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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C0821993-08-0303 August 1993 LER 93-012-00:on 930510,reported Unusual Noise Due to Small Frictional Force Release in RCS During heat-up.Developed & Implemented Enhanced Thermal Expansion Monitoring Program. W/930803 Ltr ML20045F1451993-06-30030 June 1993 LER 93-011-00:on 930518,nuclear Plant Instrumentation Sys Axial Flux Difference Limits Were Not Updated W/Ts Due to Inadequate Review of Colr.Initiated WR & Computer Software Mod request.W/930630 Ltr ML20044H0751993-06-0202 June 1993 LER 93-010-00:on 930508,Mode 3 Entered from Mode 4 W/Both MDAFWPs Rendered Inoperable by Handswitches Being Placed in pull-to-lock.Caused by Failure to Control Work Activity.Mgt Expectations clarified.W/930602 Ltr ML20045A4931993-06-0101 June 1993 LER 93-009-00:on 930504,noted That Supervising Operator Erroneously Instructed RO to Reset Steamline LP SI Signal Rather than Block SI Signal.Caused by Personnel Error. Personnel Have Been Directed to Review event.W/930601 Ltr ML20044D2821993-05-11011 May 1993 LER 93-007-00:on 930413,determined That Surveillance Test Procedure Re RHR Sys Inservice Pump B Test Not Accomplished by 930410.Caused by Lack of Oversight of Surveillance program.Past-due Notice proceduralized.W/930511 Ltr ML20045H2631992-12-31031 December 1992 LER 92-007-01:on 920326,hot Particle Discovered on Individual Left Cheek.Event Probably Occurred During Use of Plant Communications Equipment.Procedure RPP 02-510 Evaluated ML20045H2701992-04-27027 April 1992 LER 92-007-00:on 920326,hot Particle Picked Up During RCS Shim Restraint Rework Insp Results in Exposure Exceeding 10CFR20.101 Requirements.Hot Particle Control Program & Policies Being reviewed.W/920427 Ltr ML20024G9791991-05-10010 May 1991 LER 90-026-00:on 901123,tech Spec Violation Occurred Re Safety Related Class IE Battery Bank Powered from Spare Battery Charger.Caused by Error in Safety Evaluation for Procedure Mce E051Q-01.Procedure deleted.W/910510 Ltr ML20029B2361991-02-28028 February 1991 LER 91-025-01:on 901223,common Min Flow Path Return Line for SI Pumps to RWST Frozen.Caused by Faulty Ambient Temp Switch.Switches Calibr to Insure Heat Trace Circuits & Alarms activated.W/910228 Ltr ML20029A6481991-02-26026 February 1991 LER 91-002-00:on 910128,essential Svc Water Flow to Containment Cooling Units Below TS 4.6.2.3 Requirements of 4,000 Gpm.Caused by Inaccurate Flow Readings Provided by Local Annubars.Surveillance Procedure revised.W/910226 Ltr ML20028H6901991-01-22022 January 1991 LER 90-025-00:on 901223,determined That Common Min Flow Path Return Line for SI Pumps to Refueling Water Storage Tank Frozen.Cause Undetermined.Need for Effective Communications Will Be Reiterated to Plant personnel.W/910122 Ltr ML20028H4361990-12-28028 December 1990 LER 90-024-00:on 901129,portion of Contents of Waste Gas Decay Tank 6 Discharged While Maint Performed.Caused by Personnel Error.Shift Supervisor counseled.W/901228 Ltr ML20028G9191990-09-26026 September 1990 LER 90-020-00:on 900827,portable Sump Pump Installed W/Pump Discharge Directed to Storm Drains,Bypassing Turbine Bldg Drain Monitor LE-RE-59.Caused by Lack of Communication Between Involved groups.W/900926 Ltr ML20043H7201990-06-18018 June 1990 LER 90-012-00:on 900517,reactor Trip,Main Turbine Trip & Auxiliary Feedwater Actuation Signals Occurred.Caused by Steam Generator C Atmospheric Dump Valve Stuck Open. Converter Positioner Circuitry replaced.W/900618 Ltr ML20043H1531990-06-18018 June 1990 LER 90-013-00:on 900519,main Turbine Trip Occurred as Result of hi-hi Moisture Separator Reheater Level.Root Cause Investigation Not Conclusive.Cautions Added to General Operating Procedure Gen 