ML20032B639
| ML20032B639 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 10/08/1981 |
| From: | Bettenhausen L, Rekito W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20032B631 | List: |
| References | |
| 50-278-81-21, NUDOCS 8111050744 | |
| Download: ML20032B639 (12) | |
See also: IR 05000278/1981021
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U.S. NUCLEAR REGULATORY' COMMISSION'
0FFICE OF INSPECTION AND ENFORCEMENT.
Region ~I
Report No.
50-278/81-21
Docket No.
50-278
License No.
Priority
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Category
C
Licensee:
Philadelphia Electric Company
2301 Market Street
Philadelphia, Pennsylvania ~19101
Facility Name:
Peach Bottom Atomic Power Station, Unit 3
Inspection at:
Delta, Pennsylvania
Inspection' conducted: August 31, 1981
- September 8, 1981
-/;)1-
/O/6[/P/
Inspectors:
/d
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W.'A. Rekito,-Reactor Inspector
date s1gned-
Approved by:
,_ M M N ha---
/d/F/g/ -
. H. Bettenhausen, Chief, Test Programs,Section,
date sigried.
Engineering Inspection Branch, DE&TI
Inspection Summary:
Inspection on August 31 - September 8,1981(Report No. 50-278/81-21)
Areas Inspected:
Routine unannounced i.7 ea. tion of containment integrated
leakage rate test activities; outage maintenance activities; shutdown plant-
activities; and licensee action on previous inspection findings. The inspection
involved 42 inspector-hours onsite by one region-based NRC inspector.
Results: One item of noncompliance was identified in one area.
(Failure to
perform leakage test following maintenance on containment boundary, paragraph
4.g).
Region I Form 12
Aa.41 m
(Rev. 8111050744 811015
PDR ADOCK 05000278
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. DETAILS
1.
Persons Contacted
E. Black, Assistant Foreman, Mobile Turbine Group
J. Davenport, Engineer-Maintenance
J. Doering, Results Engineer
R. . Fleischmann,' Assistant Station Superintendent -
- A. Fulvio, Results Engineer
- K. Mandl, Quality Assurance Auditor-
- C. Mengers, Quality Assurance Site Supervisor
- W. Ullrich, Station Superintendent
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-* A. Wasong, Test Engineer
H. Wilkerson, Bechtel Corporation.
- rc Blough, Resident Reactor Inspector
C. Cowgill, Senior Resident Inspector
The inspector also interviewed.other. licensee employees-during the inspection
- including reactor operators, technical support, and maintenance personnel.
- denotes those present at the exit interview.
2.
Licensee Action on Previous Inspection Findings
(0 pen) ' Unresolved Item (278/77-28-05)i
Site records of-Type B and C
local-leak rate test dates for penetrations N-231A and B did not agree
with the dates reported to the NRC in the 1977 Unit 3 Reactor Containment
. Building Integrated Leakage Rate Test Report.
The licensee determined
' that the report was in error and committed to correct this discrepancy by
submitting *a am ended version of the subject report to the NRC by October
21, 1981.
(0 pen) Unresolved Item (278/77-28-07): Apparent inaccurate reporting cf
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MSIV 80B local leak rate test .results ir. the 1977 Unit 3 Reactor Containment
Building Integrated Leakage Rate Test Report. The licensee determined
that the identified report error had not yet been corrected.and committed.
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to submitting an amended version of the subject report to the NRC by
October 21, 1981.
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3.
Containment Integrated Leakage Rate Test (CILRT) Procedure Review
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a.
Documents Reviewed
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Procedure ST 12.5-1, Revision 2, " Integrated Leak Rate Test".
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Peach Bottom Technical Specification Section 4.7, Containment
Systems.
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Dwg. No. M-351, Revision'.18, fluclear Boiler.
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Dwg. No.' M-332, Revision -8, Primary Containment Leak Testing.
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Dwg. No. M-308, Revision ~ 16, Feedwater and Feed Pumps.
.Dwg.~ No. M-362, Revision 19, Core Spray Cooling System.
