ML20033A599

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IE Insp Repts 50-277/81-19 & 50-278/81-20 on 810804-0903. Noncompliance Noted:Failed to Meet Tech Specs for Inoperative Primary Containment Isolation Valves or Average Power Range Monitor
ML20033A599
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 09/16/1981
From: Blough A, Cowgill C, Mccabe E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20033A590 List:
References
TASK-2.E.4.1, TASK-2.E.4.2, TASK-2.K.3.13, TASK-2.K.3.15, TASK-TM 50-277-81-19, 50-278-81-20, NUDOCS 8111250610
Download: ML20033A599 (18)


See also: IR 05000277/1981019

Text

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50-278/810813

50-278/810830

50-277/810808

50-277/810812

50-277/810827

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT ~

Region I

50-277/81-19

,

Report No.

50-278/81-20

50-277

Docket No.

50-278

DPR-44

C

License No. DPR-56

Priority

Category

C

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Licensee: Philadelphia Electric Company

2301 Market Street

Philadelphia, Pennsylvania

Facility Name: Peach Bottom Atomic Power Station, Units 2 and 3

Inspection at: Delta, Pennsylvania

Inspection conducted: August 4 - September 3, 1981

Inspectors:

C0 kU h , h

iIf6f&l

i

C. J. Cowgill, III, Senior Resident-

date signed

Inspector

e,c. L % %., k

sluft!

A. R. Blough, Resident Inspector

date signed

Approved by:

& . O. A % b

ill6/88

E. C. McCabe, Jr., Chief, Reactor

date signed

Projects Section No. 28, DRPI

Inspection Summary:

Inspection on August 4 - September 3, 1981

(Combined Inspection Report Nos. 50-277/81-19 and 50-278/81-20)

Areas Inspected:

Routine, onsite regular and backshift inspections by the

resident inspectors (53 hours6.134259e-4 days <br />0.0147 hours <br />8.763227e-5 weeks <br />2.01665e-5 months <br /> Unit 2; 42 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br /> Unit 3). Areas inspected

included accessible portions of the Unit 2 and Unit 3 facilities, radiation

protection, physical security, operational safety, control room activities,.

LERs, periodic reports, TMI action plan items, surveillance testing, and open

items.

4

8111250610 811105

PDR ADOCK 05000277

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PDR

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Results: Noncompliances: None in seven areas, four in three areas (failure

- to take re' quired Technical Specification actions for inoper tive Primary

' Containment Isolation Valves, Detail 4; failure to take required. Technical

Specification actions for inoperative APRM, Detail 4; inadequate drawing

-

control, Detail 8; failure to log temperatures dur.ing primary system cooldown,

Detail 7).

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DETAILS

1.

Persons Contacted

W. H. Alden, Engineer-in-Charge, Nuclear Section

M. J. Cooney, Superintendent, Generation Division (Nuclear)

J. K. Davenport, Maintenance Engineer

G. F. Dawson, I&C Engineer

  • R. S. Fleishmann, Assistant Station Superintendent

A. Fulvio, Results Engineer

N. Gazda, Health Physics, Radiation Protection Manager

F. W. Polaski, Reactor Engineer

S. R. Roberts, Operations Engineer

D. C. Smith, Outage Coordinator

S. A. Spitko, Site Q.A. Engineer

S. Q. Tharpe, Security Supervisor

W. E. Tilton, Refuel Floor Supervisor

  • W.

T. Ullrich, Station Superintendent

A. J. Wasong, Test Engineer

H. L. Watson, Chemistry Supervisor

J. E. Winzenried, Technical Engineer

R. H. Wright, Test Engineer

Other licensee employees were also contacted during the inspection.

  • Present at exit interviews on site and for summation of preliminary

inspection findings.

2.

Previous Inspection Item Update

(Closed) Unresolved Item (79-07-01, 79-06-01), review OSR committee audit

transmittal dates for 1978. Timeliness of audit report issuance was the

subject of a noncompliance in combined reports 79-13 and 79-15.

Corrective actions were found adequate in combined reports 80-31 and

80-23. This item is closed.

3.

Plant Operations Review

a.

