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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C0821993-08-0303 August 1993 LER 93-012-00:on 930510,reported Unusual Noise Due to Small Frictional Force Release in RCS During heat-up.Developed & Implemented Enhanced Thermal Expansion Monitoring Program. W/930803 Ltr ML20045F1451993-06-30030 June 1993 LER 93-011-00:on 930518,nuclear Plant Instrumentation Sys Axial Flux Difference Limits Were Not Updated W/Ts Due to Inadequate Review of Colr.Initiated WR & Computer Software Mod request.W/930630 Ltr ML20044H0751993-06-0202 June 1993 LER 93-010-00:on 930508,Mode 3 Entered from Mode 4 W/Both MDAFWPs Rendered Inoperable by Handswitches Being Placed in pull-to-lock.Caused by Failure to Control Work Activity.Mgt Expectations clarified.W/930602 Ltr ML20045A4931993-06-0101 June 1993 LER 93-009-00:on 930504,noted That Supervising Operator Erroneously Instructed RO to Reset Steamline LP SI Signal Rather than Block SI Signal.Caused by Personnel Error. Personnel Have Been Directed to Review event.W/930601 Ltr ML20044D2821993-05-11011 May 1993 LER 93-007-00:on 930413,determined That Surveillance Test Procedure Re RHR Sys Inservice Pump B Test Not Accomplished by 930410.Caused by Lack of Oversight of Surveillance program.Past-due Notice proceduralized.W/930511 Ltr ML20045H2631992-12-31031 December 1992 LER 92-007-01:on 920326,hot Particle Discovered on Individual Left Cheek.Event Probably Occurred During Use of Plant Communications Equipment.Procedure RPP 02-510 Evaluated ML20045H2701992-04-27027 April 1992 LER 92-007-00:on 920326,hot Particle Picked Up During RCS Shim Restraint Rework Insp Results in Exposure Exceeding 10CFR20.101 Requirements.Hot Particle Control Program & Policies Being reviewed.W/920427 Ltr ML20024G9791991-05-10010 May 1991 LER 90-026-00:on 901123,tech Spec Violation Occurred Re Safety Related Class IE Battery Bank Powered from Spare Battery Charger.Caused by Error in Safety Evaluation for Procedure Mce E051Q-01.Procedure deleted.W/910510 Ltr ML20029B2361991-02-28028 February 1991 LER 91-025-01:on 901223,common Min Flow Path Return Line for SI Pumps to RWST Frozen.Caused by Faulty Ambient Temp Switch.Switches Calibr to Insure Heat Trace Circuits & Alarms activated.W/910228 Ltr ML20029A6481991-02-26026 February 1991 LER 91-002-00:on 910128,essential Svc Water Flow to Containment Cooling Units Below TS 4.6.2.3 Requirements of 4,000 Gpm.Caused by Inaccurate Flow Readings Provided by Local Annubars.Surveillance Procedure revised.W/910226 Ltr ML20028H6901991-01-22022 January 1991 LER 90-025-00:on 901223,determined That Common Min Flow Path Return Line for SI Pumps to Refueling Water Storage Tank Frozen.Cause Undetermined.Need for Effective Communications Will Be Reiterated to Plant personnel.W/910122 Ltr ML20028H4361990-12-28028 December 1990 LER 90-024-00:on 901129,portion of Contents of Waste Gas Decay Tank 6 Discharged While Maint Performed.Caused by Personnel Error.Shift Supervisor counseled.W/901228 Ltr ML20028G9191990-09-26026 September 1990 LER 90-020-00:on 900827,portable Sump Pump Installed W/Pump Discharge Directed to Storm Drains,Bypassing Turbine Bldg Drain Monitor LE-RE-59.Caused by Lack of Communication Between Involved groups.W/900926 Ltr ML20043H7201990-06-18018 June 1990 LER 90-012-00:on 900517,reactor Trip,Main Turbine Trip & Auxiliary Feedwater Actuation Signals Occurred.Caused by