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Dwg.'No. M-365, Revision 19, High Pressure Coolant Injection
System.
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Dwg. No. M-367,' Revision 17, Containment Atmospheric Control
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System.
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Procedure-RT 8.0, Revision 0, Safety. Instrument Valving Che'ck
Off List.
b.
Scope
The inspector reviewed Procedure ST 12.5-1, " Integrated Leak Rate
' Test," for technical adequacy and compliance with 10 CFR 50, Appendix
J, ANSI /ANS-N56-8-1981, and Peach Bottom Technical Specifications.
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The following are.some of the key aspects of the CILRT requirements
verified by the inspector:
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Containment Interior Inspection specified;
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Special Instrumentation requirements specified and instrument
error analysis performed;
Isolation valve closing mode specified to be normal;
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Valve lineups specified venting and draining of lines as required
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to prevent the creation of artificial leakage barriers that
could not be expected to exist following a Design Basis Accident
(DCA);
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Use of Test Events-Log specified;
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Method of pressurization, minimum test pressure, and depressuriza-
tion properly specified;
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Minimum test data requirements specified;
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Results evaluation techn'ique properly specified;
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Systems required to remain in operation to support the test and
assure re ator safety were pr'operly specified;
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Appropriate corrections to test results specified for sys"..ms-
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not properly vented or drained and changes to the containment
free air volume; and
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Acceptance criteria properly speciffed.
c.
_ Findings
With the exception of the one item below, the inspector found no
problems with the test procedure and had no further questions'in
this area.
The inspector noted that Procedure ST 12.5-1, Revision 2, contained
valve lineups to verify that the ' root valves forLinstrumentation
were in the proper position, but individual instrument isolation,
vent, and drain valves were not addressed in_the procedure. The
licensee representative was aware of'this fact and stated that the-
pre-startup surveillance RT 8.0, " Safety Instrumentation Valving
Check Off List" would be performed coincident with the CILRT valve
lineup to verify that all instruments are inLtheir proper normal
alignment and this would be documented in the Events Logs.
Review-
of this procedure along with general guidance for system valve
lineup requirements contained in the CILRT procedure' satisfied the
inspector's concern.
'4.
Containment Integrated Leakage Rate Test (CILRT)
a.
General
On' September 2-6, 1981, the Peach Bottom Atomic Power Station, Unit
3, performed a CILRT as required by 10 CCR 50, Appendix J and_ Technical Specification 4.7. A.
The test was performed in accordance with
Procedure ST 12.5-1, Revision 2, " Integrated Leak Rate Test". . The
inspector witnessed preparations for and various portions of the
test, verified qualifications of test personnel and independently
verified calculations of the test results. Details of the test are
discussed below.
b.
Instrumentation
The inspector reviewed the calibration records for the resista. ice
temperature detectors, dew point hygrometers, precision pressure
indicators, and.the verification test flowmeter. Their calibration
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prior to the CILRT met applicable accuracy requirements and were
traceable tu the National Bureau of Standards.
No noncompliances were identified.
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c.
Tours
The inspector conducted'several inspection. tours independently and
with licensee personnel both before and during the CILRT. During
these tours, test boundaries' were surveyed for- evidence of leakage
and on a sampling basis, selected valves were verified to be in-the
correct positions. These selected valves included test boundary
isolation ~ valves and vant-paths external to the test volume. -No;
valve misalignment were identified and no discrepancies were noted.
d.
Chronology
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Date
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Description,
P/2
2000
Drywell internal inspection complete.
9/3
Complete valve lineup verifications.
0645
Drywell ' sumps pumped down.
1605
Commence pressurization of containment.
System inspections for external leakage conducted.
Various small liquid leaks discovered at valve
stem packing were quantified and documented as
required in Appendix L of. test procedure.
Significant air leakage discovered at flange on
one drywell pressure transmitter, PT-3-5-12C.
9/4
0400
Containment reached test pressure of 64.130
psia. Secured pressurization.
0415
Began initial dat- recording at 15 minute intervals.