Logs and Records

A sampling review of logs and records was made to:

identify

significant changes and trends; assure that required entries were

being made; to verify that operating orders and night orders conform

to Technical Specification requirements; check correctness of

communications concerning equipment and lock-out status; verify

jumper log conformance to procedural requirements; and to verify

conformance to limiting conditions for operations.

Logs and records

e

reviewed were:

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(1) Shift Supervision Log - August 4 - September 2, 1981

(2) Unit 2 Jumper Log - Current Entries

_(3) Unit 3 Jumper Log - Current Entries

(4) Reactor Engineering Log - Unit 2 - August, 1981

(5) Reactor Operators Log - Unit 3 - August 4 - September 2,

1981

(6) Reactor Operators-Log - Unit 3 - August s - September 2,

1981

(7) CO Log Book - August 4 - September 2, 1981

(8) STA Log Book - August, 1981 (Sampling)

(9) Night Orders - Current Entries

(10) Radiation Work Permits (RWP's) - Various in both Units 2 and

3'- August, 1981

(11) Maintenance Request Forms (MRF's) - Units- 2 and 3, (Sampling) -

August, 1981

(12) Ignition Source Control Checklists (Sampling) - August,1981

(13) Operation Work & Information Data - August, 1981

Control room logs were reviewed pursuant to requirements of

Administrative Procedure A-7, " Shift Operations."' Frequent

initialing of entries by licensed operators, shift supervision, and

licensee on-site management constituted evidence of licensee review.

Logs were also reviewed to assure that plant conditions, including

abnormalities and significant operations, were accurately and

completely recorded.

Logs were also assessed to determine that

matters requiring reports to the NRC were being processed as

suspected reportable occurrences. This' area is discussed further'in

Detail 4.

b.

Facility Tours

During the course of this inspection, which also included shift-

turnover, the inspector conducted daily tours and made observations

of:

Control Room (daily)

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-- ' Turbine Building-(all levels)

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-Reactor Building - (accessible areas)

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Diesel Generator Building;

-Yard _ area and perimeter exterior to the power block,-including

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-Emergency Cooling Tower and torus dewatering. tank

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Security Building, including CAS, Aux.SAS, and control point

monitoring

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Vehicular Control

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The SAS and power block control points

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Security Fencing

--

Portal Monitoring

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Personnel and Badging

Control of Radiation and High Radiation areas, including locked

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door checks

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TV monitoring capabilities

Off-Shift Inspections during this inspection period and the areas

examined were as follows:

DATE

AREAS EXAMINED-

August 11

Control Room observations, Unit 3

refuel floor observations and

Reactor Building tour.

August 12

Control Room observations,

tour of cable spreading room

and radwaste building (165-

foot elevation)

August 21

Control Room observations,

tour of protected area

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September 2

Control Room observations

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Off-Normal Alarms. Selected annunciators were discussed with

control room operators and supervision to assure they were

knowledgeable of plant conditions and that corrective action,

if required, was being taken.

Examples of specific : alarms

discussed during the report period were: -Refueling Water

Storage Tank, High/ Low Level; Computer and Cable Spreading Room

Fire Suppression System Deactivated; " Accumulator" and " Drift"

alarms for individual control rods; and Standby Liquid Tank or

Pipe Temperature, High/ Low. The operators were knowledgeable

of alarm status and plant conditions.

--

Control Room Manning. On frequent occasions during this

inspection,-the inspector confirmed that requirements of 10 CFR 50.54(k), the Technical Specifications and commitments to the

NRR letter of July 31, 1980 for minimum staffing were

satisfied. The inspector frequently confirmed that a senior

licensed operator was in the control room complex. No

unacceptable conditions were identified.

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Fluid Leaks. The inspector observed sump status, alarms,

pump-out rates', and discussed leakage with licensee personnel.

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The inspector noted that the licensee was closely monitoring

Unit 2 drywell unidentified leakage as the maximum allowable

was approached.

Some leaks were found and repaired in an

outage from August 17-25. No unacceptable fluid leak

conditions were identified.

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Piping Vibration. No significant piping vibration or unusual

conditions were identified.

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Monitoring Instrumentation. The inspector frequently confirmed

that selected instruments were. operating and that indicated

values were within Technical Specification requirements. On a

daily basis when the inspector was on site, ECCS switch

positioning and valve lineups (based on control room indicators

and plant observations) were verified.