00-004.W/900618 Ltr ML20043G2761990-06-15015 June 1990 LER 90-010-00:on 900516,discovered That Insp Access Door for Motor Driven Auxiliary Feedwater Pump B Room Cooler Had Been Removed.Caused by Personnel Error.Maint Personnel Informed of Necessity of Doors Being in place.W/900615 Ltr ML20043G0741990-06-13013 June 1990 LER 90-011-00:on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure revised.W/900613 Ltr ML20043G1991990-06-0808 June 1990 LER 90-007-00:on 900510,feedwater Isolation Signal Occurred Due to Surveillance Test Requiring High Feed Rate.Caused by Feedwater Flow Rate Higher than Steam Flow.Rev to Surveillance Test Procedures clarified.W/900608 Ltr ML20043E9551990-06-0808 June 1990 LER 90-009-00:on 900608,discovered That Circuit Breakers for Accumulator Outlet IV Closed Resulting in Two Inoperable Accumulators.Caused by Personnel Error & Lack of Specific Procedural Direction.Procedure revised.W/900608 Ltr ML20043F1581990-06-0404 June 1990 LER 90-008-00:on 900504,fuel Bldg/Control Room Ventilation Isolation Signals Received from Exhaust Radiation Monitor. Caused by Burned Out Lamp & Blown Fuse in Power Supply.Fuse & Lamp Replaced & Monitor Returned to svc.W/900604 Ltr ML20043A6731990-05-16016 May 1990 LER 90-006-00:on 900416,containment Purge Isolation Signal & Control Room Ventilation Isolation Signal Occurred.Caused by Inadequate Procedures to Govern Deenergization of 120- Volt Ac Distribution Ctrs.Procedures revised.W/900516 Ltr ML20042G9171990-05-10010 May 1990 LER 90-005-00:on 900410,control Bldg/Auxiliary Bldg Pressure Boundary Door Found Open W/O Continuous Watch Established. Caused by Inadequate Procedures.Fire Protection Impairment Control Procedure revised.W/900510 Ltr ML20042G2131990-05-0707 May 1990 LER 90-004-00:on 900405,Tech Spec Surveillance Requirement Not Satisfied Because of Personnel Error in Scheduling Surveillance Test.Procedure Adm 02-300 revised.W/900507 Ltr ML20042E1851990-04-13013 April 1990 LER 90-002-00:on 900314,determined That Halon Release in Either ESF Switchgear Room Would Trip Both Class 1E Electrical Equipment Air Conditioning Units.Caused by Lack of Design Criteria.Criteria revised.W/900413 Ltr ML20043H2871990-04-0909 April 1990 Corrected LER 85-058-01:on 850731,reactor Trip,Main Turbine Trip,Auxiliary Feedwater Actuation,Feedwater Isolation & Steam Generator Blowdown & Sample Isolation Occurred.Caused by Faulty Power Supply to Channel.Power Replaced ML20012B4331990-03-0808 March 1990 LER 90-001-00:on 900206,reactor Tripped as Result of Loop Low Flow Condition Following Trip of Reactor Coolant Pump a, Causing Feedwater Isolation & Auxiliary Feedwater Actuation Signals.Caused by High Differential current.W/900308 Ltr ML20012B4741990-03-0505 March 1990 LER 88-007-01:on 880513,determined That Procedures for Setting Trip Point for Overpower & Overtemp Differential Instrument Loops Did Not Require Setpoints to Be Reset Conservatively.Setpoints recalculated.W/900305 Ltr ML20011D4391989-12-18018 December 1989 LER 89-020-00:on 891117,determined That as-built Configuration of Housing for Both Trains of Containment Cooling Fan HXs Not Seismically Qualified to Withstand Sse. Addl Seismic Restraints installed.W/891218 Ltr ML19332F9111989-12-14014 December 1989 LER 89-021-03:on 881025,preliminary Investigations Indicated That Containment Cooling Fan B Could Not Be Relied on to Perform Intended Design Function.Motor Overcurrent Condition Existed Since installation.W/891214 Ltr ML19325D5261989-10-18018 October 1989 LER 89-019-00:on 890919,determined That No Procedural Problem Existed & Equipment Problem Caused 890915 Test Deficiency.Caused by Reaching Incorrect Conclusion.Train Restored to Svc After Replacement of relay.W/891018 Ltr ML19341D8071988-01-15015 January 1988 LER 87-056-00:on 871215,one 400 Uci Sr-90/Y-90 Source Could Not Be Located.Caused by Inadequate Control of Licensed matl.Fan-Shaped Apparatuses Removed from Svc to Prevent recurrence.W/880115 Ltr 1993-08-03
