to be weak and contributed to the seal failure on June 1,1993.

The corrective actions appeared to prevent appropriate recurrence

.

(Section 4.1).

The inspector observed conduct of a monthly channel functional test of

the Channel A main steam isolation on low main steam line pressure. . The

results of the test were satisfactory, and the licensee's administrative

-

requirements were met, as were regulatory requirements (Section 5.1).

The inspector conducted the survey required by NRC Temporary

=

Inst uction (TI) 2515\\l19, " Water Level Instrumentation Errors During

i

and After Depressurization Transients," and found that the licensee had

l

adequately trained the operators to deal with the phenomenon, should it

j

occur (Section 6).

Summary of Inspection Findings:

Violation 458/92021-1 was closed (Section 7.1).

i

Violation 458/92021-2 was closed (Section 7.2).

Inspection followup Item 458/93010-2 was closed (Section 8.1).

l

Attachments:

i

Attachment 1 - Persons Contacted and Exit Meeting

Attachment 2 - NRC Survey for Evaluating Operator Guidance (TI 2515/119)

!

-?'

.

!

6

J

!

i

.

I

q

l

'

.-

.-.

.

, . .

..

._.

- - .

. -.

--

-

--

_

i

.

r

l

'

!

-3-

i

i

t

t

DETAILS

I

1 PLANT STATUS

j

At the beginning of this inspection period, the plant was in a cold shutdown

l

condition, since April 18, 1993, for the replacement of both reactor

.!

recirculation pump seals.

j

The plant remained in cold shutdown until June 1, because of additional

maintenance activities in response to a main steam isolation valve that failed'

!

to close.

This issue was documented in NRC-Inspection Report 50-458/93-18.

l

On June 1, the reactor was taken critical. While heating up, with the reactor.

at about 4 percent power, the outboard seal failed on Reactor Recirculation

!

Pump B.

Later that afternoon, the operators shut down and cooled the plant to

!

correct the problem.

l

'

At the end of this inspection period,'the plant was in a cold shutdown

.

'

condition to replace the f ailed reactor recirculation pump seal.

t

2 ONSITE RESPONSE TO EVENTS (93702)

j

.

2.1

Instrument Air Inleakage to Service Water System

On April 30, 1993, the licensee was troubleshooting a problem which was

identified by the closed loop plant normal service water (SW) system surge

tank level increasing at varying rates from approximately 2 to as much as

20 gpm. After several days of troubleshooting the system, the SW pumps began

,

to cavitate.

Large amounts of air had apparently entered the system, and the

air inleakage was displacing the water volume in the system, causing a level

!

increase in the surge tank.

j

In the reactor building, there are two air accumulators, each connect to a

high point on the safety-related Division I and 11 standby SW loops.

The

!

system was designed so that when SW pressure was lost, target rock solenoid

.:

operated valves (S0Vs) would open, injecting air into the SW piping to prevent

-l

water hammer when the standby SW pumps started.

Standby SW pumps were

programmed to start 45 seconds after the normal SW pumps stopped.

_

The licensee's inspection of the seating surfaces on the check valves and the

SOVs found good seating surfaces as evidenced by the wear patterns.

Corrosion

products were found in the bottom of Accumulator ISWP*TKlA.

Based on an

~

analysis of the corrosion products found, which included cobalt-60 and

manganese-54, and an internal inspection of the tank, the licensee concluded

i

that SW had backed up into the accumulator tank and deposited the corrosion

products.

The licensee also concluded that the cause of the air leaking into

the SW system was corrosion particles trapped on the seat of one of the SOVs

which allowed air to be continuously injected into the SW system.

--

.

. - .

-

.-.

- -..

-

-

-

.

.. -.

- -

-.

-. -

.

.

--

.-

. _ .

-

--

.

.

,

.

p

,

.

!

I

-4-

f

The licensee cleaned the S0Vs and accumulator tanks.

The licensee also

implemented daily checks of SW chemistry for oxygen content. Oxygen content

i

and SW surge tank level increases would be a good indication of air

i

in-leakage, so the operators could take timely action. The inspector reviewed

i

the licensee's actions to resolve this problem and concluded that they were

!

'

approp,riate.

2.2 Continued Discrepancies Found in Logic System Functional Tests (LSFTs)

NRC Inspection Reports 50-458/93-05 and -93-10 documented licensee-identified

!

discrepancies found in certain LSFT surveillance test procedures.

In each

case the problem was a failure to maintain testing continuity or overlap on

-;

LSFTs to assure that all logic components, from the sensor through the

actuated device were tested to verify operability.

The components in question

l

were found to be operable in every case after testing.