Examples of

instrumentation observed included flow setpoints, breaker

positioning, PCIS status, radiation monitoring instruments, and

Standby Liquid Control system parameters.

This area is

discussed further in Detail 4.

--

Fire Protection. On frequent occasions the inspector verified

the licensee's measures for_ fire protection. The inspector

observed control room indications of fire detection and fire

suppression systems, spot-checked for proper use of fire

watches and ignition source controls, checked a sampling of

fire barriers for integrity, and observed fire-fighting

equipment stations. On August 12, the inspector informed shift

supervision of a small accumulation of combustibles (white

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coveralls) near the Unit 2 remote shutdown panel -- this

condition was promptly corrected. No. items of noncompliance

were identified.

c.

Follow-up Events Occurring During the Inspection

The inspector followed-up on events that occurred during the

inspection in order to ascertain.the nature and significance of-the

event, verify safe plant conditions, verify licensee conformance to

license conditions and NRC reporting requirements, and evaluate the

need for. additional NRC involvement.

(1) Fire in Rod Position System (RPIS) Circuitry

At 10:15 a.m. August 13, 1981, with Unit 3 in cold shutdown

(for a refueling and .aodification outage), a- small fire

occurred in the rod position indication system (RPIS) fuse box

located in a cabinet in the cable spreading-room. The fire was

quickly _ extinguished, using dry chemical fire extinguishers,

but some sparking continued for about 15 minutes until'the RPIS

was de-energized. All control rods were blocked fully inserted

for Scram Discharge System modifications. The fire was caused

by shorting of an untaped, energized 120 volt-AC lead in an

adjacent cabinet as the power supply drawer was-being removed-

for modification. Workers had taped leads they believed, based

on review of electrical diagrams, to be energized. 'The

inspector toured the control room and cable. spreading room -

shortly after the fire, observed that it was out and that there

was no loss of, or continuing hazard to, additional equipment.

The inspector noted that the fire was not in the vicinity of

any equipment addressed in LER 2-82-38/IP (reference Detail 4).

The inspector reviewed logs and procedures, and discussed the

event with operations personnel. An Unusual Event had been

declared, and emergency plan procedures had been followed.

In

reviewing emergency plan implementing procedures, the inspector

noted that, for all levels of emergencies, notification of the

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NRC via the Regional Office is specified.

Per 10 CFR 50.72,

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and licensee administrative procedure, notification of

emergencies should be made to the NRC Headquarters Duty Officer

using the Emergency Notification System (ENS). The licensee

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stated that procedures would be changed; the inspector will

review the revised nrocedures.

The licensee was not able to

quickly determine why a fire, rather than merely blown fuses,

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had occurred.

Components involved were sent off-site for

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detailed analysis. This item will receive further NRC review.

(277/81-19-01; 278/81-20-02).

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(2) Unplanned Release of Radioactive Water to Storm Drains

About 8 10 a.m., August 30, the licensee discovered that water

had leaked through the Unit 3 Reactor Building railroad access

door. The water backup was caused by a clogged reactor-

building floor drain system and Reactor Water Cleanup pump seal

failure. The licensee immediately dammed the water at the

railroad door. Samples at the drain the Reactor Building

showed IE-3 microcuries per milliliter activity.

It was

estimated that between 10 and 100 gallons of water entered the

storm drain system. The storm drain in the front of the Unit 3-

Reactor Building showed SE-6 microcuries per milliliter

activity, with Zinc-65 the principle isotope.

Samples at the

culvert at the discharge to the Conowingo Pond showed no

detectable activity.

The area outside the Reactor Building

railroad access door was immediately decontaminated. No

personnel contamination resulted. The licensee notified the

NRC Duty Officer of this occurrence via the Emergency

Notification System.

The inspector reviewed sample results from August 30, observed

~ that the railroad door had been dan.med, and held discussions

with licensee personnel regarding long-term corrective actions.

Licensee management stated that modifications to prevent

recurrence were being reviewed in conjunction with corrective

action described in PECO response to NRC Immediate Action

Letter 81-18 (Reference Combined In.pection Report 277/81-07

and 278/81-09).