[Table view] Category:RO)
MONTHYEARML20046C0821993-08-0303 August 1993 LER 93-012-00:on 930510,reported Unusual Noise Due to Small Frictional Force Release in RCS During heat-up.Developed & Implemented Enhanced Thermal Expansion Monitoring Program. W/930803 Ltr ML20045F1451993-06-30030 June 1993 LER 93-011-00:on 930518,nuclear Plant Instrumentation Sys Axial Flux Difference Limits Were Not Updated W/Ts Due to Inadequate Review of Colr.Initiated WR & Computer Software Mod request.W/930630 Ltr ML20044H0751993-06-0202 June 1993 LER 93-010-00:on 930508,Mode 3 Entered from Mode 4 W/Both MDAFWPs Rendered Inoperable by Handswitches Being Placed in pull-to-lock.Caused by Failure to Control Work Activity.Mgt Expectations clarified.W/930602 Ltr ML20045A4931993-06-0101 June 1993 LER 93-009-00:on 930504,noted That Supervising Operator Erroneously Instructed RO to Reset Steamline LP SI Signal Rather than Block SI Signal.Caused by Personnel Error. Personnel Have Been Directed to Review event.W/930601 Ltr ML20044D2821993-05-11011 May 1993 LER 93-007-00:on 930413,determined That Surveillance Test Procedure Re RHR Sys Inservice Pump B Test Not Accomplished by 930410.Caused by Lack of Oversight of Surveillance program.Past-due Notice proceduralized.W/930511 Ltr ML20045H2631992-12-31031 December 1992 LER 92-007-01:on 920326,hot Particle Discovered on Individual Left Cheek.Event Probably Occurred During Use of Plant Communications Equipment.Procedure RPP 02-510 Evaluated ML20045H2701992-04-27027 April 1992 LER 92-007-00:on 920326,hot Particle Picked Up During RCS Shim Restraint Rework Insp Results in Exposure Exceeding 10CFR20.101 Requirements.Hot Particle Control Program & Policies Being reviewed.W/920427 Ltr ML20024G9791991-05-10010 May 1991 LER 90-026-00:on 901123,tech Spec Violation Occurred Re Safety Related Class IE Battery Bank Powered from Spare Battery Charger.Caused by Error in Safety Evaluation for Procedure Mce E051Q-01.Procedure deleted.W/910510 Ltr ML20029B2361991-02-28028 February 1991 LER 91-025-01:on 901223,common Min Flow Path Return Line for SI Pumps to RWST Frozen.Caused by Faulty Ambient Temp Switch.Switches Calibr to Insure Heat Trace Circuits & Alarms activated.W/910228 Ltr ML20029A6481991-02-26026 February 1991 LER 91-002-00:on 910128,essential Svc Water Flow to Containment Cooling Units Below TS 4.6.2.3 Requirements of 4,000 Gpm.Caused by Inaccurate Flow Readings Provided by Local Annubars.Surveillance Procedure revised.W/910226 Ltr ML20028H6901991-01-22022 January 1991 LER 90-025-00:on 901223,determined That Common Min Flow Path Return Line for SI Pumps to Refueling Water Storage Tank Frozen.Cause Undetermined.Need for Effective Communications Will Be Reiterated to Plant personnel.W/910122 Ltr ML20028H4361990-12-28028 December 1990 LER 90-024-00:on 901129,portion of Contents of Waste Gas Decay Tank 6 Discharged While Maint Performed.Caused by Personnel Error.Shift Supervisor counseled.W/901228 Ltr ML20028G9191990-09-26026 September 1990 LER 90-020-00:on 900827,portable Sump Pump Installed W/Pump Discharge Directed to Storm Drains,Bypassing Turbine Bldg Drain Monitor LE-RE-59.Caused by Lack of Communication Between Involved groups.W/900926 Ltr ML20043H7201990-06-18018 June 1990 LER 90-012-00:on 900517,reactor Trip,Main Turbine Trip & Auxiliary Feedwater Actuation Signals Occurred.Caused by Steam Generator C Atmospheric Dump Valve Stuck Open. Converter Positioner Circuitry replaced.W/900618 Ltr ML20043H1531990-06-18018 June 1990 LER 90-013-00:on 900519,main Turbine Trip