.

!

As of the end of this inspection period, the licensee was over 50 percent

!

complete on their reviews of surveillance tests, and the following additional

,

discrepancies were identified:

[

On April 26, 1993, the licensee identified sections of wiring and

contacts associated with the seal-in logic for high pressure core spray

!

,

'

(HPCS) injection Valve lE22A*MOVF004. Also, contacts that closed the

,

'

HPCS test return valves upon initiation of HPCS were not tested.

In

,

addition, the surveillance test procedure assumed that a Level 8

condition existed in the reactor during the test, when there should have

l

been a specific prerequisite to that effect.

The licensee ~ verified

-i

3

operability of the circuits through continuity checks, and planned to

correct the test procedure in support of the next time the surveillance

i

became due, which would be Refueling Outage 5.

The details were

l

,

documented in Condition Report (CR) 93-0228.

3

l

On May 11, during LSFT reviews of the main turbine trip system, five

i

discrepancies were identified by the licensee. The discrepancies

j

involved reactor Level 8 trips of the main turbine and reactor feedwater

!

pumps. Certain wires and contacts were not tested, and there were no

!

checks done on the reactor feedwater pump trips which were to occur on a

Level 8 signal.

The licensee subsequently verified these circuits to be

,

operable and indicated plans to correct the applicable surveillance test

j

procedures.

This problem was documented in CR 93-0267.

j

i

On June 1, while reviewing the anticipated transient without scram

!

.

system, the licensee discovered that there was no test to verify that

j

Reactor Recirculation Pump Breakers 2A, 28, 5A, and SB tripped on

!

reactor Level 2 and on high reactor pressure vessel pressure.

Also,

l

wiring from the control room panels was not tested. The discrepancy was

i

limited only to the breakers themselves.

The rest of the logic,

j

including relays, trip units, and transmitters, had been tested.

it

!

should be noted that these breakers were opened and closed for control

-

'

l

l

4

_ _

_

.

.

_

.

_

.

.

-.

-- - . -

- - . -

-

. ..

-,

w

.

t

-5-

.

!

,

purposes during each startup and shutdown evolution.

The licensee _

revised the surveillance test procedures and, as of the end of this_

inspection period, was in the process of conducting the tests. The

inspectors verified completion prior to the reactor startup. This

problem was documented in CR 93-0329.

l

On June 3, while performing an LSFT review of the automatic

.

depressurization system (ADS), the licensee identified a discrepancy

i

f

where certain contacts and wiring associated with the sealing in of the

high drywell pressure signal were not tested. The seal-in feature was

l

tested, but the procedure did not verify that the signal-stayed in until

reset. Also, sections of wire associated with the ADS initiation

signals from high drywell pressure and reactor level 1.

In addition,

i

contacts for the low pressure emergency core cooling system pump' running

,

permissive were not tested by the LSFT. These problems were documented

-

in CR 93-0336.

The licensee's reviewer also discovered that there were no channel

,

functional or channel calibration surveillance tests established for the

drywell high pressure bypass timers.

The licensee corrected the surveillance procedures and tested the

-

circuits satisfactorily prior to startup. The inspector reviewed the.

!

"as-found" channel calibration data taken on the ADS "A"

& "B" drywell

1

pressure bypass timers and confirmed that both were within the Technical

i

Specification allowable values. All of the other functions tested were

j

found to be operable.

i

The inspectors questioned the number of discrepancies found in safety-related

'

LSFT surveillance test procedures. The licensee indicated that the Human

Performance Enhancement System Engineer was developing a root cause analysis

l

and assessment which would be reviewed by plant management for any additional.

I

corrective actions and/or expansion of the scope of the reviews to other

surveillance procedures. The inspectors concluded that these actions were

.

!

appropriate and also directed the licensee's attention to NRC Information Notice 93-38, " Inadequate Testing of Engineered Safety Features Actuation

i

Systems," which addressed similar problems at pressurized water reactors. The

,'

root cause will be reviewed under Licensee Event Report 93-002.

.

!

"

2.3 Procedure for Shutdown from Outside Main Control Room

On May 21, 1993, the licensee identified, during a review of Abnormal

Operating Procedure A0F-0031, Revision 8A, " Shutdown from Outside Main Control

l

Room," that the potential existed for exceeding the heat capacity temperature

>

limit for the suppression pool within approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> from initiating

!

shutdown measures for a fire in the main control room. The licensee

i

documented the issue, and the actions taken, on CR 93-0294.

-

I

1

-

.

.

,_

- , _

_

~

- - . -

- - - .

. ~

. . , _ _ _

-

-.

_ - - .

--

. . - -

.