4.

Review of Licensee Event Reports (LERs)

a.

The inspector reviewed LERs submitted to the NRC:RI office to verify

that the details of the event were clearly reported, including the

accuracy of the description of cause and adequacy of corrective

action. The inspector determined whether further information was

required from the licensee, whether generic implications were

indicated, and whether continued operation of the facility was

conducted in accordance with Technical Specifications.

Report

accuracy, compliance with current reporting requirements and

applicability to other site systems and components were also

reviewed.

The following LERs were reviewed:

LER No.

LER Date

Event Date

Subject

2-81-37/IP

August 10, 1981 August 8, 1981

Failure to initiate

August 12,

281 (clarification)

shutdown when PCIS

August 13, 1981 (correction)

limiting conditions

for operation were

not satisfied

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2-81-38/IP. August 13, 1981 August 12, 1981

Fire protection program

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2-81-38/1T

August 26, 1981

safe shutdown analysis

indicated that cables-

associated with 4KV

emergency bus breaker

control were not

adequately separated

2-81-39/IP

August 27, 1981 August 27, 1981

Operation with inadequate

LPRM inputs from one level

(core height) to an

APRM

3-81-13/IP

August 31,_1981 August 30, 1981

Unplanned release of

radioactive water into

the storm drain system

(see Detail 3)

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LER No. 2-81-37/IP

About 7:30 a.m. on August 8, operators found a HPCI turbine

exhaust drain line-isolation valve, A0-4248, failed closed due

to a failed solenoid coil. The HPCI turbine exhaust drain line

is a one-inch line.

In order to ensure HPCI system

operability, shift personnel ~ mechanically blocked the valve

open at about 11:30 a.m., and.left the redundant, in-line-air

operated isolation valve open. Shift personnel verified

operability of the in-line valve prior to mechanically blocking

A0-4248. These valves are Primary Containment Isolation System

(PCIS) valves; and Technical Specifications require that PCIS

valves be operable or closed, or that an associated in-line

valve be closed and logged once every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

If this

condition cannot be met, then a plant shutdown is to be

initiated and cold shutdown reached within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

In this

case, less than the required containment integrity existed for

about 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />.

The inspector reviewed logs, surveillance tests, maintenance

documents, and held discussions with various licensee staff

personnel to determine the causal factors for this event.

Sequence of events.

(All times approximate)

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TIME

EVENT

7:30 a.m., August 8

A0-4248 found closed. Cause

determined to be failed solenoid

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11:30 a.m., August 8

A0-4248 mechanically blocked

open

2:05 p.m., August 8

Blocking permit applied for

repair of AO-4248

Time Unknown (prior to

Shift supervision log entry

3:00 p.m., August 8)

identifying problem with

A0-4248

3:00 p.m., August 8

Shift' turnover

6:30 p.m., August-8

. Maintenance request-2-23-M-1-35

completed and associated blocking,

permit cleared

Time unknown (prior to

Log entry in shift supervision

11:00 p.m. August 8)

log, "U/2 HPCI A0-4248 (23-138)

Repair, Tested 0.K.:and Returned

to Service."

11:00 p.m., August 8

Shift turnover

7:00 a.m., August 9

Shift turnover

7:20 a.m., August 9

Shift discovered A0-4248 still

blocked in_the open position.

Valve returned to service

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Log Review

In reviewing logs, the inspector noted that no log entries-

regarding the status of A0-4248 were made in the Unit 2 reactor

operators log book. Additionally, no mention of the abnormal

condition of A0-4248 was made on the shift turnover sheet for-

the Unit 2 reactor operator or shift supervisor.

The inspector noted that a surveillance test for checks on

inoperable isolation valves had not been used. Also,

information tags, an optional method available to convey

information which may be useful to other personnel, were not

,

used.

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Discussions with Station Personnel

The inspector discussed the event with various operators,

senior operators and station' management personnel involved.

These discussions identified that confusion' existed on

information transfer regarding the event.

The Unit 2

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afternoon Shift Supervisor and Reactor.0perator were not

provided with complete information regarding the status of

A0-4248. Both operators indicated that they.were informed that

the solenoid was being repaired but not that the valve was

mechanically blocked open. The inspector concluded that

communications inadequacies lengthened the period of valve

inoperability.