0700
Noted unstable drywell temperature changes and
corresponding pressure drop.
0730
Repressurized due to reaching minimum test
pressure.
0745
Secured two drywell cooling fans.
0940
Added water via Shutdown Cooling Keep Full
System to raise reactor water level.
1030
Adjusted the Chilled Wa'.er Cooling System flow
and number of drywell cooling fans in service to
stabilize temperatures.
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Date
Time
Description
1430
Temperature stabilization' requirements satisfied.
Continued data! recording.
Continued leakage' surveys.
2200
Calculated leakage rate of approximately 0.391
percent per day recognized to exceed acceptance
criterion of 0.375.
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2305-
Isolated leaking PT-3-5-12C and conducted local
leakage' rate test with results:being approximately
.9 SCFM.
9/5
0200'
Decision made to declare the initial CILRT
attempt a failure and rerun-the test-with.
PT-3-5-12C isolated.
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0300
Drywell Equipment Drain Sump pumped down.
Continued data. recording and leakfrate calculations.
1345
Completed 8 hocr. leakage rate test with a calculated
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leakage rate at the upper;95% confidence limit
of-0.151 percent per. day.
1445
Commenced test data-verification' test with.
imposed leakage rate of .5 %/ day (4.41 SCFM).
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1945
Completed'5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> test data. verification. test.
~2230
Commenced depressurization.
9/6
0830
Depressurization complettd and: system restoration
begun.
9/7
1000-
Completed post repair local leakage rate test of -
PT-3-5-12C with zero leakage.
No items of noncompliance were identified with the conduct of the
CILRT.
e.
CILRT Results
-(1) Initial Attempt
The initial attempt of the CILRT, from 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> on September
3 to 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on September 4 revealed a significant air leak
at,a flange on one drywell pressure sensing . instrument (PT-3-5-12C).
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The licensee's evaluation of leakage rate including required
corrections for systems in service indicated the overall contain-
ment leak rate at the 95% confidence interval to be 0.391
percent per day which exceeded the test acceptance criterion of
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nitial attempt at this
0.375 percent per day. Therefore the i
1981 CILRT was considered to be a failed test.
(2) Successful Test
After isolating PT-3-5-12C, a successful eight hour leakage
rate test was run from 0545 hours0.00631 days <br />0.151 hours <br />9.011243e-4 weeks <br />2.073725e-4 months <br /> to 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> on September 5,
1981. The calculated leakage rate including required corrections
for systems in service and changes in the test volume at the
95% confidence interval was 0.179 percent per day.
The inspector noted that the above leakage rate represented the
final total leakage rate because PT-3-5-12C which was isolated
during the test was local leak rate tested on September 8,
after being repaired, and found to have zero leakage.
The inspector observed data recording, transcription and calcula-
tions during the test.
In addition, the inspector independently
calculated several mass values and the leakage rate, using raw
data from the test to verify the accuracy of the licensee's
leakage rate calculations.
No items of noncompliance were identified in this area.
f.
Future Test Schedule
Paragraph III.A.6.(b) of 10 'r9 50, Appendix J, states that if two
consecutive periodic Type A tests (CILRT) f ail to meet the acceptance
criteria then tests shall be performed at each shutdown for refueling
or approximately every 18 months, whichever occurs first, until two
consecutive periodic tests meet the acceptance criteria
The inspector
noted that the initial attempt of the 1977 and 1981 periodic Type A
test at Peach Bottom Unit 3 failed ta meet the acceptance criteria
and that the licensee was therefore subject to the increased frequency
of tests as described above. The licensee acknowledged this fact
and stated that the 1981 CILRT Technical Summary Report to the NRC
would include an evaluation for the cause of test failure with
generic corrective action plans and a request for exemption from the
increased test frequency requirement.
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Leak Repairs and Special Testing Requirements
Paragraph IV.A of 10 CFR 50, Appendix-J, require's that any modification
or replacement of a component which is part of the primary containment
boundary be followed by a leakage test, as applicable for the area
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affe;ted.