Steam Generator C Atmospheric Dump Valve Stuck Open. Converter Positioner Circuitry replaced.W/900618 Ltr ML20043H1531990-06-18018 June 1990 LER 90-013-00:on 900519,main Turbine Trip Occurred as Result of hi-hi Moisture Separator Reheater Level.Root Cause Investigation Not Conclusive.Cautions Added to General Operating Procedure Gen 00-004.W/900618 Ltr ML20043G2761990-06-15015 June 1990 LER 90-010-00:on 900516,discovered That Insp Access Door for Motor Driven Auxiliary Feedwater Pump B Room Cooler Had Been Removed.Caused by Personnel Error.Maint Personnel Informed of Necessity of Doors Being in place.W/900615 Ltr ML20043G0741990-06-13013 June 1990 LER 90-011-00:on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure revised.W/900613 Ltr ML20043G1991990-06-0808 June 1990 LER 90-007-00:on 900510,feedwater Isolation Signal Occurred Due to Surveillance Test Requiring High Feed Rate.Caused by Feedwater Flow Rate Higher than Steam Flow.Rev to Surveillance Test Procedures clarified.W/900608 Ltr ML20043E9551990-06-0808 June 1990 LER 90-009-00:on 900608,discovered That Circuit Breakers for Accumulator Outlet IV Closed Resulting in Two Inoperable Accumulators.Caused by Personnel Error & Lack of Specific Procedural Direction.Procedure revised.W/900608 Ltr ML20043F1581990-06-0404 June 1990 LER 90-008-00:on 900504,fuel Bldg/Control Room Ventilation Isolation Signals Received from Exhaust Radiation Monitor. Caused by Burned Out Lamp & Blown Fuse in Power Supply.Fuse & Lamp Replaced & Monitor Returned to svc.W/900604 Ltr ML20043A6731990-05-16016 May 1990 LER 90-006-00:on 900416,containment Purge Isolation Signal & Control Room Ventilation Isolation Signal Occurred.Caused by Inadequate Procedures to Govern Deenergization of 120- Volt Ac Distribution Ctrs.Procedures revised.W/900516 Ltr ML20042G9171990-05-10010 May 1990 LER 90-005-00:on 900410,control Bldg/Auxiliary Bldg Pressure Boundary Door Found Open W/O Continuous Watch Established. Caused by Inadequate Procedures.Fire Protection Impairment Control Procedure revised.W/900510 Ltr ML20042G2131990-05-0707 May 1990 LER 90-004-00:on 900405,Tech Spec Surveillance Requirement Not Satisfied Because of Personnel Error in Scheduling Surveillance Test.Procedure Adm 02-300 revised.W/900507 Ltr ML20042E1851990-04-13013 April 1990 LER 90-002-00:on 900314,determined That Halon Release in Either ESF Switchgear Room Would Trip Both Class 1E Electrical Equipment Air Conditioning Units.Caused by Lack of Design Criteria.Criteria revised.W/900413 Ltr ML20043H2871990-04-0909 April 1990 Corrected LER 85-058-01:on 850731,reactor Trip,Main Turbine Trip,Auxiliary Feedwater Actuation,Feedwater Isolation & Steam Generator Blowdown & Sample Isolation Occurred.Caused by Faulty Power Supply to Channel.Power Replaced ML20012B4331990-03-0808 March 1990 LER 90-001-00:on 900206,reactor Tripped as Result of Loop Low Flow Condition Following Trip of Reactor Coolant Pump a, Causing Feedwater Isolation & Auxiliary Feedwater Actuation Signals.Caused by High Differential current.W/900308 Ltr ML20012B4741990-03-0505 March 1990 LER 88-007-01:on 880513,determined That Procedures for Setting Trip Point for Overpower & Overtemp Differential Instrument Loops Did Not Require Setpoints to Be Reset Conservatively.Setpoints recalculated.W/900305 Ltr ML20011D4391989-12-18018 December 1989 LER 89-020-00:on 891117,determined That as-built Configuration of Housing for Both