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Maintenance and Testing Activities

Maintenance, testing,'and return to service of valve A0-4248

was logged in the shift supervision log as complete before

11:30 p.m. on August 8, but the valve'was determined still-to

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be blocked open (i.e., inoperable for containment isolation

functions) during the operator's routine panel check at 7:20.

a.m., August 9.

Maintenance Request Form No. 2-23-M-1-35, for

repair of valve A0-4248, specified in Section 7, " Operation

Verification," a test for:

"No air leaks". The documented

test result (performed August 8) was: "None heard".

Station procedures require that post-maintenance testing assure

-valve operability. The specified test did not meet these

requirements, in that the containment isolation function of the =

valve in question was not tested. The inspector concluded that

the failure to adequately test after repair lengthened the

period of valve inoperability.

Findings

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A0-4248 was mechanically t, locked open for about 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />. The

redundant PCIS isolation valve was not closed.

No reactor

shutdown was initiated. The failure to comply with the

Technical Specification Limiting Condition for Operation is a

violation (277/81-19-02).

Station administrative procedures require that significant

equipment abnormalities be logged in the operator's logs.

Additionally, post maintenance testing is required to show that

equipment is operable.

The failure to log the abnormalities

associated with A0-4248 and to adequately test the valve after

repair is considered part of the above violation.

The inspector noted that Group I, II, and III PCIS valves are

provided with color-coded switch handles on control' room

panels.

No similar memery aid has been provided for Groups IV

and V (HPCI and RCIC) PCIS valves. HPCI and RCIC turbine

exhaust drain isolation valves shut on any turbine trip, as

well as in Primary Containment Isolation, to provide turbine

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isolation. Although.no' contribution to this event was

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substantiated, the inspector recommended that station

-management consider visual aids for these and similar valves.

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LER No'. 2-81-38/1P and l

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For the eight, 4KV bus breakers (per unit) which feed the 4KV

emergency buses from the two'off-site power supplies, control

cables for all breakers for a unit are run through the 'same

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cable trays from the cable spreading room to the remote

shutdown panels. A single fire could disable cortrol of all

the breakers. Diesel generators would still be available, and

I would start automatically on a LOCA signal,.but might have to

be manually closed in on the buses.

Licensee immediate

corrective actions during Unit 2 operations included marking of

the affected trays, stationing of a continously-roving fire -

watch, restricting use of ignition sources in the areas, and

increasing the emphasis on good housekeeping in the area.

PORC-reviewed instructions ware issued to operating personnel

that, in event of a fire that could affect the cables, the 4KV-

buses were to be supplied by the diesels and a Unit 2 shutdown

initiated. The inspector spot-checked implementation of these

actions and discussed provisions with licensed operators. No

inadequacies were noted.

Permanent corrective modifications

are being designed. On August 28 the inspector discussed this'

issue with the licensee and was informed that the problem

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applies also to Unit 3.

The licensee is endeavoring to

complete permanent modifications at Unit 3 during the current

outage. Additionally, the licensee identified an inadequacy.in

protective relays for the breakers--certain protective features

(related to offsite power supply transformer conditions) for

all associated 4KV breakers are fed from a single relay'in the

control room.

Individual, separated relays are needed. The-

inspector verified that the latest information was included in

revised instructions ta the operators and in the followup LER.

The inspector will review the licensee's permanent resolution

of this design problem (81-19-05 and 81-20-02).

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LER No. 2-81-39/IP

With the Unit shutdown on August 18,LPRM 32-49C failed upscale

and was by passed. This left only one operable LPRM input to

the 'C' level of APRM 'C'.

Technical Specifications require

two LPRM inputs per level for'an APRM to be considered

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operable. The unit was started up on August 24. At times

during operation, the 'A' Logic Trip System was receiving input

.C

from only one fully operable APRM because either APRM 'A'

or

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'E' was periodically by passed. When the problem was

discovered at 00:05 a.m. on August 27, APRM 'C' was promptly

by passed and subsequently returned to operability. The

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licensee was not able to determine for what period of time

either the 'A'

or the 'E' APRM had been by passed.

