ML20037A446
| ML20037A446 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 03/12/1974 |
| From: | DUKE POWER CO. |
| To: | |
| Shared Package | |
| ML20037A441 | List: |
| References | |
| NUDOCS 8001230666 | |
| Download: ML20037A446 (3) | |
Text
- @
.. --(
.-h s
.g.
+
3 Y.
q
'*[t p, -lT 1
x
.s s
1 y,,
.s P-g Ut4T Ocomre Un,'t 1 m.
N 5
- \\
,- q DATE March 12, 1974
\\
y U
+
-t 5
\\
g A
^
~'
L' P,7.R A T I N G STATUS (1
- li REPORTING PERIOD:
Januarv 1 IU
.Tanuary 31, 1974
.%^
\\
a
'\\ CROSS ' HOURS IN REPORTING PERIOD:
.743 s
,q s
\\ #
D 2
2568 MWe-NET 871 N,**, AWRRENTLY AUTEORIZED POWER LEVEL MWe
(
1 1
Nt i,
\\' d i,
g.
N 70'JCR'i.EVIh,TO WHICH RESCICTED,*.!? ANY):
- 7 5
u~+>%
'j
- w
- 4... REbQS FDR RESTRICTIONS (IF AhT)i 1l
$s e<
,\\1 S
L
,4
,17HIS CUMUI.ATIVE e
s s
j bl.TH -,YR-IO-DATE TO DATE V
'e( \\ \\ ~
y-G i
,6.,
^ g,s q
ys
[
~ '. ;
- 5. Motifs RfACTORINM CMTICAL 3$6 4 l136.6
'~4690.5
.i s.
.s
%r i
v..
t r, 6.. iiOURS GENERATOR ON INE 295.1,,
295.1 3284.2
/-
x
- \\ ' 7.g CynSs T4ERMAL'FOWER GENERATED (MWu) 653807 653807'.
6664688 y-s
-w 8.)CEOSS ELE'.TFUnit. POWkpENERATED (MWH) 221952 1,221952 1 2310540
-i
\\
R* ~
9.y FET AtCTdCAL' fb'ER'CENERATED'(MWH) 205649 203649 _
2164727 N
s x
s o
/
...f 10.' ' REACTOR ' AVAILABILITY.JACTOR f1)
's 45.3 45_3 t
W 97.7 s.
-- R.
-y a
-r g
114 yPLA'CgAILABILITY FACTOR (2) 39.7 39a7-s 68.'4
..i 1
[,
J12.7 PLANT CAPACITY FACTOP (3)'
h
- 31.8 31.8 51.8 n,,
' '. [> m r;
.?
w
's 10.8 10.8 9.1 13.
TO W.D OUTAGE RATE (4) 4
,W s m.-
\\.
^
14(,SHUTD'OQSSCHEDULEDTOBEGININNEXT61T ATp
'PE, DATE AND
,m DURATIG M E'EACH): Two week shutdown fc
_.catscns to high energy,,
. ',line cuuide containngnt 'to 4m.knence Aprn 24, 1974.
\\
- 't x
+ qth '7F SH1'"I&'N AT E::D OFs PODRT TER10D, ESTIMATED DATE OF STARTUP:
s g
'O
,)
N Y,
=s m
s s.
\\ 16..P1 ANTS'IN TEST $TATUS (PRIOR TO'00MUERCIAL OPERATION) REPGhT THE FOLLb'.!ING:
G
, f~..,,
,~~
u
.'\\DATE LAST DATE REASON FOR
.c g
2
,.",+ ~
s
, Q" F? RECAST ACHIEVED DIFFERENCE
's
+
m m
g
, mTur. cRITPA;. Ins t5 g
6 i
(
4% ' N 3 g,t..
\\
7'
- x INIITAL Eld
- CTRId'. D~
\\
^
[t\\\\T POWps'TENENTION d
t*
E.
Q-Q,%
,,, 'g
,t
'(
w,
g
, COMMERCIAL OPERATIO
-\\g
_=
'y s:
- s.,
3
\\
st (kREACTOR AVAIdABILITT FACIOR = E0XRS REACTOR WAS CRTTICAL i *100 s
- i. s GR053 Il0URS IN REPORTINC PERIOD '
3,
- \\s
~ s(2), PLANT AVAILABILITY FACTM = FOURS CENERATOR ON-LTNit
' 100 s
w s
s
'N GROSS HOURS *IN REPORTING' PERIOD
~
"g m
s
('
- . (3) PLANT CAPACITY,FA
- : TOR = NET ELECTRTCAL J'0WER GD2tRAED C
'l.' CURRENTLY,LICENfU1 POWER LEVEL
- CROSS 1100RS IN REPORTING PERIt' e
(4) PORCED OUT CE RATE = TbdCED OUTACE'110URS
- 100 LOURS GENERATOR ON-LINE.+ FORCED OUTAGE 110UR s
s M
L 8001239
~
.N.,
c.
+
~
b
'5. C"-
_T
' O
i i
~
k UNIT Oconee Unit 1 0
DATE
.3/12/74
./.
t
.s i
.i i' DAILY PLANT-POWER OUTPUT l
\\
MONTH January, 1974
)
'\\
.f / <
DAY AVERAGE DAILY MWe-net DAY AVERAGE DAILY HWe-net 8820 1
-113 22 4
23-
-825 2
-138_,
t 3
-158 24 11393 16979
4
-165 25 5
-150 26 20556
/
20289 L
-180 27 1
20865 7
-140 28 20473
-133 29 8-i,,
20650 S'
-163?
30 20697 l
10
-507 31 N
11
-240 12'
-119 13
-115. s i
14
-120
-117 15 16
-322
).-786, 17 l
4128 18
/
12150
>,t 19 4
1604) 20 17205 r
21 l
=
4 m
=
=
D01ARY:
UNIT NAME Oconee Unit 1 DATE March 12, 1974 REPORiMONm January,1974
- FLANT' SHUTDOWNS r
k TYPE METHOD OF F-TORCED DURATION SHUTTIND DOWN.
NO.
DATE S-SCHEDULED (HOURS)
REASON (1)
THE REACTOR (2)
COM: T.i,
1 740101 S
412.5 B
A 2
740122 F
35.7 A
C Cenerator differential relay 87C failed causing-turbine-generator / reactor trip.
m.
(1) REASON:
(2) METRO 3:
A-EQUIFMENT FAILURE (EXFLAIW)
A-MArJAL -
B-MAINT. OR. TEST B- !*/.fUAL SCRAM i
C-REFUELING C-TJIOMATIC SCRAM D-REGULATORY RESTRICTION E-OPERATG2 TRAINING M.'D LICENSE EXA'.IINATION F-AD 11NISTRATIVE G-OPERATIO;3AL ERROR i
(EX?!.AIN) i l
-