- - ~ _ .

.- ..

-

'

-

,

!

-6-

[

!

The concern was related to Design Criterion 240.201 which addressed a main

.

i

control room fire with a loss of offsite power, failure of the Division II

emergency diesel generator, and failure of the high and low pressure core

The Safe Shutdown Analysis assumed that reactor core isolation

spray pumps.

cooling would be used for reactor level control, residual heat removal Pump A

would be available for suppression pool cooling until shutdown cooling could

'

be achieved, and reactor pressure would be controlled by three available

safety relief valves, one of which was in the ADS.

The design criterion also

assumed " repairs," such as electrical jumpers to restore control air to the

l

'

ADS would not be necessary until late in the 72-hour postfire period.

Based on preliminary calculations and the guidance provided in the emergency

operating procedures, the licensee found that the operator would need to take

,

control of reactor pressure using safety relief valves within the first hour.

Therefore, an electrical jumper would need to be installed much earlier than

was assumed in the design criterion.

The licensee concluded that the existing procedures provided adequate guidance

,

to achieve safe shutdown within the assumptions used in Design

Criterion 240.201, for a main control room fire. Therefore, the concern was

determined to not be reportable under 10 CFR Sections 50.72 and 50.73.

-

However, to respond to the discrepancies between assumptions made in Design

Criterion 240.201 and the approved procedures for operating the plant in an

emergency, the licensee made the following improvements:

A modification was made to install a switch on Motor Control

,

Center IEHS*MCC2L to replace the jumper that would be installed in

accordance with Procedure A0P-0031. This would provide backup air for

the ADS using permanent plant equipment.

Minor changes were made to Procedure A0P-0031 to improve the guidance

!

.

for the above scenario.

j

Training of the plant operators was implemented to cover the changes to

{

=

Procedure A0P-0031.

The inspectors reviewed the disposition of the CR, verified completion of the

above items, and noted that all but the training had been. completed for

l

startup.

The licensee's response to the concern, and actions taken, were

l

considered appropriate.

i

2.4 Conclusions

?

The licensee's actions to determine the cause and correct air in-leakage to

[

i

the SW system were appropriate.

l

,

5

k

-

_

_

_ .

__

-

.

. , _

_

.

-.

~-

. .

...

.

. - -

'

.

.

.

-7-

,

The licensee's findings of overlap or continuity problems demonstrated

excellent attention to detail.

The licensee's determination of the root

!

causes will be reviewed as followup to the licensee event report.

.

The licensee's resolution of the procedure for shutdown from outside the main

control room during a fire in the control room, combined with a loss of

,

offsite power, was appropriate.

'

3 OPERATIONAL SAFETY VERIFICATION (71707)

!

The objectives of this inspection were to ensure that this facility was being

operated safely and in conformance with regulatory requirements.

l

3.1

Review of Startup Issues

During liquid penetrant testing of reactor control rod hydraulic control unit

.

piping welds, a linear indication was found on Hydraulic Control Unit 40-09.

.

CR 93-0209 was generated to document the linear indication. Maintenance Work

'

Order (MWO) R158892 was generated to repair and reinspect the weld.

,

t

Approximately 10 thousandths of- an inch (mils) of material was removed and a

penetrant test was performed that determined the indication was a surface

fl aw. Minimum wall thickness was maintained per design.

l

As a result of a " weak link" calculation performed for motor-operated valves,

i

i

it was determined that the stem on Valve 1G33*MOVF004 had been overstressed

due to an error in calculating closing torque for the valve. MWO R173872 was

,

written to replace the valve stem, stroke time test the valve, conduct

i

signature tracing, and perform an local leak rate test. The testing was

performed satisfactorily after the valve was reassembled with a new stem.

,

,

3.2 Control Room Observations

- i

The inspectors observed control room operations on a sampling basis.

l

Operations management had informed the inspectors that efforts had been

underway to continue improvement of control room professionalism and demeanor.

,

During this inspection period, the inspector noted an_ increase in control room

'

formal ity. Nonoperator access constraints were apparent.

On May 31, the inspector performed back shift (night) observations of the

reactor startup.

The operators were withdrawing reactor control rods on_the

,

approach to criticality following the outage.

The operator at the reactor

1

controls exhibited careful and deliberate communication with the reactor

engineer by repeating back rod selections.

On June 1, the inspector was in the control room during low power operation at

.

i

about 4 percent reactor power.

The operators were heating up the plant at

less than 30 F per hour to minimize thermal stresses on the leaking fuel

!

assembly (see NRC Inspection Report 50-458/93-10, Section 2.1).

The Reactor

n

I

.n-

-,

.,.