Technical

Specifications require two operable APRMs per trip system;

otherwise, either the trip system shall be tripped or all

,

operable control rods shall be inserted within four hours.

l

Failure to meet the Technical' Specification Limiting Condition

i

for Operation from startup on August 24 until 00:05 a.m.,

August 27, is s noncompliance (277/81-19-04).

During the time when less than the required number of inputs

were available, APRM 'C' apparently responded properly to power

changes from both rod movement and flow adjustments. All LPRM

inputs from the

'A', 'B'

and 'D' levels were operable.

Improper APRM response would have been detected by the

operators through routine checks of the instruments du' ring

power changes and during steady-state operations.

Additionally, process computer printouts used by the reactor

engineer during power ascension would have indicated an

abnormal " gain adjustment factor", and excessive gain

adjustments during APRM calibrations would have been required.

No such inconsistencies were identified by the licensee. The

inspector reviewed process computer printouts of core

y~

performance parameters and identified no abnormalities.

The inspector discussed this occurrence with licensee

representatives and reviewed licensee procedures.

There are no

formal checks to verify two LPRM inputs per level for APRMs.

The licensee is examining this inadequacy and stated that tha

subject would be addressed in the followup report.

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The inspector also expressed concern that other reactor

f

engineering requirements may receive no formal checks (e.g.,

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MFLPD not routinely compared to fraction of rated power; see IE

Report 277/81-03).

The inspector observed that an APRM may be

left by passed unnecessarily, which does not appear to be good

engineering practice.

For example, the inspector observed on

August 28 that, at Unit 2, one APRM in each logic trip system

was by passed, possibly from testing the previous day. No

notation regarding APRMs being by passed had been made in

reactor operator turnover sheets since startup four days

earlier.

The turnover sheet includes a section for

instrumentation by passed or out of service. These

observations were provided to station management.

5.

Radiation Protection

During this report period, the inspector examined work in progress in

accessible areas of the Unit 2 and Unit 3 facilities. Areas examined

included:

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a.

Health Physics (HP) controls

b.

Badging

c.

Usage of protective clothing

d.

Personnel adherence to RWP requirements

-e.

Surveys

f.

Handling of potentially contaminated equipment and materials

Add *+.ionally, inspections were conducted of usage of friskers and portal

monitors by personnel exiting various RWP areas, the power block, and the

licensee's final exit point. More than 50 people were observed to meet

frisking requirements of Health Physics procedures during the month. A

samplina of high radiation doors were ve.rified to be locked as required.

No unacceptable conditions were identified.

6.

physical Security

'

The inspector spot-checked compliance with the Accepted Security Plan and

implementing procedures, . including operations of the CAS and SAS, over 20

spot-checks of vehicles onsite to verify proper control, observation of

protected area access control and badging procedures on each shift,

inspection of physical barriers, checks on control of vital area access

and escort procedures. No unacceptable conditions were identified.

7.

Surveillance Testing

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Du-ir.; facility and control room tours the inspector observed portions of

surveillance tests in progress and spot-checked recorded data.

Following

a normal shutdown and cooldown of Unit 2 on August 17-18, the inspector

reviewed the completed test ST 9.12, " Reactor Vessel Temperatures," used

to record temperatures.during heatups and cooldowns. The test had been

properly initiated. Data was properly recorded. Calculations were

t

correct. At about 220 degrees, cooldown temperature logging was stopped

at 5:00 a.m.

Temperaturas had changed 42-47 degrees in the preceding

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45 minutes. ST 9.12 requires continued temperature logging at least

,

every 15 minutes until less than five degrees di ference occurs between

any two readings taken 1.n a 45 minute period. This .is a violation.

1

(277/81-19-06). The inspector noted that cooldown had progressed in a

deliberate, controlled manner, well within Technical Specification limits

for'cooldown rate.

Recorder traces m ntaining'all required temperatures

were reviewed for the period during which required logging was not done.

The inspector reviewed ST 9.12 as performed for a previous cooldown of

~

each unit.

Logging of temperatures in each case had continued until

completion of the cooldown (about 150 to 160 degrees Farenheit).

In

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reviewing these tests, the inspector also noted that the " Test Frequency"

statement, as written, was potentially susceptible to being misread.