Trains of Containment Cooling Fan HXs Not Seismically Qualified to Withstand Sse. Addl Seismic Restraints installed.W/891218 Ltr ML19332F9111989-12-14014 December 1989 LER 89-021-03:on 881025,preliminary Investigations Indicated That Containment Cooling Fan B Could Not Be Relied on to Perform Intended Design Function.Motor Overcurrent Condition Existed Since installation.W/891214 Ltr ML19325D5261989-10-18018 October 1989 LER 89-019-00:on 890919,determined That No Procedural Problem Existed & Equipment Problem Caused 890915 Test Deficiency.Caused by Reaching Incorrect Conclusion.Train Restored to Svc After Replacement of relay.W/891018 Ltr ML19341D8071988-01-15015 January 1988 LER 87-056-00:on 871215,one 400 Uci Sr-90/Y-90 Source Could Not Be Located.Caused by Inadequate Control of Licensed matl.Fan-Shaped Apparatuses Removed from Svc to Prevent recurrence.W/880115 Ltr 1993-08-03
[Table view] Category:RO)
MONTHYEARML20046C0821993-08-0303 August 1993 LER 93-012-00:on 930510,reported Unusual Noise Due to Small Frictional Force Release in RCS During heat-up.Developed & Implemented Enhanced Thermal Expansion Monitoring Program. W/930803 Ltr ML20045F1451993-06-30030 June 1993 LER 93-011-00:on 930518,nuclear Plant Instrumentation Sys Axial Flux Difference Limits Were Not Updated W/Ts Due to Inadequate Review of Colr.Initiated WR & Computer Software Mod request.W/930630 Ltr ML20044H0751993-06-0202 June 1993 LER 93-010-00:on 930508,Mode 3 Entered from Mode 4 W/Both MDAFWPs Rendered Inoperable by Handswitches Being Placed in pull-to-lock.Caused by Failure to Control Work Activity.Mgt Expectations clarified.W/930602 Ltr ML20045A4931993-06-0101 June 1993 LER 93-009-00:on 930504,noted That Supervising Operator Erroneously Instructed RO to Reset Steamline LP SI Signal Rather than Block SI Signal.Caused by Personnel Error. Personnel Have Been Directed to Review event.W/930601 Ltr ML20044D2821993-05-11011 May 1993 LER 93-007-00:on 930413,determined That Surveillance Test Procedure Re RHR Sys Inservice Pump B Test Not Accomplished by 930410.Caused by Lack of Oversight of Surveillance program.Past-due Notice proceduralized.W/930511 Ltr ML20045H2631992-12-31031 December 1992 LER 92-007-01:on 920326,hot Particle Discovered on Individual Left Cheek.Event Probably Occurred During Use of Plant Communications Equipment.Procedure RPP 02-510 Evaluated ML20045H2701992-04-27027 April 1992 LER 92-007-00:on 920326,hot Particle Picked Up During RCS Shim Restraint Rework Insp Results in Exposure Exceeding 10CFR20.101 Requirements.Hot Particle Control Program & Policies Being reviewed.W/920427 Ltr ML20024G9791991-05-10010 May 1991 LER 90-026-00:on 901123,tech Spec Violation Occurred Re Safety Related Class IE Battery Bank Powered from Spare Battery Charger.Caused by Error in Safety Evaluation for Procedure Mce E051Q-01.Procedure deleted.W/910510 Ltr ML20029B2361991-02-28028 February 1991 LER 91-025-01:on 901223,common Min Flow Path Return Line for SI Pumps to RWST Frozen.Caused by Faulty Ambient Temp Switch.Switches Calibr to Insure Heat Trace Circuits & Alarms activated.W/910228 Ltr ML20029A6481991-02-26026 February 1991 LER 91-002-00:on 910128,essential Svc Water Flow to Containment Cooling Units Below TS 4.6.2.3 Requirements of 4,000 Gpm.Caused by Inaccurate Flow Readings Provided by Local Annubars.Surveillance Procedure revised.W/910226 Ltr ML20028H6901991-01-22022 January 1991 LER 