Occurred as Result of hi-hi Moisture Separator Reheater Level.Root Cause Investigation Not Conclusive.Cautions Added to General Operating Procedure Gen 00-004.W/900618 Ltr ML20043G2761990-06-15015 June 1990 LER 90-010-00:on 900516,discovered That Insp Access Door for Motor Driven Auxiliary Feedwater Pump B Room Cooler Had Been Removed.Caused by Personnel Error.Maint Personnel Informed of Necessity of Doors Being in place.W/900615 Ltr ML20043G0741990-06-13013 June 1990 LER 90-011-00:on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure revised.W/900613 Ltr ML20043G1991990-06-0808 June 1990 LER 90-007-00:on 900510,feedwater Isolation Signal Occurred Due to Surveillance Test Requiring High Feed Rate.Caused by Feedwater Flow Rate Higher than Steam Flow.Rev to Surveillance Test Procedures clarified.W/900608 Ltr ML20043E9551990-06-0808 June 1990 LER 90-009-00:on 900608,discovered That Circuit Breakers for Accumulator Outlet IV Closed Resulting in Two Inoperable Accumulators.Caused by Personnel Error & Lack of Specific Procedural Direction.Procedure revised.W/900608 Ltr ML20043F1581990-06-0404 June 1990 LER 90-008-00:on 900504,fuel Bldg/Control Room Ventilation Isolation Signals Received from Exhaust Radiation Monitor. Caused by Burned Out Lamp & Blown Fuse in Power Supply.Fuse & Lamp Replaced & Monitor Returned to svc.W/900604 Ltr ML20043A6731990-05-16016 May 1990 LER 90-006-00:on 900416,containment Purge Isolation Signal & Control Room Ventilation Isolation Signal Occurred.Caused by Inadequate Procedures to Govern Deenergization of 120- Volt Ac Distribution Ctrs.Procedures revised.W/900516 Ltr ML20042G9171990-05-10010 May 1990 LER 90-005-00:on 900410,control Bldg/Auxiliary Bldg Pressure Boundary Door Found Open W/O Continuous Watch Established. Caused by Inadequate Procedures.Fire Protection Impairment Control Procedure revised.W/900510 Ltr ML20042G2131990-05-0707 May 1990 LER 90-004-00:on 900405,Tech Spec Surveillance Requirement Not Satisfied Because of Personnel Error in Scheduling Surveillance Test.Procedure Adm 02-300 revised.W/900507 Ltr ML20042E1851990-04-13013 April 1990 LER 90-002-00:on 900314,determined That Halon Release in Either ESF Switchgear Room Would Trip Both Class 1E Electrical Equipment Air Conditioning Units.Caused by Lack of Design Criteria.Criteria revised.W/900413 Ltr ML20043H2871990-04-0909 April 1990 Corrected LER 85-058-01:on 850731,reactor Trip,Main Turbine Trip,Auxiliary Feedwater Actuation,Feedwater Isolation & Steam Generator Blowdown & Sample Isolation Occurred.Caused by Faulty Power Supply to Channel.Power Replaced ML20012B4331990-03-0808 March 1990 LER 90-001-00:on 900206,reactor Tripped as Result of Loop Low Flow Condition Following Trip of Reactor Coolant Pump a, Causing Feedwater Isolation & Auxiliary Feedwater Actuation Signals.Caused by High Differential current.W/900308 Ltr ML20012B4741990-03-0505 March 1990 LER 88-007-01:on 880513,determined That Procedures for Setting Trip Point for Overpower & Overtemp Differential Instrument Loops Did Not Require Setpoints to Be Reset Conservatively.Setpoints recalculated.W/900305 Ltr ML20011D4391989-12-18018 December 1989 LER 89-020-00:on 891117,determined That as-built Configuration of Housing for Both Trains of Containment Cooling Fan HXs Not Seismically Qualified to Withstand Sse. Addl Seismic Restraints installed.W/891218 Ltr ML19332F9111989-12-14014 December 1989 LER 89-021-03:on 881025,preliminary Investigations Indicated That Containment Cooling Fan B Could Not Be Relied on to Perform Intended Design Function.Motor Overcurrent Condition Existed Since installation.W/891214 Ltr ML19325D5261989-10-18018 October 1989 LER 89-019-00:on 890919,determined That No Procedural Problem Existed & Equipment Problem Caused 