This comment was provided to licensee management.

8.

Review of TMI Action-Plan (TAP) Requirements

The inspector reviewed the status of licensee action on the following TAP

requirements to verify that the licensee is meeting his NRC commitments,

a.

TAP Item II.E.4.1--Dedicated Hydrogen Penetrations

Plants using external recombiners or purge systems for post-accident

combustible gas control of the containment atmosphere should provide

containment penetratit.n systems for external recombiner or purge

systems that are dedicated to that service only, that meet the

redundancy and single-failure requirements of General Design

Criteria 54 and 56 of Appendix A to 10 CFR 50, and that are sized to

satisfy the flow requirements of the recombiner or purge system.

The licensee reviewed this item and responded that the criteria

would be met with addition of two isolation valves: one outboard of

the radioactive gas sampler valves, and one on the nitrogen

compressor suction line.

NRC:NRR letters dated October 29, 1980 and

August 18, 1981 concluded that the design changes met the General

Design Criteria and satisfied.this TAP item. The inspector reviewed

modification packages, interviewed licensee personnel and observed

in plant indicators to verify that the modifications had been

adequately implemented.

PORC review was verified, and selected

procedures and drawings were checked. The inspector noted that, for

Unit 2, one controlled copy of drawing M-372, "P&ID, Containment

Atomsphere Dilution System" had m t been updated to include the

radioactive gas sampler isolation valve, installed October, 1980.

When notified, a licensee representative promptly corrected this

oversight. The inspector also verified that Technical

Specifications had been amended to include the new valves. The

inspector had no further questions regarding this TAP item.

Based on the above-noted inadequacy in a controlled drawing, the

inspector reviewed a larger sample of drawings and procedures to

verify that modifications had been properly incorporated. A

sampling of ten procedures was reviewed and no inadequacies noted.

The shift supervision and the control room copies of seven selected

drawings were reviewed. The inspector noted that a new revision of

drawing M-372 had been issued. On the new revision, the radioactive

gas sampler valve was not clearly depicted on either copy reviewed.

The in-line valve denotion was unclear, and the valve number and

operator were not discernible. Two of three licensed operators

questioned believed the print shcwed a section of pipe with no

valve.

Failure to update and maintain controlled drawings following

piant modifications violates requirements for appropriate (up-to-date)

drawings in 10CFR50 Appendix B Criterion V, Peach Bottom QA Plan Section

2, and Peach Bottom Precedure A-6. (217/81-19-03)

,

.

..

16

b.

TAP Item II.E.4.2.5--Containment Isolation Dependability

Pressure Setpoint

The containment setpoint pressure that initiates containment

isolation for non-essential penetrations must be the minimum

compctible with normal operating conditions (within one PSI of

maximum pressure normally expected). The licensee's response, dated

January 8, 1981, justifies the current setpoint of 2.0 PSIG using

-rationale outlined in NUREG-0737. NRC:NRR accepted this submittal

in a letter dated July 14, 1981. This item is closed.

c.

TAP Item II.E.'4.2.7--Containment Isolation Dependability

--High Radiation Trip

Containment purge and vent isolation valves must close on a high

radiation signal. The licensee's December 22, 1980 submittal

indicated that discussions with the licensing staff were in progress

and that a schedule for implementation would follow. The inspector

contacted the NRC Licensing Project Manager, who stated that the

item is still under discussion, and further correspondence will

result. This item remains open.

d.

TAP Item II.K.3.13--HPCI and RCIC Initiation Levels-

The initiation levels of the HPCI and RCIC system should be

separated so that the RCIC system initiates at a higher water level

than the HPCI system.

Further, the initiation logic of the RCIC

system should be modified so that the RCIC system will restart on

low water level. These changes have the potential to reduce the

number of challenges to the HPCI system and could result in less

stress on the vessel from cold water injection. Analyses should be

performed to evaluate these changes, and submitted to the NRC staff.

Modifications shall be implemented if justified by the analyses.

The licensee participated in a Boiling Water Reactor Owners' Group

program to study this issue. The owners group conclusion, endorsed

by the licensee, was that separation of the initiation levels would

yield only minimal reduction in the thermal cycle history.