- - ,

-~, -

e

-

r

-

.

__

-_

.

_ .

-

._ .

_ _

.

_ _

.

. I

~

.

i

2

t

-8-

Recirculation Pump B seal failed suddenly, the shift supervisor evaluated the

i

condition and, with the support of plant management, decided to shut down and

^

repair the seal.

/

The shift supervisor briefed all of the operators that were to be involved in -

the shutdown, assigned specific stations, and made sure they were

,

knowledgeable of expected plant responses. When everybody was ready and on

station, he directed the reactor operator to scram the reactor as part of the

-i

normal shutdown process. When the scram was executed, all systems responded

1

normally, and the operators responded well to the annunciators.

3.3 Plant Tours

I

The inspectors toured 'Se areas of the plant, including the drywell.

,

Particular attention

given to the potential of fibrous material clogging

i

emergency core cool

sfetem suction strainers during accident conditions, as

described in NRC E

3-02, " Debris Plugging of Emergency Core Cooling

,

Suction Strainers.'

spectors noted that there was no such material on

j

the drywell coolers,

,a the filters were not installed for this' outage.

The inspectors noted _ e examples of damaged metal covers on fiberglass

r

insulation in the drywell.

The damaged insulation was repaired.

i

During an evening tour on May 5, the inspectors noted that the Division I

emergency diesel generator fuel oil day tank level was reading slightly below

,

55 percent on Level Indicator 1EGF-LIl6A. The inspector questioned a nuclear

equipment operator (NEO) because the level appeared lower than normal. The

!

NE0 stated that he was not aware of the required Technical Specification level

,

nor was the level indicated for evaluation on his daily rounds log.

During the next morning, the inspector reviewed Surveillance Test

Procedure STP 309-0201, " Diesel Generator Division I Operability Test."

Step 7.12.9 required the operator to verify that the day tank contained a

minimum of 316.3 gallons of fuel, equivalent to a level of 56.5 percent, as

!

indicated by Level Indicator 1EGF-LIl6A on Local Panel 1EGS*PNL3A.

The

inspector then immediately reverified that the level indicator still read

j

approximately 55 percent.

l

The inspector called the control room and notified the control operating

>

foreman.

The foreman declared the diesel generator inoperable and initiated

j

CR 93-0258 to review the problem.

,

l

System engineers developed calculations to evaluate the fuel oil level

i

required to meet the minimum requirements of Technical

.

,

Specification 3.8.1.1.b.l.

This specification required that the day tank

!

contain a minimum of 316.3 gallons of fuel. The inspector reviewed the

,

calculation, which indicated that 44.9 percent indicated level was equivalent

i

to 316.3 gallons in the tank.

Additionally, the licensee determined that,

!

even with worst-case instrument error, the minimum volume would be assured

!

with an indicated tank level of 52.3 percent,

j

.

.

-

-

e

,

-m,

v

r - -

-

c-

-

rw

.--

.

-

.

-

.

. .

.

-

-. - - , .

-

-

,

'

j

-

-i

.g.

!

,

The inspector independently verified the actual position of the fuel oil

'

suction tap on the tank and the relative position of the level transmitter

'

sensing line tap. The inspector also independently performed calculations to

verify the licensee's statement that the Technical Specification number of

t

316.3 gallons included the unusable volume of the tank.

3

'

The inspector concluded that on May 5 and 6,.1993, the day tank had contained

i

.

'

more than the minimum usable volume of fuel oil required by Technical

.

Speci fication 3.8.1.1.b.1.

The licensee also found that the automatic fuel oil transfer pump was

,

programmed to refill the day tank at a level below the minimum required by

Procedure STP 309-0201. The low level alarm was also below this value. The

licensee implemented Modification Request 93-0001 to change the fuel transfer

.

pump start and the low level alarm to above the conservative 56.5 percent

l

minimum indication required by Procedure STP 309-0201.

'

The inspector discussed the NE0's performance with the assistant plant manager

'

for operations. He stated that the NE0 should have followed up on the

inspector's original question. He also stated that this was an additional

example of the lack of questioning attitude by plant workers previously

,

i

identified by the licensee and that corrective actions were in progress.

Additionally, the licensee revised Operations Section Procedure OSP-0012,

>

" Daily Log Report," to include a verification of the day tank level in the NE0

,

daily rounds log.

Overall, the inspectors found that housekeeping and plant equipment' condition

,

had improved.

A few minor exceptions were noted and brought to the attention

!

of the licensee. The cleanliness and material condition of all- three

emergency diesel generators was not good.

In an effort to improve these

6

areas, the licensee implemented cleaning outages on each diesel generator, one

!

at a time, during this outage.