90-025-00:on 901223,determined That Common Min Flow Path Return Line for SI Pumps to Refueling Water Storage Tank Frozen.Cause Undetermined.Need for Effective Communications Will Be Reiterated to Plant personnel.W/910122 Ltr ML20028H4361990-12-28028 December 1990 LER 90-024-00:on 901129,portion of Contents of Waste Gas Decay Tank 6 Discharged While Maint Performed.Caused by Personnel Error.Shift Supervisor counseled.W/901228 Ltr ML20028G9191990-09-26026 September 1990 LER 90-020-00:on 900827,portable Sump Pump Installed W/Pump Discharge Directed to Storm Drains,Bypassing Turbine Bldg Drain Monitor LE-RE-59.Caused by Lack of Communication Between Involved groups.W/900926 Ltr ML20043H7201990-06-18018 June 1990 LER 90-012-00:on 900517,reactor Trip,Main Turbine Trip & Auxiliary Feedwater Actuation Signals Occurred.Caused by Steam Generator C Atmospheric Dump Valve Stuck Open. Converter Positioner Circuitry replaced.W/900618 Ltr ML20043H1531990-06-18018 June 1990 LER 90-013-00:on 900519,main Turbine Trip Occurred as Result of hi-hi Moisture Separator Reheater Level.Root Cause Investigation Not Conclusive.Cautions Added to General Operating Procedure Gen 00-004.W/900618 Ltr ML20043G2761990-06-15015 June 1990 LER 90-010-00:on 900516,discovered That Insp Access Door for Motor Driven Auxiliary Feedwater Pump B Room Cooler Had Been Removed.Caused by Personnel Error.Maint Personnel Informed of Necessity of Doors Being in place.W/900615 Ltr ML20043G0741990-06-13013 June 1990 LER 90-011-00:on 900514,feedwater Isolation Signal & Main Turbine Trip Signal Occurred When Steam Generator B Reached hi-hi Level Setpoint & Generator C Reached lo-lo Setpoint. Caused by Power Oscillations.Procedure revised.W/900613 Ltr ML20043G1991990-06-0808 June 1990 LER 90-007-00:on 900510,feedwater Isolation Signal Occurred Due to Surveillance Test Requiring High Feed Rate.Caused by Feedwater Flow Rate Higher than Steam Flow.Rev to Surveillance Test Procedures clarified.W/900608 Ltr ML20043E9551990-06-0808 June 1990 LER 90-009-00:on 900608,discovered That Circuit Breakers for Accumulator Outlet IV Closed Resulting in Two Inoperable Accumulators.Caused by Personnel Error & Lack of Specific Procedural Direction.Procedure revised.W/900608 Ltr ML20043F1581990-06-0404 June 1990 LER 90-008-00:on 900504,fuel Bldg/Control Room Ventilation Isolation Signals Received from Exhaust Radiation Monitor. Caused by Burned Out Lamp & Blown Fuse in Power Supply.Fuse & Lamp Replaced & Monitor Returned to svc.W/900604 Ltr ML20043A6731990-05-16016 May 1990 LER 90-006-00:on 900416,containment Purge Isolation Signal & Control Room Ventilation Isolation Signal Occurred.Caused by Inadequate Procedures to Govern Deenergization of 120- Volt Ac Distribution Ctrs.Procedures revised.W/900516 Ltr ML20042G9171990-05-10010 May 1990 LER 90-005-00:on 900410,control Bldg/Auxiliary Bldg Pressure Boundary Door Found Open W/O Continuous Watch Established. Caused by Inadequate Procedures.Fire Protection Impairment Control Procedure revised.W/900510 Ltr ML20042G2131990-05-0707 May 1990 LER 90-004-00:on 900405,Tech Spec Surveillance Requirement Not Satisfied Because of Personnel Error in Scheduling Surveillance Test.Procedure Adm 02-300 revised.W/900507 Ltr ML20042E1851990-04-13013 April 1990 LER 90-002-00:on 900314,determined That Halon Release in Either ESF Switchgear Room Would Trip Both Class 1E Electrical Equipment Air Conditioning