ML20028C982

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Monthly Operating Rept for Dec 1982
ML20028C982
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 01/04/1983
From: Norris H
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20028C979 List:
References
NUDOCS 8301140370
Download: ML20028C982 (3)


Text

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OPERATING DATA. REPORT

~

. DOCKET NO: 50-261 DATE: 830104 9

~ COMPLETED BY:

H. Ray Norris -

TELEPHONE: (803) 383-4524 OPERATING STATUS Notes:

1. Unit'Name:

H.

B'. Robinson Unit #2 2.' Reporting Period: 821201, 0000 / 821231, 2400 There are presently 157 spent fuel

3. Licensed Thermal Power,(FMt):

2300 assemblies in the spent fuel pool.

4. Nameplate Rating (Gross PMe):

739

5. Design Electrical Rating (Not FMe):

-700

, 6. Maximum Dependable Capacity (Gross FMe): 700

7. Maximum Dependable Capacity (Net FMe):

665

~

8. If Changes Occur in Capacity Ratings (Item Number 3 through 7) Since Last Report, Give Reasons:

No change'

9. Power Level to Which Restricted, If Any (Net FMe):

1955 MWt Reactor Power 10._ Reasons For Restrictions, If Any: Although the unit is not restricted by any outside agency l. the power level is presently reduced due to steam generator considerations.

~

This Month' Yr.-to-Date Cumulative

11. Hours in Reporting Period 744 8,760 103,686-
12. Number of Hours Reactor Was Critical 707.35 4494.25 76,839.67
13. Reactor Reserve Shutdown Hours 36.65 67.68 1307.77.
14. Hours Generator On-Line 704.9 4.280.74 74.836.05

.15. Unit Reserve Shutdown Hours 0

0

-23.20

16. Cross Thermal Energy Generated (FMH) 1,297,144.8 7,669,164.4 150,764,538.2-
17. Cross Electrical Energy Generated (FMH) 416,398 2,430,793 48;508,763
18. Net Electrical Energy Generated (MWil) 391,624 2,251,851 45,872,102 19, Unit Servide Factor 94.74 48.86 72.17-
20. Unit Availability Factor 94.74 48.86 72.19
21. Unit Capacity Factor (Using MDC N'et) 79.15 38.65 66.52
22. Unit Capacity Factor (Using DER Net) 75.19 36.72 63.20

~

23. Unit Forced Outage Rate 5.25 7.47 14.21
24. Shutdowns Scheduled Over Next 6 Honths (Type, Date, and Duration of Each):

Type Two 5/14/83, Four week steam generator inspection outage.

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25. If Shut Down At End of Report Period, Estimated Date of Startup:

1/1/83

26. Units In Test Status (Prior to Consacreial Operation):

Forecast Achieved L

INITIAL CRITICALIiY L~

INITIAL ELECTRICITY L

COMMERCIAL OPERATION 8301140370 830103 PDR ADOCK 05000261 l:

R PDR (9/77)

cs

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AVERAGE DAILY UNIT l'OWER LEVEL DOCKET NO.

50-261 UNIT _ H. B. Robinson DATE 830104 CO3tPLETED BY IL Rav Norris s

TELErilONE (803) 383-4524 P.iONT11 December DAY AVERAGE DAILY POWER LEVEL '

DAY AVERAGE DAILY POWER LEVEL (h!We Net) thiWe Net) i 59 37 563 556

~

2 gg 561 3

560 39 498 561 561 4

20 557 g

21 564 560 6

22 564 564 7

23 8

561 24 565 9

560 25 564 10 560 26 564 560 27 563 561 565 12 28 562 563 g3 29 14 562 30 563 562 36 gg 3,

. 562 16 INSmUCTIONS On this format. list the antag daily unit power levet in.\\twe Net for each d:y in the reporting month. Compute to the nestest whole sneg2wstt.

(9/77) s.; +

DOCKET NO. 50-261 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT N A\\tE H. B. Robinson DATE 830104

-COMPLETED BY H. Ray Norris REPORT MONTil December TELEPilONE (803) 383-4524 w.

Cause & Corrective

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.Yh Licensee E-r, N," -

DJEC i.

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.E 5 E Event g7 3.?

Action to ~

cE jdi g Report *

<dy y0 Prevent Recurrence d

WC

'VALVEX S/G chemistry was unacceptable due 11-1 821201 F

17. 5 5,

A 3

to mechanical f ailure of caustic injection valves. This resulted in inleakage of sodium. hydroxide into the make-u'p water system and*from there to the S/G's.

The va,1ves were replaced. As the reactor was being manually shut down for outage, an automatic trip' occurred due to a -

source range spike upon reenergizing, resulting in reactor trip.

HB INSTRU A 'f aulty fuse holder caused the power, 12-1 821231 F

21.5 5 A

3 solenoid for "C" MSIV, to de-energize closing the MSIV which caused a low-low level in "C" S/G and sub-seqdent unit trip.

4 3

2 Method:

Exhibit G -Instructions 1

for Preparation of Data F: Forced Iteason:

1-Manua!

S: Scheduled A l'quipment Failure (Explain) 2-Manual Scrarn.

Entrs Sheets for Licensee J-Automatic Scram.

Even't Rep.nt (LER) Fde (NUREG.

Il Mainter.ance of Test

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C Refueling 4 Other (Explain) 0161)

D Itegulatory Restriction E-Operator Training & License Examination 5

F Administrative Exhibit 1.Sanw Source G Operational Error (Ex' plain)

N/77)

Il-Other (Explain) 4 b-

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