3.4 Security Observations

,

!

The inspectors observed security operations at the primary access point as the

security officers processed people into the protected area.

The officers

3

appeared to be alert and responsive to all alarms and made sure that people

used the various detection equipment properly

3.5 Radiation Protection Activities

The inspectors noted emphasis on the part of radiation protection technicians

' '

.

for minimizing exposures as they processed people into the radiologically

i

controlled area.

The licensee's "As Low As Reasonably Achievable (ALARA)"

programs appeared to be given high priority.

~

On May 3, 1993, the licensee's radiation protection engineer published an

internal report showing the benefits gained in exposure reduction for this

'-

outage as a result of the Refuel 4 decontamination of the reactor coolant

l

I

j

l

,

.

_ . . , . _

. -

-

- - . -.

.

_

_ , - . . . - , ,

. . , _ , , , - . , , _ , . ,

, -,

f

-i

'

,

i

-

,

-10-

,

system and the reactor water clean up piping replacement. The inspectors

reviewed the report and noted that significant dose reduction factors were

,

developed. On the drywell 82-foot elevation, comparing average dose rates

,

prior to Refuel 4 decontamination with average dose rates during this outage,

dose rates had been reduced by a factor of 3.7.

Similarly, for the drywell

'

95-foot elevation, dose rates had been reduced by a factor of 2.1.

3.6 Conclusions

.

During the outage, the licensee showed careful work controls, conservative

4

approaches to system breaches, and a slow and deliberate approach to the

May 31 startup.

Radiation Protection's emphasis on keeping worker doses as

low as reasonable achievable was appropriate.

4 MONTHLY MAINTENANCE OBSERVATIONS (62703)

l

The station maintenance activities addressed below were observed and the

'

documentation of the activities was reviewed to ascertain that the activities

were conducted in accordance with the licensee's approved maintenance

programs, the Technical Specifications, and NRC regulations.

!

4.1 Reactor Recirculatino Pump Seal Failure

On June 1, 1993, during the startup from Forced Outage 93-01, the outboard

.;

seal for Reactor Recirculating Pump B promptly failed. The plant was at

approximately 4 percent reactor power, and reactor pressure was approximately

,

400 psig. The outboard seal cavity pressure had deteriorated from

approximately 220 psig to zero.

Concurrently, drywell unidentified leakage

increased from zero to approximately 0.4 gallons per minute. Within about

.:

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, the operators commenced a normal shutdown and cooldown to repair the

i

seal.

l

,

The licensee's maintenance planners and engineers developed and implemented a

work instruction to pressurize the seal with a hydrostatic test pump while the

i

recirculating pump was isolated. The licensee was not able to pressurize the

l

seal because of excessive leakage of the recirculation pump isolation

i

valve (s) . MWO R175034 was developed to use the control rod drive pump as a

higher volume pressure source.

The inspector reviewed the MWC and questioned

whether the test should have been prepared as a special test procedure. The

MWO format did not appear to include sufficient step-by-step instructions and.

e

precautions, and adequate technical reviews may not have been performed to

,

assure a safe test designed to preclude equipment damage or personnel injury.

+

i

The licensee's representatives revised the MWO and indicated that the facility

Review Committee had reviewed the MWO.

The licensee's definition of "Special

Test Procedures" in Administrative Procedure ADM-0003, " Development, Control

and Use of Procedures," was sufficiently general to allow the licensee to use

the MWO for pressure tests in conjunction with General Maintenance

Procedure GMP-0070, " General Maintenance Pressure Testing Procedure."

However, this was considered nonconservative based on the reason discussed

above,

y

_;__

iw-

-

_

F

,

,

-11-

The inspector observed the test on June 3.

Appropriate briefings were held

and the shift supervisor appeared well informed of the planned test details.

Radiation Protection was actively ensuring that radiation exposures were

minimized.

However, test communications were poor.

The test director was in

the drywell, using the gaitronics telephone and paging system to communicate

with a person in the reactor building, who in turn used hand signals to the

operator at the test gauges, who also used hand signals to the operator who

was throttlir.g the control rod drive system valves.

Noise levels in this area

were high, so personnel were required to wear ear plugs. After the test was

started, the control rod drive system was incapable of developing sufficient

flow to overcome recirculating pump isolation valve leakage.

The seal was

only pressurized to approximately 150 psig, which provided inconclusive test

results. The test was terminated and the licensee decided to disassemble the

reactor recirculation pump seal.

[

!

On June 4, while checking the dimension (referred to as the "D" dimension)

between the throttle sleeve nut of the seal and the motor coupling, the

'

repairmen noted that the gap was 0.355 inches; it was recorded at 0.176 inches

during installation in early May.