Units.Caused by Lack of Design Criteria.Criteria revised.W/900413 Ltr ML20043H2871990-04-0909 April 1990 Corrected LER 85-058-01:on 850731,reactor Trip,Main Turbine Trip,Auxiliary Feedwater Actuation,Feedwater Isolation & Steam Generator Blowdown & Sample Isolation Occurred.Caused by Faulty Power Supply to Channel.Power Replaced ML20012B4331990-03-0808 March 1990 LER 90-001-00:on 900206,reactor Tripped as Result of Loop Low Flow Condition Following Trip of Reactor Coolant Pump a, Causing Feedwater Isolation & Auxiliary Feedwater Actuation Signals.Caused by High Differential current.W/900308 Ltr ML20012B4741990-03-0505 March 1990 LER 88-007-01:on 880513,determined That Procedures for Setting Trip Point for Overpower & Overtemp Differential Instrument Loops Did Not Require Setpoints to Be Reset Conservatively.Setpoints recalculated.W/900305 Ltr ML20011D4391989-12-18018 December 1989 LER 89-020-00:on 891117,determined That as-built Configuration of Housing for Both Trains of Containment Cooling Fan HXs Not Seismically Qualified to Withstand Sse. Addl Seismic Restraints installed.W/891218 Ltr ML19332F9111989-12-14014 December 1989 LER 89-021-03:on 881025,preliminary Investigations Indicated That Containment Cooling Fan B Could Not Be Relied on to Perform Intended Design Function.Motor Overcurrent Condition Existed Since installation.W/891214 Ltr ML19325D5261989-10-18018 October 1989 LER 89-019-00:on 890919,determined That No Procedural Problem Existed & Equipment Problem Caused 890915 Test Deficiency.Caused by Reaching Incorrect Conclusion.Train Restored to Svc After Replacement of relay.W/891018 Ltr ML19341D8071988-01-15015 January 1988 LER 87-056-00:on 871215,one 400 Uci Sr-90/Y-90 Source Could Not Be Located.Caused by Inadequate Control of Licensed matl.Fan-Shaped Apparatuses Removed from Svc to Prevent recurrence.W/880115 Ltr 1993-08-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station ML20236P3441998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Wolf Creek Generating Station ML20236P3481998-05-31031 May 1998 Corrected Page of MOR for May 1998 for Wolf Creek Generating Station ML20249A0171998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Wolf Creek Generating Station ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247H0901998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Wolf Creek Generating Station ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20216F6101998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Wolf Creek Generating Station ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20216G1971998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Wolf Creek Nuclear Operating Corp ML20202H0721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Wolf Creek Generating Station ML20217G4311997-12-31031 December 1997 Western Resources 1997 Annual Rept & Financial Statements for Years Ended 971231 & 1996 for Ks Electric Power Cooperative,Inc ML20203H0151997-12-31031 December 1997 Annual Operating Rept 13 for Jan-Dec 1997 ML20217G3711997-12-31031 December 1997 Kansas City Power & Light Co 1997 Annual Rept ML20216D7771997-12-31031 December 1997 Annual SER 12 for Jan-Dec 1997, for Wolf Creek Generating Station 1999-09-30
[Table view] |
Text
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W$LFCREEK NUCLEAR OPERATING CORPORATION
.' John A. Bausy ;
s VW Premesed,,,.
w o,,,, , - -. =
y T -:r . ' December 18, 1989
, NO 89-0217.
