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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C0821993-08-0303 August 1993 LER 93-012-00:on 930510,reported Unusual Noise Due to Small Frictional Force Release in RCS During heat-up.Developed & Implemented Enhanced Thermal Expansion Monitoring Program. W/930803 Ltr ML20045F1451993-06-30030 June 1993 LER 93-011-00:on 930518,nuclear Plant Instrumentation Sys Axial Flux Difference Limits Were Not Updated W/Ts Due to Inadequate Review of Colr.Initiated WR & Computer Software Mod request.W/930630 Ltr ML20044H0751993-06-0202 June 1993 LER 93-010-00:on 930508,Mode 3 Entered from Mode 4 W/Both MDAFWPs Rendered Inoperable by Handswitches Being Placed in pull-to-lock.Caused by Failure to Control Work Activity.Mgt Expectations clarified.W/930602 Ltr ML20045A4931993-06-0101 June 1993 LER 93-009-00:on 930504,noted That Supervising Operator Erroneously Instructed RO to Reset Steamline LP SI Signal Rather than Block SI Signal.Caused by Personnel Error. Personnel Have Been Directed to Review event.W/930601 Ltr ML20044D2821993-05-11011 May 1993 LER 93-007-00:on 930413,determined That Surveillance Test Procedure Re RHR Sys Inservice Pump B Test Not Accomplished by 930410.Caused by Lack of Oversight of Surveillance program.Past-due Notice proceduralized.W/930511 Ltr ML20045H2631992-12-31031 December 1992 LER 92-007-01:on 920326,hot Particle Discovered on Individual Left Cheek.Event Probably Occurred During Use of Plant Communications Equipment.Procedure RPP 02-510 Evaluated ML20045H2701992-04-27027 April 1992 LER 92-007-00:on 920326,hot Particle Picked Up During RCS Shim Restraint Rework Insp Results in Exposure Exceeding 10CFR20.101 Requirements.Hot Particle Control Program & Policies Being reviewed.W/920427 Ltr ML20024G9791991-05-10010 May 1991 LER 90-026-00:on 901123,tech Spec Violation Occurred Re Safety Related Class IE Battery Bank Powered from Spare Battery Charger.Caused by Error in Safety Evaluation for Procedure Mce E051Q-01.Procedure deleted.W/910510 Ltr ML20029B2361991-02-28028 February 1991 LER 91-025-01:on 901223,common Min Flow Path Return Line for SI Pumps to RWST Frozen.Caused by Faulty Ambient Temp Switch.Switches Calibr to Insure Heat Trace Circuits & Alarms activated.W/910228 Ltr ML20029A6481991-02-26026 February 1991 LER 91-002-00:on 910128,essential Svc Water Flow to Containment Cooling Units Below TS 4.6.2.3 Requirements of 4,000 Gpm.Caused by Inaccurate Flow Readings Provided by Local Annubars.Surveillance Procedure revised.W/910226 Ltr ML20028H6901991-01-22022 January 1991 LER 90-025-00:on 901223,determined That Common Min Flow Path Return Line for SI Pumps to Refueling Water Storage Tank Frozen.Cause Undetermined.Need for Effective Communications Will Be Reiterated to Plant personnel.W/910122 Ltr ML20028H4361990-12-28028 December 1990 LER 90-024-00:on 901129,portion of Contents of Waste Gas Decay Tank 6 Discharged While Maint Performed.Caused by Personnel Error.Shift Supervisor counseled.W/901228 Ltr ML20028G9191990-09-26026 September 1990 LER 90-020-00:on 900827,portable Sump Pump Installed W/Pump Discharge Directed to Storm Drains,Bypassing Turbine Bldg Drain Monitor LE-RE-59.Caused by Lack of Communication Between Involved groups.W/900926 Ltr ML20043H7201990-06-18018 June 1990 LER 90-012-00:on 900517,reactor Trip,Main Turbine Trip & Auxiliary Feedwater Actuation Signals Occurred.Caused by Steam Generator C Atmospheric Dump Valve Stuck Open. Converter Positioner