890915 Test Deficiency.Caused by Reaching Incorrect Conclusion.Train Restored to Svc After Replacement of relay.W/891018 Ltr ML19341D8071988-01-15015 January 1988 LER 87-056-00:on 871215,one 400 Uci Sr-90/Y-90 Source Could Not Be Located.Caused by Inadequate Control of Licensed matl.Fan-Shaped Apparatuses Removed from Svc to Prevent recurrence.W/880115 Ltr 1993-08-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station ML20236P3441998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Wolf Creek Generating Station ML20236P3481998-05-31031 May 1998 Corrected Page of MOR for May 1998 for Wolf Creek Generating Station ML20249A0171998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Wolf Creek Generating Station ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247H0901998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Wolf Creek Generating Station ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20216F6101998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Wolf Creek Generating Station ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20216G1971998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Wolf Creek Nuclear Operating Corp ML20202H0721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Wolf Creek Generating Station ML20217G4311997-12-31031 December 1997 Western Resources 1997 Annual Rept & Financial Statements for Years Ended 971231 & 1996 for Ks Electric Power Cooperative,Inc ML20203H0151997-12-31031 December 1997 Annual Operating Rept 13 for Jan-Dec 1997 ML20217G3711997-12-31031 December 1997 Kansas City Power & Light Co 1997 Annual Rept ML20216D7771997-12-31031 December 1997 Annual SER 12 for Jan-Dec 1997, for Wolf Creek Generating Station 1999-09-30
[Table view] |
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. October 18,.1989 ;
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U. S. Nuclear: Regulatory Conunissha
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' ATTN' Document Control Desk l*v Mail Station Pi-137
- : Washington, D. C. 20555-i Subjects. Docket,No.'50-482: Licensee Event Report 01-019-00 a ;
.b 0- Centlemen:
, The' attached Licensea Event Report (LER). is submitted- . pursuant 'to l
- 10 CPR 50.75 (a) (2) (1) concerning a Technical Specification. violation.
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} Very truly yours.
, ,1 .
L % g . M s
i John A. Bailey ,
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Vice President i Nuclear Operations
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u 9 ACILITT NAME (t) DOCKtf NVainst R (2) PAGE G Wolf Creek Generating Station 0 1610101014I 812 1 loFl 0 l 5 Technical Specification 3.0.3 Entry caused By Discovery of Equ'.pment Inoperability In One Train While The Other Train Was Out Of Service
- t. ,> EYlNT DATS tel Llm NVM8tR tel REPORT DATE 171 OTHE R , ACILITit t INVOLvl0181 MONT H OAY YlAR YEAH j 'Ab
, [, MONTH DAY VEAR F ACILIT Y NAMES OOCKE T NUM9tR451 0l6l0l0l0l l l 0l9 1l 9 8 9 8! 9 0l1l 9 0 l0 1l0 1l8 8h 05 1 0 to O i i I
,,,,,,,,, THis MtPoRT is sueMiTTED evRsuANT TO THE RlouiREMENTs Op to CPR 6: sca.ca ea, er ene<er e ne neuemae s sitt
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. ARtACODE Merlin G. Williams - Manager Plant Support 3l1 i6 3,6 (4 l-l B i 8 3l1 COMPLlf t O..t LINE FOR B ACH COMPONENT f ALLURE DESCRISED IN THIS REPORT (13t MA C. " *T 8 CAV84 6 'f t tM COMPONeht n{0 NPR CAu$t 84 STE M COMPONEN? hE' }'O Nf RD ' ' '
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v remorm EXP(*1tO svewsssON OATEI NO l l l AesTi ACT tua,ir w sm w.ca. u. .aoremmar .rmea r e,no c. rema,ne,, o, > ns, I
On September 15, 1989, during perfomarce of a surveillance test sw o-lure, l
the "A" train Centrifugal Charging Ptmp (CCP) Minimum Flow Valve, BG HV- .