U." S. Nuclear Regulatory Co:nmission
~ ATTN : '. Document' Control Desk-
.Q ; Mail' Station P1-137 0 -Washington, D. c. 20555 Subjects l Docket No. 50-482: Licensee Event' Report 89-020-00 n
Gentlemen:
tThe attached Licensee Event- Report (LER) is -submitted pursuant to-lotCFR=50;73 (a)n(2) (ii) concerning a condition outside the design basis of the plant.L
'Very truly yours,-
, s c' -
L John A.' Bailey Vice President.
..r 1 Nuclear., Operations JAB / a em'-
Attachment
-cci: B. L. Bartlett (NRC), w/a E.-J. Holler (NRC) w/a R=. .
D. Martin-(NRC), w/a
~
D. V. Pickett (NRC), w/a cif. . - ; P.O. Box 411/ Burungton, KS 66839 / Phone: (316) 364 8831
'%' ' 8912270220 891218 An Equel opportunity Employer hW/He/ VET M' ' '
PDR ADOCK 05000482 9 PNV .
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NRCt .'au u.s.::uCLEAa REtutaTORY COMMISSION i APPROVED OMS NO 2194 0104 LICENSEE EVENT REPORT (LER) * * *'au 8' '"
g.
,? FACitfTY NAME 11) DOCKE 7 NUM91R (2) . PAGE(3.
Wolf Creek Generatino Station 0l5tol0l0l4lg;7 1 lOFl O[4 Seismic Analysis Discrepancies Afiecting Containment Cooling Fan System Housj ng EVENT DATE (Si LER NUMBER ($1 REPORT DATE 17: OTHER f ACILITIES INVOL VED (St sat MONTH I DAY F AC4L'T v e. Awas DOCKET NUMBER,81 MONT H DAT YEAR YEAR SQu p a$ YEAR 0 16101010 1 l I c 1l1 1l 7 .
8 9 8l 9 0l2l0 0l0 1l2 1l8 Cl9 0 1 5 1 0 totoi l l i
- OPE R ATING .TMis REPORT IS SUSMITTEO PURSUANT TO THE REQUIREMENTS OF 10 CFR $: (Checa e or asore of the retroempf Ull MODE W } 20 402M 20 405(el 60.73teH2Hel 73.71161 POWER 30.4064sH1H4) . 60.36(sH O $0.73(aH2Hvl 73.714s!
' 'IEe"' 11010 20.40ei. Hum so.m(.H2i so.73<.i2H,iii OTHE R ts,.,<<r <a A.,,r.ce
- . s 20.406teH1Hdy 60.73tal(21H) 60.73(a H2HvillHAl 6A gg _
20 4061sH1Hiv)
] 50.734sH2Hi0 50.73t.12HeliiH81 20.406(eH1Hvl 60,731s H2Hsil) 50.73tell2Hui LICENSEE CON'ACT POR THl3 LER (12)
NAME TELEPHONE NUMBER ARE A CODE Merlin G. Williams - Managcr P1 ant Support 3l1;6 3i6i 4 l-i 8 i 8 l 3l1 COMPLETE ONE LINE FOR E ACh COMPONENT F AILURE DESCRISED lN TMl5 REPORT H3)
"# ' A C. REPORtA LE MA C- REPORTA E s CAU0E SYSTEM COMPONENT ' gg yo pp s CAUSE SYSTEM COMPONENT ,
s s
'l l I 'l i I I I I I I I I I 1 I I I I I I I I I I I I I I '
l SUPPLEMENTAL REPORT EXPECTED H4) MONTH DAY YEAR
$U8uis$lON T vu <<r m.M weCreo svowssion oAres G NO o; 4 l3 l 0 9lo u A T R AC1,- ,~ a . ., ,,, N _,.. .. , n.1
,On Nov m ber 17, 1989, it es determined by a calculation ttat the as-ballt ,
configuration of the housing for both trains of containment cooling fan heat ~
exchangers a s not seismically qualified to withstand a Safe Shutdown Earthquake.- It e s further determined that this situation placed the Wolf Creek Generating Station in a condition outside the design basis of the
- plant.