The "D" dimension was set as a function of

!

critical seal internal clearances, which in turn affected the clearances and

spring tensions for the sealing surfaces.

Examination of the seal components

upon disassembly in the shop revealed a single crack in the outboard rotating

.

seal that went completely through the tungsten carbide element.

Both the

l

inboard and the outboard carbon faces were scored.

In addition, the metal at

'

the lower end of the keyway in the shaft sleeve was scored indicating that the

sleeve may have been forced against the key.

The licensee concluded that the sleeve failed to go all the way down on the

pump shaft when the seal was installed. The assembly procedure assumed the

sleeve assembly was fully seated and, as such, set up a "D" dimension that was

to establish proper seal clearances and spring tension.

By not going all the

way in, the sleeve was pulled up too high (by 0.355 minus 0.176 inches).

As a

result, the seal springs were compressed too tightly.

This caused excessive

sealing surface forces and, as reactor pressure increased to about 400 psig, a

-

ridge on the rotating sleeve contacted the outboard rotating element, creating

abnormal stresses and breaking the element.

As corrective action to prevent recurrence, the licensee developed a series of

specific inspections and measurements to assure that the pump shaft sleeve

would fit freely over the shaft without interference.

These measurements'and

inspections included verification of proper motor end play. Specific internal

clearance dimensions were specified to be taken in the shop when the seal was

,

assembled and, as the cartridge was being assembled in the pump, to verify

that internal clearances and rotating element spring tensions would be

correct.

This would assure valid "D" dimension establishment during the final

I

stages of assembly.

l

At the end of this inspection, the licensee had made the decision to check the

i

seal on Reactor Recirculation Pump A, but the scope of that work had not yet

been determined.

J

,

,

'

.-

.

-

-

-

.

.

.

- . . - . - . , .

-

I

e

.

.

-12-

4.2 Conclusions

Performance of the troubleshooting pressure test was poor, in that

communications established between the pressure source control station and the

equipment being tested were crude and could have caused problems if quick

action to mitigate a rupture or a spray had occurred.

The licensee's-

application of the administrative definition of when to implement the more-

formal special test procedure for unusual evolutions aopeared to be

nonconservative.

Work instructions to assure proper assembly of the seal in the pump appeared

to be weak and contributed to the seal failure on June 1.

The corrective

actions to prevent a recurrence of the seal failure that occurred on June 1

appeared sound.

5 BIMONTHLY SURVEILLANCE OBSERVATIONS (61726)

The inspectors observed the surveillance testing of safety-related systems and

components addressed below to verify that the activities were being performed

in accordance with the licensee's approved programs and the Technical

Specifications.

5.1 Main Steam Line Pressure Channel Functional Test

On June 4,1993, the inspector observed instrument and control technicians as -

they performed the channel functional test of the Channel A main steam line

isolation on low main steam line pressure. Thi: test was a monthly

surveillance required by Technical Specification 4.3.2.1.

The test was

performed in accordance with Surveillance Test Procedure STP-051-4514,

Revision 4, " Isolation Actuation /MSLI-Main Steam Line Pressure - Low Monthly

Chfunct; (B21-N676A)."

The technicians performed the test in a deliberate, step-by-step manner, and

the acceptance criteria were met.

Independent verification of leads lifted

and restored was accomplished as required by the licensee's administrative

requirements.

The appropriate approvals were obtained from the operators as

,

required by the procedure.

6 WATER LEVEL INSTRUMENTATION ERRORS DURING AND AFTER DEPRESSURIZATION

TRANSIENTS (TI 2515/119)

The objective of this TI was to verify licensee implementation of operator

guidance and training to ensure required operator actions concerning reactor

vessel water level following rapid depressurization transients and, also, to

ensure that this guidance and training was consistent with plant Emergency

,

Operating Procedures.

Attachment 2 of this inspection report is the completed survey form provided

as Appendix A, "NRC Survey for Evaluating Operator Guidance," to TI 2515/119.

The survey results are documented by the survey form.

,

w

vv.

v .

m

-

I

,

i

i

-13-

l

1he inspector reviewed the licensee's response of September 28, 1992, to the

j

generic letter and noted that they were aware of BWR owners group activities

,

and guidance provided on this issue.

Based on that guidance, the licensee

'

incorporated the effects of noncondensible gases on reference leg reactor

pressure vessel water lever instrumentation in Lesson Plan Number REQ-501-0.

The licensed operators were trained in the classroom on the phenomena, how to

recognize it, and how to deal with it through use of the emergency operating

procedures.