8110, did not stroke procerly in respanse to a sinulated flow signal. 'Ihe i
surveillance test was sniperded pending a review of the procedure l
, nethodology as tha sw slure had recently been revised. On September 19, :
l 1989, at 0420 CDP, a preventative traintenance outage began for several "B" ,
train components, including the emargency power source for the "B" train l CCP. At approximately 1200 CD? on Septaber 19, it was determined that no p proce'aral prdblem existed, and that an equipnent problem associated with BG l l HV-8W) had likely caused the September 15 test deficiency. At ;
l cppr.ox.imately 1755 CDP, it was determined that with BG HV-8110 inoperable, i the "A" train CCP could not be e.:cnsidered operable. Because the "B" train ,
CCP was also inoperable, the unit entered 'Iechnical Specification (T/S) 3.0.3 At 1940 CDT, the "A" train CCP was reatored to service after replacenent of i a faulty slave relay, and T/S 3.0.3 was exited at that ti;ne. This event l
occurred'as a result of maching mrrect conclusion when initially i evaluating the test deficiency. 9 '
ation's philosophy of a conservative l
aprcoach to pr.oblem solving w' .s It @. sized to licensed personnel. :
L The :.esponsibilities of test <
rners has been reiteratert to Instr.utentation and Control D .sannel.
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wac Nm apeA . U s. Nucttan r.toutaiow commission P' LICENSEE EVENT REPORT (LER) TEX ( CONTINUATION waovto on wo mow EkPIRil:Bf31/m e Acattiv NAM 4 Ill DOCKLT NUMBLR 423 f tR NUMBER ($l PA06 (31 l va'a "203^' ?#32 Wolf Creek Generating Station 0 l5 [0 l0 j 0 l l0[ 0l 019g O0 0 g5
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- i. TENT (# rnare spece a segweef. arse ammsons/ NRC Form ap5WsH171 pmmucrIm j On Septenbar 19,1989, at 1755 CDP, the unit entered Technical Specification l (T/S) 3.0.3 because of the inoperability of two independent naargency Core 2 Cooling System subsystems [BP, BQ). At the time of this event, the "B" train O.s paicy Diesel Generator [EK-DG) was out of service for planned maintenance activities rendering the "B" train Centrifugal Charging Punp .
[BQ-P) inoperable. It was subsequently detennined that the "A" train l Centrifugal Charging Punp was also inoperable. At 1940 CDP, the "A" train Centrifugal Charging Punp was restored to operable status and T/S 3.0.3 was exited. '1his report is being subnitted pursuant to 10CER50.73 (a)(2)(1)(B) as a cond). tion prohibited by the plant's Technical Specifications. ]
l DESCRIPTIGE & EVElff )
On September 15,1989, at 1455 CDP, Instruinantaticn and Centrol (I&C) 1 L Fiu;issuel ocmnanced performance of surveillance test suc lare SIS IC-603A, ,
t
" Slave Relay Test K603 Train A Safety Injection." This s ucM ure, in part, denonstrates pa:5er operation of valve BG W-8110, the "A" Train Centrifugal ;
Charging Punp Mininum Flow Valve [BQ-V). Under nonel operation, BG-W-8110 ,
is open to provide recirculation flow to the centrifugal charging punp.
l Following receipt of a safety injection signal, the mininun ficw valve ;
I should remain open if there is not sufficient flow passing through the flow
- switch in order to maintain adequate minimum flow to the centrifugal charging punp. 2his recirculation flow is necessary at high Reactor Coolant !
System pressures in order to prevent damage to the centrifugal charging punp I under low flow conditions. The minimum flow valve also receives an auto-closure signal to autenatically isolate the recirculation line when sufficient flow has been sensw by the flow switch. This automatic closure ,
I- feature ensures adequate safety injection flow is delivered to the reactor !
coolant system..
]
During performance of the sucedure, BG W-8110 stroked closed on a high flow sir; al as expected and then stroked back open, which was not expected.