Administrative Procedure A-26, Revision 23, " Procedure for Corrective
Maintenance," requires that a " Maintenance Request-Form" (MRF) be
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used to: (1) specify sufficient rsst repair testing to assure that
the equirment has been returned to a fully operable condition and
(2) document the performance of post repair testing and accentance
for operations.
Following the isolation of.PT-3-5-12C during the CILRT,-this instrument
was disassembled, repaired and leak tested at 50 psig as documented
on MRF 3-60-L-1-95.
During disassembly-the cause of leakage was'
determined to be an "0" ring seal missing from the process flange
(instrument sensing line connection).
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The inspector requested the previous maintenance and test records
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for PT-3-5-12C.
Review of MRF 3-94-L-1-51, dated July 30, 1981,
revealed that t.._ instrument was disassembled for repairs and was
recalibrated on August 19, 1981 in accordance with Procedure ST
2.6.02C-which was specified to be-the applicable post repair test
requirement.
The purpose of Procedure ST 2.6.02C, Revision 4, is stated to verify'
the operability and set point of PT/PIS 3-5-12C.
However, the..
inspector noted that the maximum pressure specified in the procedure
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is 138.7 inches of water (5 psig) which does not prove the functional
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capability of the instrument to act as a primary containment barrier
at the design basis accident pressure of 49.1 psig. The licensee
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acknowledged this discrepancy and identified that the problem is
applicable to nine other primary contlinment instruments calibrated
to normal operating pressure and not design basis accident pressure.
The Station Superintendent stated that the stan'trd practice for
post repair testing of'all instruments was to perform.the normal
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calibration check.
He also stated that due to an oversight, this
amount of . testing is not sufficient for certain primary containment
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instrumentation and final corrective actions would be generic.
The inspector stated that corrective actions taken for PT-3-5-12C
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were acceptable but questioned what assurance was the*e that adequate
post maintenance testing would be performed on primary containment
boundaries prior to implementation of final generic corrective
action. The Station Superintendent stated that the instrument
departmant: personnel would be advised of this requirement and a
review of primary containment instrument work would be conducted
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prior to the next reactor start y .
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Failure to perform a local leakage test' of PT-3-5-12C, which is part
of the primary reactor containment boundary, following maintenance
on August-19, 1981-constitutes an item of noncompliance with 10 CFR 50,. Appendix J and Procedure A-26.
(278/81-21-01)
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Outage Maintenance' Activities
a.
Documents Reviewed
The inspector selected three' major maintenance activities, being-
completed during the current refueling outage, for review.
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(1) Torus to Drywell Vacuum Breaker Modification.
(2) Main Steam Isolation Valve Maintenance.
(3) High Pressure Coolant Injection (HPCI) Turbine Maintenance.
The following procedures and associated Maintenance Request Forms
(MRFs) were reviewed:
Procedure MS-7.2, Revision 0, Torus /Drywell Vacuum Breaker -
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Hinge Arm No. 1 Fabrication.
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Procedure MS-7.3, RLvision C, Torus /Drywell Vacuum Breaker -
Hinge Arm No. 2 Fabrication.
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Procedure MS-7.4, Revision 0, Torus /Drywell Vacuum Breaker -
Hinge Pin Fabrication.
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Procedure M-7.10, Revision 0, Replacement of Torus /Drywell
Vacuum Breaker Hinge Arms, Hinge Pins, Hinge Pin Bushings,
Pallet seal and 24 inch "0" Ring.
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MRS , 3-37-M-1-15,16,17 and 18, Torus Drywell Vacuum Breakers,
Janetry 20, 1981.
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Procedure M-1.3, Revision 6, Main Steam Isolation Valve Maintenance.
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Procedure MS-1.4, Revision 2, Main Steam Isolation Valve -
Fabrication of "0"-Ring Retainer.
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Procedure M-1.5, Revision 6, Main Steam Isolation Valve Pneumatic
Control Manifold Ma'ntenance.
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Procedure M-1.28, Revision 0, MSIV Pneumatic Control Valve
Rework.