Circuitry replaced.W/900618 Ltr ML20043H1531990-06-18018 June 1990 LER 90-013-00:on 900519,main Turbine Trip Occurred as Result of hi-hi Moisture Separator Reheater Level.Root Cause Investigation Not Conclusive.Cautions Added to General Operating Procedure Gen 00-004.W/900618 Ltr ML20043G2761990-06-15015 June 1990 LER 90-010-00:on 900516,discovered That Insp Access Door for Motor Driven Auxiliary Feedwater Pump B Room Cooler Had Been Removed.Caused by Personnel Error.Maint Personnel Informed of Necessity of Doors Being in place.W/900615 Ltr ML20043G0741990-06-13013 June 1990 LER 90-011-00:on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure revised.W/900613 Ltr ML20043G1991990-06-0808 June 1990 LER 90-007-00:on 900510,feedwater Isolation Signal Occurred Due to Surveillance Test Requiring High Feed Rate.Caused by Feedwater Flow Rate Higher than Steam Flow.Rev to Surveillance Test Procedures clarified.W/900608 Ltr ML20043E9551990-06-0808 June 1990 LER 90-009-00:on 900608,discovered That Circuit Breakers for Accumulator Outlet IV Closed Resulting in Two Inoperable Accumulators.Caused by Personnel Error & Lack of Specific Procedural Direction.Procedure revised.W/900608 Ltr ML20043F1581990-06-0404 June 1990 LER 90-008-00:on 900504,fuel Bldg/Control Room Ventilation Isolation Signals Received from Exhaust Radiation Monitor. Caused by Burned Out Lamp & Blown Fuse in Power Supply.Fuse & Lamp Replaced & Monitor Returned to svc.W/900604 Ltr ML20043A6731990-05-16016 May 1990 LER 90-006-00:on 900416,containment Purge Isolation Signal & Control Room Ventilation Isolation Signal Occurred.Caused by Inadequate Procedures to Govern Deenergization of 120- Volt Ac Distribution Ctrs.Procedures revised.W/900516 Ltr ML20042G9171990-05-10010 May 1990 LER 90-005-00:on 900410,control Bldg/Auxiliary Bldg Pressure Boundary Door Found Open W/O Continuous Watch Established. Caused by Inadequate Procedures.Fire Protection Impairment Control Procedure revised.W/900510 Ltr ML20042G2131990-05-0707 May 1990 LER 90-004-00:on 900405,Tech Spec Surveillance Requirement Not Satisfied Because of Personnel Error in Scheduling Surveillance Test.Procedure Adm 02-300 revised.W/900507 Ltr ML20042E1851990-04-13013 April 1990 LER 90-002-00:on 900314,determined That Halon Release in Either ESF Switchgear Room Would Trip Both Class 1E Electrical Equipment Air Conditioning Units.Caused by Lack of Design Criteria.Criteria revised.W/900413 Ltr ML20043H2871990-04-0909 April 1990 Corrected LER 85-058-01:on 850731,reactor Trip,Main Turbine Trip,Auxiliary Feedwater Actuation,Feedwater Isolation & Steam Generator Blowdown & Sample Isolation Occurred.Caused by Faulty Power Supply to Channel.Power Replaced ML20012B4331990-03-0808 March 1990 LER 90-001-00:on 900206,reactor Tripped as Result of Loop Low Flow Condition Following Trip of Reactor Coolant Pump a, Causing Feedwater Isolation & Auxiliary Feedwater Actuation Signals.Caused by High Differential current.W/900308 Ltr ML20012B4741990-03-0505 March 1990 LER 88-007-01:on 880513,determined That Procedures for Setting Trip Point for Overpower & Overtemp Differential Instrument Loops Did Not Require Setpoints to Be Reset Conservatively.Setpoints recalculated.W/900305 Ltr ML20011D4391989-12-18018 December 1989 LER 89-020-00:on 891117,determined That as-built Configuration of Housing for Both Trains of Containment Cooling Fan HXs Not Seismically Qualified to Withstand Sse. Addl Seismic Restraints installed.W/891218 Ltr