Because the gvcedure had recently undergone a major revision, the test performer believed that a s ucadural problem had likely caused the unexpected str i s or a of BG W-0110. STS IC-603A was susguded at 1542 Car to allow for further review of the procedure methodology. l l
l On September 19,1989, at 0420 CDT, several "B" train ccmponents, including i Eg==ynicy Diesel Generator "B" and Residual Heat Renwal Punp "B" [BP-P) !
were tagged out of service for preventative maintenanc.e activities. Entry I was made into T/S 3.8.1.1, Actions b and d. Action b requires, in part, I that with one ciesel generator of the requW A.C. electrical pcmr somnec inoperable, demonstrate the operability of as offsite A.C. sources witLn 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and at least once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> thereafter and demanstrate the operability of the renaining operable diesel generator within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; restore the inoperable diesel generator to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> 1
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ie+ effBC Penn agSA U S. NUCLE A3 $.ESULATORY COMMISSION Y 7."' '
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AwRovio ovs No mo-om EXPIRE 4: t/3008 7 ACsLif y Naut DI DOCKit NUMStR g)
LfR NUMBER @ PA06 (3) I g
"aa " EP. W,?,n !
l Wolf Creek Generating Station o p, j o l o l o l 4l 8 l2 8l9 __ 0 jl l 9 _ 0jo 0;3 or 0 l5 ,
TEXT (# snore speco is esqpgyod. afee eeWhortsf hRC ,oren MW M7) or be in at least 1.ot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> arxi in cold shutdown -
within the followbg 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Acticn d requires, in part, that with one -
diesel generator inoperable verify that all required systens, subsystems, trains, conponents, .and devices that depend on the remaining operable diesel generator as a source of energency power, are also operable, and that the steam-driven auxiliary feedwater punp [BA.-P) is q = m ble. Entry was also c nade into T/S 3.5.2, Action a, which requires, in part, that with one Liamsysncy Core Cooling Systen subsystem inoperable, to Iestore the inoperable subsystem to cperable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. An Emergency Core :
Cooling System subsystem consists of one Centrifugal Charging Pump, one Safety Injection Punp [BQ.-P), one Residual Heat Renoval Punp and one
- Residual Heat Removal Heat Exchanger (BP-HK).' +
!- At approximately 1200 CCT, on September 19, 1989, I&C personnel ocnpleted a .
l review of STS IC-603A and concluded that no st-Mm1 problem existed. It (
was determined that a circuitry problem, most likely a bad relay, had caused '
the unexpected test result on Septanbar 15. An evaluatica was initiated to determine if ingvpar operation of BG HV-8110 would cause ine== ahility of.
I the "A" train Centrifugal Charging Ptmp. While this evaluation was being conducted, work was suspended on Limyzicy Diesel Generator "B" and efforts -
were focused on restoring it to service. In ack11 tion, preparations to replace the suspect relay were initiated.
At approximately 1755 CDP, Safety Analysis personnel concluded that there nay be insufficient huh head Safety Injection flow for certain accidents !
frcan the '"A" Centrifugal Charging Pump if the recirculation valve were to malfunctlon. '1herefore, the "A" Centrifugal Charging Punp could not be considered operable. The "B" Centrifugal Charging Punp could not be ,
considered q=mble because of the ingamhility of its emergency power !
sou::ce. Becense the Technical Specifications do not contain provisicms for ingamhility of two Limyisicy Ctre Cooling System subsystems, the plant ,
entered T/S 3.0.3.
At approximately 1827 CDT, IEC pw..caniel confirmed the gooence of a faulty slave relay (JG-EY) . By 1940 CDP, the slave relay had been replaced and STS IC-603A had been ca pleted satisfactorily, thus restoring the "A" Centrifuoal Charging Punp to oprable status. T/S 3.0.3 was exited at that time.
STS IC-603B, the corresponding "B" train surveillance gvc= dure, was subsequently perfonned satisfactorily to confirm supw: operation cd the slave relay controlling the recirculation valve for the "B" Centrifugal Charging Ptmp.
By approximately 2212 CDP, on September 21, 1989, the "B" train Limvency Diesel Generator was restored to c,perable status, and the Action Staternents of Technical Specifications 3.8.1.1 and 3.5.2 were exited at that time,
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181RC F.am PA U $ NUCLE 12 KE2VL AToAY COMMitSION TTO LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AreRovto ove =o mo-om exeints. e se. 1
/' f AC14tTV hANt Hi DCtR61 NUM9tR (2) gg h NuggER 16) PA05 (3) f vta. "un;r ::.y i h . Wolf Creek Generating Station o ls jo lo l0 l 4l8l 2 8l9 ._
0 gl j 9 ._ 0;0 04 or 0 l5 .