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-- :MRF.3-31-M-1-16,fMSIV A0 80A, completed July 17,'1981.
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MRF 3-31-M-1-17, MSIV A0 80B, comp.leted March. 19, 1981.
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.MRF 3-31-M-1-18, MSIV A0 80C, completed May 8, 1981.
MRF 3-31-M-1-19,.MSIV A0 80D, completed June'25, 1981.
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MRF 3-31-M-1-20, MSIV A0 86A, completed May" 12,~ 1981
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MRF 3-31-M-1-22, MSIV A0 86C, completed May 22, 1961.
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MRF:3-31-M-1-23, MSIV A0.86D, completed June 15, 1981.
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Procedure M-23.1, Revision 0, High Pressure Coolant Injection
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(HPCI) Pump Drive Turbine Maintenance.
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Procedure M-23.10, Revision 1, HPCI Woodward Governor Remate
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Servo Maintenance.
Procedure M-23-11, Revision 0, HPCI. Turbine Stop. Valve / Hydraulic
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Cylinder. Maintenance.
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Procedure M-23-13, Revision 1, HPCI' Pump Drive Turbine Casing
Disassembly and Reassembly.
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Procedure M-23-15, Revision 1, HPCI Overspeed Trip Device.
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MRF 3-23-M-1-18, January 26, 1981, Perform 5 year Inspection,
~ Perform 011 Flush, Install new Governor.
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MRF 3-23-M-1-20, January 26, 1981, Replace HPCI Rupture Disc.
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MRF 3-23-M-1-134, July 23, 1981, Repair _and Set Overspeed Trip
Device.
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b.
Scope
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The inspector reviewed the above documents to ascertain that maintenance
activities were being conducted in accordance with approved procedures
' which met applicable regulatory guidance. . The following are key
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aspects of maintenance procedure requirements verified by the: inspection.
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Administrative controls established for. system / equipment prior;
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to and during maintenance activities.
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'QA inspection / audit requirements.identifled.
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'Special_ process'and personnel' qualification requirements identified.
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Equipment classification =and special material certification
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requirements identified.
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General Housekeeping.and system / component cleanliness requirements
identified.
--- Post maintenance test requirements specified.
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. Administrated approval for return of system / equipment to~ service.
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No items of noncompliance were identified during this review.
c.
Work Activity Witnessing
On September 1, 1981, the inspector observed maintenance technicians
performing work on the.HPCI turbine.
They were installing the
Woodward Governor and restoring the lube oil piping to normal following
the lube oil system-flush. The work was being performed.in accordance
with Procedure M-23.4 and the Turbine Instruction Manual.
The
inspector _ interviewed the technicians and foreman who were turbine
repair specialists and determined that they were knowledgeable of
procedural requirements and were suitably qualified for the_ work
being done.
No' items of noncompliance were identified and the inspector had no
further questions in this area.
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6.
Facility Tours
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The inspector made 'several tours of the f acility including the Reactor
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Building, Relay Room, and Control Room.
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During-these tours, the inspector observed operations and activities in
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progress, implementation of radiological controls, general condition of
safety related equipment, component tagging and system operations to
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support the CILRT.
No items of noncompliance were identified.
7.
Exit Interview
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The inspector met with licensee representatives (see detail 1 for attendees)'
at the conclusion of the inspection on September 8, 1981. The inspector
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summarized the scope and findings of'the ' nspe: tion at that time.
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Regarding the future CILRT schedule described in paragraph 4.f, the
Station Superintendent acknowledged the requirement for increased frequency
of tests.
Regarding the item
noncompliance in paragraph 4.g, the Stulon Superin-
tendent stated
.. che post maintenance calibrations had erroneously
been conside
,atisfactory for assurir.g containment leak-tight integrity
and that e
ective actions would be generic to all primary containment
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instrum- . tion.
In addition, he stated that prior to the next reactor
start
a review would be conducted to assure that all containment
ins'
...ientation work was adequately leak tested following maintenance.
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