ML19332F9111989-12-14014 December 1989 LER 89-021-03:on 881025,preliminary Investigations Indicated That Containment Cooling Fan B Could Not Be Relied on to Perform Intended Design Function.Motor Overcurrent Condition Existed Since installation.W/891214 Ltr ML19325D5261989-10-18018 October 1989 LER 89-019-00:on 890919,determined That No Procedural Problem Existed & Equipment Problem Caused 890915 Test Deficiency.Caused by Reaching Incorrect Conclusion.Train Restored to Svc After Replacement of relay.W/891018 Ltr ML19341D8071988-01-15015 January 1988 LER 87-056-00:on 871215,one 400 Uci Sr-90/Y-90 Source Could Not Be Located.Caused by Inadequate Control of Licensed matl.Fan-Shaped Apparatuses Removed from Svc to Prevent recurrence.W/880115 Ltr 1993-08-03
[Table view] Category:RO)
MONTHYEARML20046C0821993-08-0303 August 1993 LER 93-012-00:on 930510,reported Unusual Noise Due to Small Frictional Force Release in RCS During heat-up.Developed & Implemented Enhanced Thermal Expansion Monitoring Program. W/930803 Ltr ML20045F1451993-06-30030 June 1993 LER 93-011-00:on 930518,nuclear Plant Instrumentation Sys Axial Flux Difference Limits Were Not Updated W/Ts Due to Inadequate Review of Colr.Initiated WR & Computer Software Mod request.W/930630 Ltr ML20044H0751993-06-0202 June 1993 LER 93-010-00:on 930508,Mode 3 Entered from Mode 4 W/Both MDAFWPs Rendered Inoperable by Handswitches Being Placed in pull-to-lock.Caused by Failure to Control Work Activity.Mgt Expectations clarified.W/930602 Ltr ML20045A4931993-06-0101 June 1993 LER 93-009-00:on 930504,noted That Supervising Operator Erroneously Instructed RO to Reset Steamline LP SI Signal Rather than Block SI Signal.Caused by Personnel Error. Personnel Have Been Directed to Review event.W/930601 Ltr ML20044D2821993-05-11011 May 1993 LER 93-007-00:on 930413,determined That Surveillance Test Procedure Re RHR Sys Inservice Pump B Test Not Accomplished by 930410.Caused by Lack of Oversight of Surveillance program.Past-due Notice proceduralized.W/930511 Ltr ML20045H2631992-12-31031 December 1992 LER 92-007-01:on 920326,hot Particle Discovered on Individual Left Cheek.Event Probably Occurred During Use of Plant Communications Equipment.Procedure RPP 02-510 Evaluated ML20045H2701992-04-27027 April 1992 LER 92-007-00:on 920326,hot Particle Picked Up During RCS Shim Restraint Rework Insp Results in Exposure Exceeding 10CFR20.101 Requirements.Hot Particle Control Program & Policies Being reviewed.W/920427 Ltr ML20024G9791991-05-10010 May 1991 LER 90-026-00:on 901123,tech Spec Violation Occurred Re Safety Related Class IE Battery Bank Powered from Spare Battery Charger.Caused by Error in Safety Evaluation for Procedure Mce E051Q-01.Procedure deleted.W/910510 Ltr ML20029B2361991-02-28028 February 1991 LER 91-025-01:on 901223,common Min Flow Path Return Line for SI Pumps to RWST Frozen.Caused by Faulty Ambient Temp Switch.Switches Calibr to Insure Heat Trace Circuits & Alarms activated.W/910228 Ltr ML20029A6481991-02-26026 February 1991 LER 91-002-00:on 910128,essential Svc Water Flow to Containment Cooling Units Below TS 4.6.2.3 Requirements of 4,000 Gpm.Caused by Inaccurate Flow Readings Provided by Local Annubars.Surveillance Procedure revised.W/910226 Ltr ML20028H6901991-01-22022 January 1991 LER 90-025-00:on 901223,determined That Common Min Flow Path Return Line for SI Pumps to Refueling Water Storage Tank Frozen.Cause Undetermined.Need for Effective Communications Will Be Reiterated to Plant personnel.W/910122 