L This calculation was performed in response to a notification by the Architect / Engineer (Bechtel Power Corporation) of generic errors / discrepancies in the original seismic qualification report. Upon empletion of the calculation, both trains of containment cooling fans were declared inoperable. A plant modification package e s developed to install additional seismic restraints.- The installation of the restraints was conpleted on November 19, 1989 on the 'B' train and on Nuvwam: 20, 1989, on the 'A' train, thereby restoring both trains of containment cooling fans to operable status.
. A' detailed review and evaluation of the original seismic analysis methodology in cmparison to the conservative methodology utilized in Novmber, 2989, is being perfarned. The conclusions reached will be provided in a supplenent to this report.
ll f
NRC Form 300 42w- . _ _ _ - - _ _ - _ - _ _ _ - _ _ _ _ - . _ _ _ _ - - - - _ - . _ . _ - - - _ - _ _ _ _ _ _ _ _ _ - _ _ _ . _ - _ . . - _ . _ - _ _ _ _ _ _ _ - _ _ _ - _ _ . _ - _ _ ;
- Y I efMC Fenn 3RDA ~ U.6, NUCLEAR REOULATORY COMMISSION 7# LICENS'EE EVENT REPORT (LER) TEXT CONTINUATION maoveo ous no. siso-oio -
LXPIRE$: 8731180 ,
CILITY HAM tia DOCKE T NUMBER (2I LtR NUMSER (6) PAGE (3)
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.r On Novenber 17,1989, it was detemined that the as-built configuration of' the housing foi both trains of containment cooling fan heat exchangers [BK-
.HX) was not seismically qualified to withstand a Safo Shutdown Earthquake. ;
It was further detemined that this situation placed the Wolf Creek '
Generating Station (NOGS) in a condition outside the design basis of the plant. 'Iherefore this report is being subnitted pursuant to 10CFR50.73(a)(2)(ii).
OtEKRIPTIGi T BVENT Wolf Creek Nuclear Operating Corporation (NCNOC) was notified by the plant's Architect / Engineer, Bechtel Power Corporation, that generic
- errors / discrepancies had been identified in seismic analysis reports prepared by American Air Filter (AAF). 'Ihese errors were discovered during-qualification of equiprent by analysis. 'Ihe only safety-related AAF Lequipnent installed at NOGS are the four containment cooling fan heat exchangers.
-After conducting a thorough review of the identified discropancies, NCNOC engineering personnel perfomed a calculation on.Novenber 17, 1989, which-detamined that the cooling fan heat exchanger housing would be over stressed when subjected to the peak ground acceleration for a Safe Shutd v p Earthquake. ' At that time the unit was operating in Mode 1, Power Operat.1,-
at approximately 100 peromt rated themal power.
Based on the calculation results, both trains of containment cooling fans were declared inoperable at 1151 CST on November 17, 1989. An entry was m3de into Technical Specification 3.6.2.3, Action 'b', which requires that L with two groups of containment cooling fans inoperable and both Containment l Spray Systens [BE] operable, restore at least one group of cooling fans to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least Hot Standby within the
-next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> and restore both groups of cooling fans to operable status within 7 days of initial loss
- or be in.at least Hot Standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Cold Shutdown within the following.30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
A plant modification package was developed to install additional seismic restraints to restore the containment cooling fans to npm-ahle status.
Installation of the restraints on the 'B' train containment cooling fan heat ll exchanger housings was conpleted at 1731 CST on Novenber 19, 1989, thereby restoring one train to operable status. Tnis modification subsequently was completed on the 'A' train containment cooling fan heat exchanger housings at 1305 CST on November 20, 1989, and Technical Specification 3.6.2.3, Action 'b was exited at that time. 'Ihroughout this event, the unit remained in Mode 1,. Power Operation.
