ML20037A447
| ML20037A447 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 03/12/1974 |
| From: | DUKE POWER CO. |
| To: | |
| Shared Package | |
| ML20037A441 | List: |
| References | |
| NUDOCS 8001230667 | |
| Download: ML20037A447 (2) | |
Text
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J oconee Unit 2 UNIT March 12. 1974 MTE CPERATING STATUS January 31, 1974 1.
REPORTING PERIOD: January I gn 743 GilDSS EDURS IN REPORTING PERICD1 2568
' MW-NET 2.
CURRENTLY AUTHORIEED POWER LEVEL IMt 4
None 3.
POWER LEVEL 10 WEICH RESTRICTED (IF ANY):
REASONS FOR RESTRICTIONS (IF ANY):
4.
Oconee Unit 2 is presently in power escalation testing and is not ecnetercially operable. Items 10-13 are not applicable.
THIS CUMULATIVE MONTH YR-TO-DATE TO DATE 5.
HOURS ETACTOR WAS CRITICAL 85.6 85.6 743.0 6.
HOURS GENERATOR ON-LINE 64.0 64.0 577.2 7.
CROSS THERMAL POWER GENERATED (MWH) 104099 104099 709271 8.
CROSS ELECTRICAL Pok7.R GENERATED (MVH) 33000 33000 209310 9.
NET ELECTRICAL POhT.R GENERATED (MWH) 25964 25964
~ 178251 i
- 10. REACTOR AVAILABILITY FACTOR (1)
^
- 11. PLAhT AVAILABILITY FACTOR (2)
- 12. PLAhT CAFACITY FACTOR (3)
- 13. 70RCED OUTAGE RATE (4)
- 14. SHUTDOWNS SCHEDULED TO BEGIN IN NEXT 6 M0hTilS (STATE TYPE, DATE AND DURATION OF EACil):
- 15. IF SHUTDOWN AT ENE OF REPORT PERIOD, ESTI:!ATED DATE OF STARTUP:
- 16. PLANTS IN TEST STATUS (PRIOR TO Com!ERCIAL OPERATION) REPOT.T THE FOLLOUING DATE LAST DATE REASON FOR FORECAST ACHIEVED DIFFERENCE 11/11/73 INITIAL CRITICALITY 12/5/73 INITIAL ELECTRICAL 70VER GENERATION 5/15/74 COMIERCIAL OPERATION
- 100 (1) REACTOR AVAILABILITY FACTOR = 110URS REACTOR WAS CRITICAL CROSS IDURS IN REPORTING PERIOD
- 100 (2) PLAhT AVAILABILITY FACTOR = HOURS GENERATOR OS-LINE GROSS HOURS IN REPORTING PERIOD (3) PLANT CAPACITY FACTOR = NET _ ELECT,RICAL POWER CENERATED_ _,
CURREhTLY LICENSED POWER LEVEL
- CROSS IDURS IN RZPO
~* 100 (4) FORCED OUTAGE RATE = FORCED OUTACE 110URS BOURS GENERATOR ON-LINE + FORCED 00 G 1 800128
- y htARY:
Oconee Unit 2 UNIT W at
~
DATg February 28, 1974
- Janudry,.1974 33ront McNis.
FLANT SEUTDOWNR i
TYPE HETHOD OF F-F0RCED DURATION
'SHUITIND.DOWN NO.
DATE S-SOIEDULED (HOURS)
REASON (1) tile react 0R (2)
ColttENTS,
1 740101 F
27 B
A Repaired feedwater and condensate system valves 2
,740104 F
410.7 A
C Detected loose object in reactor vessel lower bead following reactor trip; AEC approval to. continue operation granted January 15, 1974
,3 74b122 F-198.3 A
B Reactor coolant pump 2B2 seal failed i
(1) REASON:
(2) METH03:
A-EQUIFHENT YAILURE (EIFLAIN)
A-MArJAL -
E-l' 3UAL SCRAM B-MAINT. OR, TEST C-REFUELING C-TJTOMATIC SCRAM D-REGULATORY RES1RICTION E-OPERATOR TRAINING AHD LICENSE EXA*lINATI0t4 F-ADH1!!!STRATIVE G-Ol'ERATIOllAL ERROR (EXPLAIN) g