05000321/LER-1983-002-03, /03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced

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/03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced
ML20028G091
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 01/27/1983
From: Tipps S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028G089 List:
References
LER-83-002-03L, LER-83-2-3L, NUDOCS 8302070388
Download: ML20028G091 (1)


LER-1983-002, /03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced
Event date:
Report date:
3211983002R03 - NRC Website

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NRC FORM 366 U.S. NUCLE AR REGL LATORY COMMISSION

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i E, VENT DESCRIPTION AND PPOH ABLE CONSEQUENCES h lo12_JlWhile performing the "IlYDRAULIC SHOCK AND SWAY ARRESTOR INSPECTION AND l

g l FUNCTIONAL TEST" surveillance procedure, a snubber was discovered to bc l [oj4_j l inoperable. Tech. Specs, section 3.6.L.4.

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loisIl y this repetitive event as last reported on LER 50-321/1982-090.

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