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Offic form 306A - U.S. NUCLEAR 86004ATORY COMMISSION 7
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION sanovfo ove No mo-om EXPlRES: 8/31/08 9 ACittTY NAME (1) DOCKET NUMBER G5 LER NUM85R 16) PAGE (3) vE*a 5103^' b # 0e?0 i
Wblf Creek Generating' Station o is jo ]o l0 l 4l8 l 2 8l9 -
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0l0 0l3 OF 0 l4 TEXT (# more asse de regwred, use eddwoner NAC Form JsM'st (17)
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Further review and evaluation of the methodology utilized to detemine seismic qualification of the containment cooling fen heat exchanger housings is being omducted. 21s etfort includes a~ review of the j conservatisms utilized in the November,1989, calculation to detemine -
seismic qualificaticn. Also within the scope of this effort is a review to identify the root cause and any further required corrective measures.
Following conpletion of this effort, a supplement to this report will .be i subnitted describing the details of the review. % e expected subnission l
'date of the supplement is April 30, 1990.
p The present configuratica of the ocntainment cooling fan heat exchanger housings is adequate to ensure adherece to seismic design requiranants ;
itdependent of the results of this evaluation effort. ,
l; !
ADDITIG9L DilGMATIGi' The Containment Cooling System consists of two trains of Containment Spray i
- and two trains of containment cooling fans. Se current NOGS containment
[NH] analysis assumes the single failure of one protection train (i.e., loss
! .of one train of Containment Spray and one train of containment cooling fans) and therefore takes credit for one train of Containment Sp rf and one train
' of ccntainment cooling fans. Consequently, the situation described in this report, namely, the postulated failure of both trains of containment cooling fans upon occurrence of a Safe Shutdown Earthquake, represents a condition outside the design basis of the plant.
i In order to assess the consequences of failure of the Containment Cooling System a containment re-analysis was performed assuming the loss of all containment cooling fans. The main stu m1 Me break is the bounding event for peak pressure and peak tenperature'in containment, with peak pressure being the parameter of nost concern. The analysis concluded that with both l> trains of containment spray operating and an initial Refucling Water Storage
', Tank (RWST) (BP-3] tanperature of 100 degrees Fahrenheit or less, which is the base case temmture in the Updated Safety Analysis Report (USAR), the '
maxinum' containment pressure would remain within the containment design pressure. Assuming a failure of one train of containment spray and an
. initial RHST temperature of 75 degrees Fahrenheit or less (tauperature expected under current conditions), the design pressure of the containment
.would not be exceeded.
An evaluation of the probability of a seismic event which would exceed the original as-built capabilities of the containment cooling fan heat
- . exchangers housings was performed. The evaluation concluded that the probability of' occurrence of a seismic event of the magnitude to cause l
extensive containment cooling fan heat exchanger housing damage is very low.
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.o 48tC Form astA U.S NUCLEAR RE2ULATORY COMMISSION
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l m LICENSEE EVENT REPORT (LER) TEXT CONTINUATION enaovto oue No. stso-oio4 Expiats; Staires F ACILITY NAMS t)) DOCKET NUMBER (21 LtR NUMBER (81 . PAGE (3) vsaa " O!,';l'.
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= Wolf Creek Generating Station 0 l5 l0 l0 l0 l 4 l8 l 2 8l 9 -
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0l0 0l4 OF 0 l4 iExT ta more spece a revumed use emnonalNAC Form asE4'st(17) 1 Additionally, as statai in the NOGS USAR, in designing and analyzing for a f Design Basis Accident (i.e. , loss of coolant accident, nain staaml % break, ,
fuel handling accident, or steam generator tube rupture), these events are !
not assumed to be the result of a tornado, hurricane, flood, fire, loss of j offsite power, or' seismic event. 'Ihe assumed operation of the Containment Cooling Systen, following a Design Basis Accident without a concurrent seismic event, is not affected by the seismic design concerns discussed in this report.
Based on the low probability of a seismic event occurring, the Design Basis Accident discussion in the USAR, and the results of the containment' analysis ;
performed to specifically evaluate this condition, it is conclirtM that this l situation did not significantly jaq=rriize containment integrity. ;
i
'1here have been no previots similar occurrences. I i
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