Ltr ML20028H4361990-12-28028 December 1990 LER 90-024-00:on 901129,portion of Contents of Waste Gas Decay Tank 6 Discharged While Maint Performed.Caused by Personnel Error.Shift Supervisor counseled.W/901228 Ltr ML20028G9191990-09-26026 September 1990 LER 90-020-00:on 900827,portable Sump Pump Installed W/Pump Discharge Directed to Storm Drains,Bypassing Turbine Bldg Drain Monitor LE-RE-59.Caused by Lack of Communication Between Involved groups.W/900926 Ltr ML20043H7201990-06-18018 June 1990 LER 90-012-00:on 900517,reactor Trip,Main Turbine Trip & Auxiliary Feedwater Actuation Signals Occurred.Caused by Steam Generator C Atmospheric Dump Valve Stuck Open. Converter Positioner Circuitry replaced.W/900618 Ltr ML20043H1531990-06-18018 June 1990 LER 90-013-00:on 900519,main Turbine Trip Occurred as Result of hi-hi Moisture Separator Reheater Level.Root Cause Investigation Not Conclusive.Cautions Added to General Operating Procedure Gen 00-004.W/900618 Ltr ML20043G2761990-06-15015 June 1990 LER 90-010-00:on 900516,discovered That Insp Access Door for Motor Driven Auxiliary Feedwater Pump B Room Cooler Had Been Removed.Caused by Personnel Error.Maint Personnel Informed of Necessity of Doors Being in place.W/900615 Ltr ML20043G0741990-06-13013 June 1990 LER 90-011-00:on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure revised.W/900613 Ltr ML20043G1991990-06-0808 June 1990 LER 90-007-00:on 900510,feedwater Isolation Signal Occurred Due to Surveillance Test Requiring High Feed Rate.Caused by Feedwater Flow Rate Higher than Steam Flow.Rev to Surveillance Test Procedures clarified.W/900608 Ltr ML20043E9551990-06-0808 June 1990 LER 90-009-00:on 900608,discovered That Circuit Breakers for Accumulator Outlet IV Closed Resulting in Two Inoperable Accumulators.Caused by Personnel Error & Lack of Specific Procedural Direction.Procedure revised.W/900608 Ltr ML20043F1581990-06-0404 June 1990 LER 90-008-00:on 900504,fuel Bldg/Control Room Ventilation Isolation Signals Received from Exhaust Radiation Monitor. Caused by Burned Out Lamp & Blown Fuse in Power Supply.Fuse & Lamp Replaced & Monitor Returned to svc.W/900604 Ltr ML20043A6731990-05-16016 May 1990 LER 90-006-00:on 900416,containment Purge Isolation Signal & Control Room Ventilation Isolation Signal Occurred.Caused by Inadequate Procedures to Govern Deenergization of 120- Volt Ac Distribution Ctrs.Procedures revised.W/900516 Ltr ML20042G9171990-05-10010 May 1990 LER 90-005-00:on 900410,control Bldg/Auxiliary Bldg Pressure Boundary Door Found Open W/O Continuous Watch Established. Caused by Inadequate Procedures.Fire Protection Impairment Control Procedure revised.W/900510 Ltr ML20042G2131990-05-0707 May 1990 LER 90-004-00:on 900405,Tech Spec Surveillance Requirement Not Satisfied Because of Personnel Error in Scheduling Surveillance Test.Procedure Adm 02-300 revised.W/900507 Ltr ML20042E1851990-04-13013 April 1990 LER 90-002-00:on 900314,determined That Halon Release in Either ESF Switchgear Room Would Trip Both Class 1E Electrical Equipment Air Conditioning Units.Caused by Lack of Design Criteria.Criteria revised.W/900413 Ltr ML20043H2871990-04-0909 April 1990 Corrected LER 85-058-01:on 850731,reactor Trip,Main Turbine Trip,Auxiliary Feedwater Actuation,Feedwater Isolation & Steam Generator Blowdown & Sample Isolation Occurred.Caused by Faulty Power Supply to Channel.Power Replaced ML20012B4331990-03-0808 March 1990 LER 90-001-00:on 900206,reactor Tripped as Result of Loop Low