This training was completed on February 19, 1993.

In addition,

the general operating procedure for startup was revised in the fall of 1992 to

make it mandatory to fill reference legs during startup.

The licensee did not have a scenario programmed into the plant simulator where

the operators would be challenged to respond to an unannounced rapid plant

i

depressurization concurrent with reactor water level instrument failures due

to gases coming out of solution, nor did they indicate any plans to procure

such a program at the time of this inspection.

In summary, the licensee appeared to adequately train the operators to be

prepared to respond to inaccuracies in reactor pressure vessel level

indications during rapid depresurrizations, and with the aid of a video tape,

clearly explained the phenomenon.

As of the end of this inspection, the

licensee was in the process of expanding the training on this issue based on

receipt of additional information from the BWR Owners Group, and Emergency NRC

Bulletin 93-03, " Resolution of Issues Related to Reactor Vessel Water Level

Instrumentation in BWRs."

)

7 FOLLOWUP 0F CORRECTIVE ACTIONS FOR VIOLATIONS (92702)

j

8.1

(Closed) Violation 458/9221-01:

Failure to Comoly with ASME Code

i

f

Requi rement s

Established measures did not assure that reactor pressure vessel feedwater

nozzle safe end and feedwater system elbow replacements complied with

ASME Code requirements for, respectively, test specimen location and wall

thickness.

The inspector verified that Procedure EDP-E0-22, " Items With Special

Considerations for Procurement, Transfer or Upgrade," Revision 0, included

committed actions for identification of test specimen locations in

ASME Class 1 forged materials and verification of wall thickness in ASME large

bore elbows.

The inspector also confirmed that the feedwater system elbow had

j

been rejected and that the final mechanical testing of the safe-end material

'

was in conformance with ASME Section Ill Code requirements.

7.2 1 Closed) Violation 4S8/9221-02:

f ailure to litilize Qualified Welding

Procedure Specification

The welding procedure specification (WPS) for welding the reactor vessel

feedwater nozzle safe end replacement material, WPS W3-16-AGT, Revision 0, was

not qualified in accordance with the requirements of MME Code,Section IX.

- _ _

.

.

_ . . _ _ ___

__

_

1

'l

'O

-14-

Specifically, supplementary essential variables QW-405.2 and-QW-409.1,

pertaining, respectively, to a change in position to the vertical position

uphill progression and an increase in heat input over that which was

qualified, were not supported by appropriate procedure qualification records.

The inspector verified that the committed training of the licensee welding

!

group had been performed and that the-additional procedure qualifications

l

tested by the licensee brought WPS W3-16-AGT into conformance with ASME Code,

Section IX, qualification requirements.

'

8 FOLLOWUP (92701)

8,1 IClosed) Inspection Followup Item 458/9310-02: Adeauacy of

Pp;.saintenance Testing Specified for Replacement Relays

l

f

On May 4,1993, the inspector reviewed the process for establishing the retest-

for the MDR relays used in the circuits for the Main Steam Line Isolation,-

Main Steam Line Radiation High feature. The planners selected a surveillance

'

test procedure and verified, from the elementary schematic, that the relay

!

circuits were tested. The system engineer performed a second verification of

the testing.

In some cases a specific continuity check would be specified in

the retest portion of the MWO to supplement the surveillance test procedure or

i

simplify the retest. The inspector concluded that the process used to specify

retesting of MDR relays was comprehensive and thorough.

j

,

r

-. ;

!

I

f

i

!

[

!

t

f

1

5

>

!

- -- - .

.

.

!

i

-l

i

s'

_g

ATTACHMENT 1

1 PERSONS CONTACTED

1.1 Licensee Personnel

,

  • R. L. Biggs, Supervisor, Quality Control
  • J. B. Blakley, Assistant Plant Manager, System Engineering
  • J. E. Booker, Manager, Safety Assessment and Quality Verification

B. R. Burke, Chemistry Supervisor

  • M. E. Crowell, Maintenance Support Supervisor
  • W. L. Curran, Cajun Site Representative

D. R. Derbonne, Assistant Plant Manager, Operations, Radwaste & Chemistry

L. L. Dietrich, Supervisor, Nuclear Licensing

R. G. Easlick, Radwaste Supervisor

L. A. England, Director, Nuclear Licensing

A. O. Fredieu, Supervisor, Maintenance Services

  • P. E. Freehill, Assistant Plant Manager - Outage Management

!

  • K.

J. Giadrosich, Director, Quality Assurance

P. D. Graham, Vice President (RBNG)

J. R. Hamilton, Manager-Engineering (RBNG)

i

  • W. C. Hardy, Radiation Protection Supervisor

.

