ML20028C984
| ML20028C984 | |
| Person / Time | |
|---|---|
| Site: | Robinson |
| Issue date: | 12/01/1982 |
| From: | Norris H CAROLINA POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML20028C979 | List: |
| References | |
| NUDOCS 8301140374 | |
| Download: ML20028C984 (2) | |
Text
_
OPERATING DATA REPORT h
DOCKET NO: 50-261 DATE: 821201 w
COMPLETED BY:
H. Ray Norris TELEP110NE: (803) 383-4524 OPERATING STATUS Notes:
- 1. Unit Name:
H. B. Robinson Unit #2
- 2. Reporting Period: 821101, 0000 / 821130, 2400 There are presently 157 spent fuel
- 3. Licensed Thermal Power (FMt):
2300 assemblies in the spent fuel pool.
- 4. Nameplate Rating (Gross' M'.le):
739
- 5. Design Electrical Rating (Net FMe):
700
- 6. Maximum Dependabic Capacity (Gross FMe):
700
- 7. Maximum Dependable Capacity (Neti FMe):_
665 4
- 8. If Changes Occur in Capacity Ratings (Item Number 3 through 7) Since Last Report Reasons:
No change '
, Give
- 9. Power Level to Which Restricted, If Any (Not FMe):
- 10. Reasons For Rest,rictions, If Any:_ Although the unit 1955 MW't Reactor Power is not restricted by any outside agency, the power level is presently reduced due to steam generator considerations This Month ~
Yr.-to-Date Cumulative
- 11. Hours in Reporting Period 720 8.016 102942
- 12. Number of Hours Reactor Was Critical 688.97 3786.9 76132.32
- 13. Reactor Reserve Shutdown Hours
- 14. Ilours Generator On-Line 31.0 3 31.03
- 1271.12 687.2 3575.84 74131.15
- 15. Unit Reserve Shutdown Hours O'
0 23.20
- 16. Gross Thermal Energy Generated (IMH)
- 17. Gross Electrical Energy" Generated (?MH)
_ 1265349.6 6372019.6 149467393.6 404872 2014395
- 18. Net Electrical Energy Generated (MWU) 48092365 380823 1860227 45480478
- 19. Unit Service Factor
- 20. Unit Availability Factor
__ 95.4 4 44.61 72.01 93.44 44.61 72.03
- 21. Unit Capacity Factor (Using MDC N'et) 79.54 34.89 66.44
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rate
_ /5.56
_ 33.15 63.11
~
_=4.3b
_*7.90 14.29
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
_ Type Two 5/14/83. Four week steam generator inspection outade.
- 25..If Shut Dcwn At End of Report Period, Estimated Date of Startup:
12/1/82
- 26. Units In Test Status (Prior to Commercial Operation):
3 Forecast Achieved i
INITIAL CRITICALITY t
f INITIAL ELECTRICITY COMMERCIAL OPERATION l
8301140374 830103 PDR ADOCK 05000261 R
PDR i
j
- Corrected on 830104 5
cg 9777)
e u
DOCKET NO. 50-261 UNIT SHUTDOWNS AND POWER REDUCTIONS ~
UNIT NA\\1E H. B. Robinson DATE 821201 j
COMPLETED BY H. Ray Norris' REPORTMONTil ovember TELEPilONE (803) 383-4524 N
e.
E 4.u,5 sx Licensec
,E r.,
b
'Cause & Correstive
'=
5?
E Action to
Date g
3g
(
jgy Event g,?
Prevent Recurrence 8,:
j;5g Report 8 my H
,2
- 'g
=
W VALVEX S/G chemistry was unacceptable due 11-1 821129 F
- 32.80 A
3 to mechanical. failure of caustic i
injection valves. This resulted. in j
~
inleakage of sodium hydroxide into the make-up water system and*from there to the S/G's.
The va.lves were replaced.
~
4 3
2 Method:
Exhibit G-Instructions F: Forced Reaum:
l.Madual for Preparati m of Data S: Scheduled A l'quipment Failure (Explain).
2-Manual Scram.
Entr> Sheets for Licensee
- 3. Automatic Scram.
Event Report (LER) File (NUREG-Il Mainter.ance of Test C. Refueling 4 Other (Explain) '
0161)
D.Regulatiny Resiriction E-Operaio Training & License Examination 5
F Admmistrative Exhibit ! Same Source G Operational Errur (Ex' plain) 19/77) ll Other (Explain)
- Corrected on 830104
- t 1
- su-o-
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