Flow Condition Following Trip of Reactor Coolant Pump a, Causing Feedwater Isolation & Auxiliary Feedwater Actuation Signals.Caused by High Differential current.W/900308 Ltr ML20012B4741990-03-0505 March 1990 LER 88-007-01:on 880513,determined That Procedures for Setting Trip Point for Overpower & Overtemp Differential Instrument Loops Did Not Require Setpoints to Be Reset Conservatively.Setpoints recalculated.W/900305 Ltr ML20011D4391989-12-18018 December 1989 LER 89-020-00:on 891117,determined That as-built Configuration of Housing for Both Trains of Containment Cooling Fan HXs Not Seismically Qualified to Withstand Sse. Addl Seismic Restraints installed.W/891218 Ltr ML19332F9111989-12-14014 December 1989 LER 89-021-03:on 881025,preliminary Investigations Indicated That Containment Cooling Fan B Could Not Be Relied on to Perform Intended Design Function.Motor Overcurrent Condition Existed Since installation.W/891214 Ltr ML19325D5261989-10-18018 October 1989 LER 89-019-00:on 890919,determined That No Procedural Problem Existed & Equipment Problem Caused 890915 Test Deficiency.Caused by Reaching Incorrect Conclusion.Train Restored to Svc After Replacement of relay.W/891018 Ltr ML19341D8071988-01-15015 January 1988 LER 87-056-00:on 871215,one 400 Uci Sr-90/Y-90 Source Could Not Be Located.Caused by Inadequate Control of Licensed matl.Fan-Shaped Apparatuses Removed from Svc to Prevent recurrence.W/880115 Ltr 1993-08-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station ML20236P3441998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Wolf Creek Generating Station ML20236P3481998-05-31031 May 1998 Corrected Page of MOR for May 1998 for Wolf Creek Generating Station ML20249A0171998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Wolf Creek Generating Station ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247H0901998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Wolf Creek Generating Station ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20216F6101998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Wolf Creek Generating Station ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20216G1971998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Wolf Creek Nuclear Operating Corp ML20202H0721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Wolf Creek Generating Station ML20217G4311997-12-31031 December 1997 Western Resources 1997 Annual Rept & Financial Statements for Years Ended 971231 & 1996 for Ks Electric Power Cooperative,Inc ML20203H0151997-12-31031 December 1997 Annual Operating Rept 13 for Jan-Dec 1997 ML20217G3711997-12-31031 December 1997 Kansas City Power & Light Co 1997 Annual Rept ML20216D7771997-12-31031 December 1997 Annual SER 12 for Jan-Dec 1997, for Wolf Creek Generating Station 1999-09-30
[Table view] |
Text
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l W4M.F CREEK NUCLEAR OPERATING CORPORATION ~ i L' John A. Belley Vlee Present Nucteer Operatione
{
i i
May 16,1990 :
N0 90-0158-
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l
'U. S. Nuclear Regulatory Commission ATTN: Document Control Desk
, Mail Station F1-137 Washington, D. C. 20555 l
Subject:
Docket No. 50-482: Licensee Event: Report 90-006-00 1
Gentlemen: !
The attached Licensee Event Report (LER) . is being submftted. pursuant to ;
10 CFR 50.73 (a) (2) (i) concerning a Technical Specification violation', and pursuant to 10 CFR 50.73(a)(2)(iv) concerning acplanned' actuations of
, Engineered Safety Features.