R. T. Kelly, Instrument and Controls Supervisor

,

G. R. Kimmell, General Maintenance Supervisor

  • R. W. Koffman, Nuclear Security Representative
  • R. P. Lacour, Employee Relations Administrator
  • D. N. Lorfing, Supervisor, Nuclear Licensing
  • R. C. Lundholm, Supervisor, Mechanical Process Systems

i

  • I. M. Malik, Supervisor, Quality Operations
  • C. R. Maxson, Supervisor, Performance Assessment

J. F. Mead, Supervisor, Control Systems

  • Q. V. Nguyen, P,eliability Engineer

W. H. Odell, Director, Radiological Programs

  • S. R. Radebaugh, Assistant Plant Manager - Maintenance

R. L. Roberts, Electrical Maintenance Supervisor

,

  • L. W. Rougeux, Senior ISEG Engineer
  • J. P. Schippert, Plant Manager

B. R. Smith, Mechanical Maintenance Supervisor

M. A. Stein, Director - Plant Engineering

,

  • K. E. Suhrke, Manager, Site Support

!

W. J. Trudell, Assistant Operations Supervisor

J. E. Venable, Operations Supervisor

S. L. Woody, Director, Nuclear Station Security

  • Denotes personnel that attended the exit meeting.

In addition to the

.

'

personnel listed above, the inspectors contacted other personnel during this

inspection period.

,

0

,

.i-

,

I

-2-

l

.!

2 EXIT MEETING

I

An exit meeting was Lunducted On Jena 8. 1993. During this meeting, the

inspectors reviewed the scope and findings of the' report.

The licensee did

!

j

not identify as proprietary any information provided to, or reviewed by, the

inspectors.

'!

.!

}

i

'i

I

.

?

i

i

I

f

I

f

i

i

f

.

I

&

I

l

I

>

l

f

!

i

f

i

t

t

!

i

i

i

!

!

>

h

i

4

--.

_ ,

- .

I

.

s

.

!

ATTACHMENT 2-

APPENDlX A TO TI 2515/119

NRC Survey for Evaluating Operator Guidance

,

Docket Number:

50-458

Plant Name:

River Bend Station

'

Date Completed:

May 31, 1993

Inspector: Ward F. Smith

Yes

1.

Are licensed operators knowledgeable and capable of executing the

guidance discussed in the August 19, 1992, and October 16, 1992

letters from B. T Williamson II, Chairman of the BWROG Emergency

Procedures Committee (EPC) to all plant operations superintendents

(references 3 and 4)?

No

2.

Have licensed operators been provided other guidance in addition

to or in place of the above letters concerning this issue?

If

yes, provide discussion below.

Yes

3.

Have all licensed operators received classroom training on this

guidance?

If not, when will it be completed? February 19, 1993

.

No

4.

Have all licensed operators received simulator training on this

guidance?

If not, when will it be completed?

The operators have had simulator scenarios where upon loss of RPV

'

level indication, the E0P contingency for RPV ficoding was

entered.

.

.

No

5.

Does the licensee's plant simulator adequately model the failure

of reactor water level instrumentation to lead the operators to

enter the E0P contingency for RPV flooding?

No

6.

Have the contents of the above letters or similar guidance

consistent with this guidance been permanently incorporated into

licensee training programs for licensed operators?

If not, when

will this be completed?

,

The guidance was incorporated into the 2-year cycle

requalification training programs, and all existing licensed

,

'

operators were trained by February 19, 1993. The licensee had not

"

I

incorporated the guidance into initial training, as of this

inspection, but indicated plans to do so in time to support the

next initial training sequence which was scheduled to start in

June 1993.

No

7.

Does the licensee's continuing training program for licensed

operators include a dynamic simulator scenario for rapid plant

depressurization concurrent with reactor water level instrument

,

failures?

Yes

8.

Has the licensee checked the Emergency Operating Procedures (EOPs)

l

for inconsistencies with the above guidance?

.

r

.

i

_

-

'

>

6

-2-

No

9.

Wert any inconsistencies found by the licensee between the E0Ps

and the guidance?

If yes, what were the inconsistencies and have

they been resolved?

Yes

10.

Has the licensee taken or planned any actions to minimize the

likelihood of level indication errors, such as minimizing leakage

from the level instrumentation?

If yes, provide discussion below.

The licensee is considering a modification which would provide a

constant vent coming off the condensing pot to the main steam

header.

This is the most favored alternative at this time;

however, others are being looked at.

No

11.

Has the licensee experienced any level instrumentation anomalies

during depressurization?

If yes, provide discussion below.

A