ML20028C984

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Revised Monthly Operating Rept for Nov 1982
ML20028C984
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 12/01/1982
From: Norris H
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20028C979 List:
References
NUDOCS 8301140374
Download: ML20028C984 (2)


Text

_

OPERATING DATA REPORT .

, h DOCKET NO: 50-261 DATE: 821201 w COMPLETED BY: H. Ray Norris

. TELEP110NE: (803) 383-4524 OPERATING STATUS Notes:

1. Unit Name: H. B. Robinson Unit #2
2. Reporting Period: 821101, 0000 / 821130, 2400
3. Licensed Thermal Power (FMt): 2300 There are presently 157 spent fuel
4. Nameplate Rating (Gross' M'.le): 739 assemblies in the spent fuel pool.
5. Design Electrical Rating (Net FMe): 700
6. Maximum Dependabic Capacity (Gross FMe): 700 ..
7. Maximum Dependable Capacity (Neti FMe):_ 665 4
8. IfReasons:

Changes Occur in Capacity No change ' Ratings (Item Number 3 through  ;

7) Since Last, Report Give
9. Power Level to Which Restricted, If Any (Not FMe):
10. Reasons For Rest,rictions, If Any:_ Although the unit 1955 MW't Reactor Power is not restricted by any outside agency, the power level is presently reduced due to steam generator considerations .

This Month ~ Yr.-to-Date Cumulative

11. Hours in Reporting Period 720 8.016
12. Number of Hours Reactor Was Critical 102942 688.97 3786.9 76132.32
13. Reactor Reserve Shutdown Hours 31.0 3
14. Ilours Generator On-Line 31.03 *1271.12 687.2 3575.84
15. Unit Reserve Shutdown Hours O' 74131.15 0 23.20
16. Gross Thermal Energy Generated (IMH)

_ 1265349.6 6372019.6

17. Gross Electrical Energy" Generated (?MH) 404872 149467393.6
18. Net Electrical Energy Generated (MWU) 2014395 48092365 380823 1860227
19. Unit Service Factor 45480478
20. Unit Availability Factor __ 95.4 4 44.61 72.01 93.44 44.61
21. Unit Capacity Factor (Using MDC N'et) .

72.03 79.54 34.89

22. Unit Capacity Factor (Using DER Net) 66.44 -
23. Unit Forced Outage Rate _ /5.56 _ 33.15 63.11

~

, _=4.3b _*7.90 14.29

24. _Shutdowns Type Two Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

5/14/83. Four week steam generator inspection outade.

3

25. .If Shut Dcwn At End of Report Period, Estimated Date of Startup: 12/1/82
26. Units In Test Status (Prior to Commercial Operation):

i' Forecast Achieved t INITIAL CRITICALITY --

INITIAL ELECTRICITY f --

COMMERCIAL OPERATION --

l 8301140374 830103 PDR ADOCK 05000261

! R PDR i

j

  • Corrected on 830104 5

cg 9777)

-- - - . - . . .- _ - e u -

DOCKET NO. 50-261

- UNIT SHUTDOWNS AND POWER REDUCTIONS ~ UNIT NA\1E H. B. Robinson "- '-

j

. DATE 821201

  • COMPLETED BY H. Ray Norris' REPORTMONTilN ovember TELEPilONE (803) 383-4524 e.

E

= 'Cause & Correstive 5?

E 4 .u,5 sx Licensec ,E r., b Action to No. Date g 3g ( jgy Event g,? Prevent Recurrence H 8,: $ j;5g Report 8 my [S3 -

,2 - 'g -

=

-- W VALVEX S/G chemistry was unacceptable due F *32.80 A 3 i 11-1 821129 . - to mechanical . failure of caustic injection valves. This resulted. in j . .

~ inleakage of sodium hydroxide into the make-up water system and*from there to the S/G's. The va.lves were replaced.

% ~

3 4

! - 2 . Method: Exhibit G-Instructions

  • F: Forced Reaum: for Preparati m of Data l.Madual S: Scheduled A l'quipment Failure (Explain). 2-Manual Scram. Entr> Sheets for Licensee .

Il Mainter.ance of Test

  • Event Report (LER) File (NUREG-
3. Automatic

C. Refueling .

4 Other (Explain) ' 0161)

D.Regulatiny Resiriction .

E-Operaio Training & License Examination 5 F Admmistrative Exhibit ! Same Source G Operational Errur (Ex' plain) .

ll Other (Explain) 19/77) -

  • Corrected on 830104 - su-o- -

} *t 1

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