Very truly youre,- l l
- j V . A John A. Bailey
/
Vice~ President
, Nuclear Operations -l
-1 JAB /jra
. Attachment 1 j
cc R. D. Martin (HRC), w/a D. Persinko (NRC), w/a D. V. Pickett-(NRC), w/a '-
M. E. Skov (NRC), w/a .1 I
p Ov'5 E p.s }6 q Kif*S l c _ 'l F[lR H LIU LJ . ( F it it it 14 t ,_
y k'[li[
RO. Box 411/ Burlington, KS 66839 / Phone:(316) 364-8831 An Equal opportunity F.mployer MF/HCNET I i
e a.C perm 364 CSM U.5 NUCLEAR REOULa10AY COMMl5510N APPROVID OMS NO 3150 0104 I
LICENSEE EVENT REPORT (LER) '"at'"
7 ACILITY NAME (1) DOCKET NUMBE R (2) FAGE iY i Wolf Creek Generatin(StaLion o l5 l o j o l 0 l 418 l 2 1lOFl0l5 Engineered Safety Features Equipment Actuations and Technical Specification Violation Caused By Jnadequate Procedural Guidance i tVENT DATE (81 LER NUMetR ($1 REPORT DATE in OTMtR F ACILITit$ INVOtVED 10)
MONTH DAY YEAR Y&AR "*[ L" ' N,$ MONT H DAY YEAR F ACsLITv hauts DOCKET NUM8tRtSt ol5l0lolot l l l!6
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O!4 9 0 9l 0 0l 0! 6 0l 0 0l5 1 l6 9!0 oistoioici i i OPE R ATING THis REPORT is SUBMITTED PURSUANT TO TMt REO' UIREMEN1'8 GP 10 C7 R { (Chece one er enore of the tonovati(11)
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LICENSEE CONT ACT FOR THl3 LER 112)
NAME TELEPHONE NUMBER ARE A COD 4 Merlin G. Williams - Manager Plant Support 3 l1 16 361 14 l- 1 8 l 8l3 l 1 COMPLETE ONE LINE FOR E ACH COMPONENT f AILURE OtSCRIBED IN THIS REPORT (13}
CAUSE 8v$'EM COMPONENT MA%AC.
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I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 114) MONTH DAY YFAR SU8 MIS $10N YtS ill yen. cameter. tx9ECTf0 5V06t!SSION CA TEI No l l l 1.. T R ACT a- . ,m c.u . . w ,,N ,, ,s.,wc, ,,-., ,,,,,,, n.>
On April 16,1990, at 0819 CDT, a Containment Purge Isolation Signal and a Control Rom Ventilation Isolation Signal (CRVIS) occurred when power es renoved fran Containment Purge Radiation Monitor GP RE-33. As a result of this event it me discovered that the 'B' train Control Room Pressurization Fan OGK04B had not been restored to service prior to declaring the 'B' train Control Rom Emergency Ventilation Systen operable, resulting in a violation of Technical Specification 3.7.6. CGK04B was restored to service at approximately 0847 CDT. At 2140 CDP, another CRVIS occurred when signal power ws renoved fran Control Rom Air Intake Chlorine Monitor, GK AIT-2.
All required equipnent responded properly.
These Engineered Safety Features equipnent actuations occurred when the associated 120 volt A.C. distribution center a s de-energized for Refueling activities without placing all affected instruments in the bypass position.
'lhe root cause of these events es inadequate pro :iures to govern de-energization of individual 120 volt A.C. distribution centers. Appus-iate procedures are being developed. OGK04B had not been restored to service
~
following the electrical bus maintenance because of procedural ambiguity. A s ucelure change has been initiated to clarify this procedure.
N C Poem 306 q
_ _ _ _ _ )
)
NRC POAW 3e6A U.S. ICUCL4A2 A53ULATU.sY Coeduiss10N EXPIRts 473oM2 UCENSEE EVENT REPORT (LER) f,Ns'd',%',f"80,'C4",o"'AIS*f,2 ,,o* 'l'TA' !R,l'd's .,
TEXT CONTINUATlON Su "",f."/o'#%%"d5,'UW'C0'*/l#l,"'"'8 "f! !