-_ Automatic restart of the RCIC was considered beneficial, however. A

representative of NRR stated that the owners group report is under

review.

-The licensee committed to implementation of the automatic restart

feature by July 1, 1981. The inspector reviewed the modification

package, verified PORC review of the modification, and interviewed

licensee personnel. The modification makes the high reactor water

level trip effective on the steam' supply valve rather than the

. _ _ _ -_ - . - _ - _ _ _ _ _ _ _ . - _ - _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

17

turbine trip and throttle valve, so that no manual. reset is-

required. The modification was completed at Unit 2 on June 18,

1981, and is being completed during the current Unit 3 outage. This

item remains open (Unit 3 only).

e.

TAP Item II.K.3.15--HPCI and RCIC Break-Detection Logic

The HPCI and RCIC steam line break detection circuitry should be

modified so that pressure spikes resulting from. system initiation

will not cause inadvertent system isolation.

The licensee participated in a BWR Owners' Group evaluation of this

issue and concluded that a time delay in the break detection

circuitry should eliminate any spurious isolations from flow peaks

during a normal system start. Further, the time delay preserves the

4

break detection. capabilities and does not impact on the design basis

accident analysis of HPCI and RCIC steam line breaks. An NRC:NRR

representative stated that the owners group position is under staff

review.

,

i

The licensee committed to installation of a three-second time delay

,

feature by July 1, 1981.

The inspector reviewed the modification

package, verified PORC review of the modification,-and interviewed

licensee personnel. PORC minutes indicated that no Technical

Specification change was needed, whereas the Safety Evaluation

.

recommended additions to the Technical Specifications but concluded

' .

that prior approval was not needed. 14 licensee representative

stated that the inconsistency was an oversight in PORC minutes and

that revision would be submitted for PORC review.

(The actual

Technical Specifications change request had been received by PORC in

-

,

!

a separate action).

Further, the licensee reviewed other

modifications in progress during the current Unit 3 outage and

determined that clarification of PORC minutes was warranted in one

additional case. The modification was completed at Unit 2 on May

26, 1981 and is being completed during the current Unit 3 outage.

.

This item remains open (Unit 3 only),

9.

In-Office Review of Monthly and Special Reports

j

The following licensee reports have been reviewed in-office onsite.

3

a.

Peach Bottom Atomic Power Station Monthly Operating Report for:

July, 1981 dated August 14, 1981

This report was reviewed pursuant to Technical-Specifications and

verified to determine that operating statistics had been accurately

reported and that narrative summaries of the month's operating

'

experience were contained therein. No unacceptable conditions were

identified.

7

~. - * - - -

.

. - .

-

. -

- - .

. .

-

- - - -

_-__._-____._.___.,___.__.------.___.____._-_a

-

. - - -

-

_ _ _ _ _ _ _ _ _ _ _ _ . _ - _

_

-

_

_ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ -

- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ .

. .

. .

r

18

b.

Thermal Mapping Reports:

No. 81-2 for July 22, 1981, transmitted August 17,.1981

.,

No. 81-3 for July 28, 1981, transmitted August 17, 1981

These reports were reviewed pursuant to Environmental Technical

Specifications to verify that the required data had been. submitted to

NRC:NRR. No unacceptable conditions were identified.

'

10. Management Meetings--Preliminary Inspection Findings

A summary of preliminary findings was provided to the Station

Superintendent at the conclusion of the inspection. During the period of

this inspection, licensee management was periodically notified of the

preliminary findings by the resident inspectors.

The dates involved, t!-

senior licensee representative contacted, and subjects discussed were as

follows.

Date

Subject

Senior Licensee Representative Present

,

August 7

Routine discussions

Station Superintendent

August 12

LER 2-81-37/IP (Detail 4)

Assistant Station Superintendent

August 14

Routine Discussions

Station Superintendent

,

August 19

Maintenance procedural

Maintenance Engineer

adherence

August 20

Shift Operations Procedural

Operations Engineer

Adherence

,

August 21

LCO and procedural adherence Station Superintendent

4

(Detail 4), Surveillance

Testing (Detail 7), and

Routine Discussions

August 28

Routine Discussions

Station Superintendent

September 3

Summary of Preliminary

Station Superintendent

Findings

!

2

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