TiTnT ., A o .uwmei.-,mwnn
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L ROOP CADSE AIO Qmar.LTNE ACPINS l
This event occurred as a result of an incorrect conclusion being reached when initially evaluating the test deficiency encountered during the c performance of STS 10-503A. W e I&C technician performing the surveillanme test believed that the test deficiency could have been caused by a s vcodore '
error. W ie was the first performance of the s uc= dure utilizing a new methodology. When dispositioning the test deficiency, the Shift Supervisor (utility licensed operator) classifisi the deficiency as a sucedural error and believed that t w suc dare uould be reviewed and revised as necessary.
h I&C technician was unaware of any urgency to review the procedure methodology because the surysillanN " late date" was vct until Septanbar 30 and because the Shift Supervisor had classified the deficiency as a Non-l Technical Specification failure. Consequently, the technician did not
! initiata a' review of the sucedure until he returned to work en Tuesday, September 19. . After determining that no sveadore error existed, I&C pm.cunel pronptly notified the Control Rom that an equipnent problem did I exist. Following natificatim that there was a proble:n with equipnas.t in the "A" train, Control Roczn personnel initiated an evaluation of the condition and initiated actions to expedite restoration of equipnent to service.
u In order to reamphasize Wolf Creek Generating Station management philosophy relative to a conservative approach to problem solving, this Idoensee Event Report will be incorporated into Required Reading for all licensed personnel. In addition, a letter clarifying the test performer's responsibilities upon discovery of a test deficiency has been issued as required reading for I&C personnel. h letter highlights the inportance of i making conservative assunptions when a test deficiency is encountered and ;
when notifying the Shift Speisor that a deficiency has la identified. l h faulty relay was found to be eticking in its energized position with no I power to the coil. While renoving the relay, it cycled to its de-energized (correct) position. N relay was then cycled several times with no further problems encountered. A new relay was installed, and the faulty relay was taken to the I&C shop for further root cause analysis. h faulty relay was mnufactur".d by Potter & Brumfield, Model No TY93-MDR-4103-1.
l l
ADDITIONAL IFJRMATIm ,
1 During the time of this event, the unit was operating in Mode 1, Power Operation, at approximately 100 perc e t Icted W ermal Power. Centrifugal Charging Panp "B" was available to pr. ovide high head injection flow, although it was technically inoperable because its associated einu.gewy power supply was inoperable. Centrifugal Charging Punp "A" was also capable of delivering flow to the Reactor Coolant Systen. The Wolf Creek Steamline l
axC ,onu uA - ' ' * " ' " " ' * ' " " " "
- 3 33) ;
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i 88AC Paran ateA U.S Nut *LE A3 7.tguLATORY COMMISSION I f**! ' ' ' UCENSEE EVENT REPORT (LER) TEXT CONTINUATION anao. io ove No. mo-oioa (KPIRE S. 8/31/MI FAC6Lify Naast itl DOCR ET NUMBER (21 Ltd NUMelR (61 PA95 ($1 l naa " $ '?,i "iTJ,W .
t Wolf creek Generatano Station o l5 l0 l0 lo l 4l8 l 2 8l9 - 0 l lj 9 -
0l0 0]5 or 0l 5 -
TEXT fJ anose apoco e regenest, use m 44C perrn JesAw (17; break end IOCA analycos have been examined to determine the inpact of a reductica in safety injection flow frun CCP "A" due to the failure of the auto-closure function of the centrifugal charging pung mininum flow recirculation valve. It is concluded that there is no adverse effect en the s+-1% break analysis due to the case in which a OCP Icininum flow g isolation valve fails in an open position. No penalty was noted for the large treak IOCA 4.nalysis while a penalty of 68 degrees Fahrenheit wa::
- i. calculated for the anall break IOCA analysis. 'Ihe Peak Clad Tenparature (PCT) for the limiting emall break case with a reduction in safety injection flow as h rt M above is 1858 degrees Fahre heit. 'Ihis resultant POT for the.amall break IOCA case maintains considerable margin to the 2200 %= s l- Fahrenheit limit of 10CPR50.46 and continues to be bounded by the large :
l break IDCA result of 2111.5 degrees Fahrenheit. ;
I There have been no previous similar reportchle occurrences. ,
i 4
0 NRC FORM PSSA *ll 8* CP0e 1988-3 20- SM O M 711 0