E PAPE WO RG U T ON 3 04 i 07 MANAGEMENT ANL18UDGET, WASHINGTON,DC 20503.
pJ.CitiTV NAM 6 IH DOCKET NUMBER ul LtR NUMSER 16) PA05 13) vsAa -
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TEXT (# ruere spece a ,evosett, use : MAC form Jests / 07) i e i On April 16,1990, at 0819 CDP, a Containment Purge Isolation Signal (CPIS) }
and a Control Room Ventilation Isolation Signal (CRVIS) occurred when povar }
was removed from Contalment Purge Radiation Monitor GT RE-33 [IIrle). As a result of this event, it was discovered that the 'B' train Control Rom 4 Pressurization Fan CGK04B [VI-FAN]- had' not been restored to service prior to .i declaring the 'B' train Control Roan Bnergency Ventilation Syistem oper.able,
'resulting in a violation of 'Dochnical Specification 3.7.6. At 2140 C M ,- .
another CRVIS occurred when signal power.was removed from Control Rean Air Intake Chlorine Monitor, GK AIT-2 [VI-AIT). 'Ihis report is being robnitted pursuant to 10 CFR 50.73(a)(2)(iv) concerning unplanned actuatione.of Engineered Safety Features (ESF) [JE] equipnent, and pursuant to 10 CFR 50.73(a)(2)(1) concerning a condition prohibited-by Technical:
Specifications.
DIEKRIPTIGT T EVEBRS At the time of these events, the plant was in Mode 6, Refueling, with the #
Reactor Coolant System [AB) average t=am m ture at 82 degrees. Fahrenheit. ,
Ta'annmry power was being supplied to the 120 volt A.C. Class 1E '
distribution centers. On the norning of April 16, propmtions were in i g upass to restore the 120 volt A.C. Class 1E distribution centers to their normal power supply following maintenance activities. In preparation for removal of tangnmry power to the distribution centers, several instruments required placement in the bypass position to prevent unnamaaey actuations of ESF equipnent when power was renoved. . At 0740 CDT on April- 16, the .
Control Roan Air Intake Radiation Monitor GK RE-04 [IIeM21], the Contalment Atmosphere Radiation Monitor GT RE-31 [IL-lG), the Fuel Building Exhaust.
Radiation Monitor GG RE-28 [IIrMJN), and GK. AIT-2.were placed in the bypass position. Entry was made into the app usiate Technical Specification-Action Statements. At 0819 CDP, a CPIS and a CRVIS occurred as a result of loss of power to GT RE-33 when .the tenporary power was renoved. GT RE-33 had not been placed in bypass along with the other affected instruments, and upon loss of power, an actuation signal was generated as required by the design of the monitor.
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At 0840 CDT, nozmal power ma restored to the affected instruments, and at approxinately 0847 CDP, restoration of the Control Roczn Ventilation System i (VI) to nonnal configuration began. During this s ucess, it e s discovered that the 'B' train Control Room Pressurization Fan OGK04B (VI-FAN) had not 3 started because its handswitch a s in pull-to-lock. Following this l discovery, CGK04B es restored to q=mble status. . All other required i equipnent responded sply to the actuation signals. At 0910 CDT, restoration fram the actuation signals ma ccmpleted.
Subsequent investigation revealed that the handswitch for CGK04B had been placed in pull-to-lock on April 7, 1990, as part of the 'B' train Class lE electrical bus outage, rendering the 'B' train Control Room Bnergency Ventilation Systen inoperable. Technical Specification 3.7.6 requires that with one train of the control Rom Emergency Ventilation System inoperable, to restore it to operable status within.7 days or to initiate and maintain 1 operation of the reaining train in.the recirculation node. Between April 7, 1990 and April 16,1990 at 0300 CDP, this Action Statement was satisfied. On April 16,1990, at 0300 CDP, Control Rom operators -realigned the Control Rom Dnergency Ventilation System frm.the recirculation mode to the normal configuration upon restoration of the 'B' train. Control Rom Air Conditioning Unit [VI-ACU) to service. The Action Statement of Technical Specification 3.7.6 m s exited at that time. It me not recognized that .
OGK04B should also be returned to service as required for q=mhility of the
'B' train Control Room Emergency Ventilation System. At the time, the "
Control Rom operators did not recognize that a non-14ance with Technical' Specifications had occurred.
At 2140 CUT on April 16, 1990, 120 volt A.C. Class 1E Distribution Center NN04 [EF-BUS) was Imoved frun service for cleaning. When NN04 was de-energized, a CRVIS occurred because of a loss of signal power to GK AIT-2.
When the signal power es lost, the monitor failed low and initiated an ESF actuation as required by the design of the nonitor. All equipment responded properly to the CRVIS. At approximately 2145 CDP, GK AIT-2 m s placed in the bypass position. At 2207 CDP, the Control Rom Ventilation Systen was restored to normal configuration. NN04 was re-energized at 0244' CDP on April 17, 1990, and GK AIT-2 was restored to service at 0248 CDP.
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%e root cause of these events was the failure to have adequate prMwes i to govern de-energization of-inctividual 120 volt A.C. distribution centers. l System operating gvwdure SYS G331, "De-energization of 480 volt Class 1E Bus (es)," is utilized to de-energize the notor control centers supplying the -
120 volt A.C. distribution centers. When the 120 volt A.C. distribution -
centers were originally de-energized to allow the installation of taiporary power, this suce. lure a s utilized, and consequently, no unnecessary ESF actuations resulted. %is procedure identifies the actions to be taken to '
de-energize entire motor control centers to prevent unnecessary ESF actuations, but does not specify those actions which are specific to a ,
particular 120 volt A.C. distribution center. Upon conclusion of the 480 >
volt A.C. bus outage, the t-vary power supply was -left installed to the 1 120 volt' A.C. distribution centers. When subsequently pramvNg to renove '
the tarporary power supply, the anu.vslate instruments were not placed in' bypass and unnecessary ESF actuations resulted when the associated distribution center was de-energized. While SYS E 331 contained )
information relative to the distribution centars, it was not recognized that this information could be selectively applied to individual 120 volt A.C.
distribution centers. To preclude recurrence,la procedure for de-energizing aan.vgiate 120 volt A.C. distribution centers will be developed prior to ,
the next scheduled 120 volt A.C. distribution center dewanergization. '
Investigations were conducted to determine the reason that CGK04B was not restored to service along with SGK04B at 0300 CDT on April 16, 1990. ..It was determined that during the re-energization of the 480 volt A.C. notor control centers, the handswitch for CGK04B ms left in pull-to-lock because of a lack of clarity in system operating procedure SYS !G-131, ."Energization.
of 480 volt Class 1E Bus (es)". W e applicable procedural step states that CGK04B and SGK04B should be restored to service utilizing the aan.vgiate procedure. mis step was interpreted to mean that .CGK04B and SGK04B should 1
[ be restored concurrently. Because SGK04B was to renain out of service for unrelated activities, the Control Room operators left CGK04B out of service.
in accordance with their understanding of t M procedure. When SGK04B was >
restored to service on April 16, 1990, at 0300 CDT, it was not recognized that CGK04B required restoration also. A clarification to SYS G 331~has l been initiated to no longer require placement of CGK04B in pull-to-lock prior to de-energization of the associated 480 volt A.C. bus. A revision to SYS E131 has also been initiated to list restoration of CGK04B and'SGK04B. !
as separate sign off steps to ensure personnel are aware that the um s ments T may be restored separately. %ese changes will be issued prior to June 30, ,
1990. !
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OF MANAGEMENT AND 9UDOtt, WASHINGTON,0C 20503 PkCILif y NAMt 11 DOCKET NUMttR 121 LER NUMetR 161 PAS 8131 YE*" n adI aYa Wolf Creek Generating Station o l5 l0 l0 j o l 4l8 l2 9 l 0 ,0 l0l6 -
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- A previous similar occurrence of unnecessary ESF actuations which resulted fran a lack of gvcisdural guidance for de-energization of electrical equipnent is discussed in Licensee Event Report 87-049-00. In response to that event, a procedure e s developed for de-energizing safety related'4.16 i kilovolt division buses. However, prior to the events discussed in this report, it was believed that the gvcx. dure governing de-energization of the entire 480 volt Class 1E notor control center provided sufficient guidance I for de-energization of 120 volt A.C. distribution centers.
In each of the events discussed in this report, the plant was in a stable shutdown condition thereby the occurrence of these events-did not pose a- '
threat to the health and safety of the public or u.m p unise safe plant operation. ,
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s NXC Form 365A 16401