05000339/LER-2009-001, Regarding Automatic Start of 2H EDG Due to Loss of B Reserve Station Service Transformer

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Regarding Automatic Start of 2H EDG Due to Loss of B Reserve Station Service Transformer
ML091810109
Person / Time
Site: North Anna Dominion icon.png
Issue date: 06/22/2009
From: Stoddard D
Virginia Electric & Power Co (VEPCO)
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
09-288 LER 09-001-00
Download: ML091810109 (5)


LER-2009-001, Regarding Automatic Start of 2H EDG Due to Loss of B Reserve Station Service Transformer
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
3392009001R00 - NRC Website

text

1 OCFR50.73 Virginia Electric and Power Company North Anna Power Station P. 0. Box 402 Mineral, Virginia 23117 June 22, 2009 U. S. Nuclear Regulatory Commission Serial No.:

09-288 Attention: Document Control Desk NAPS:

MPW One White Flint North Docket No.: 50-339 11555 Rockville Pike License No.: NPF-7 Rockville, MD 20852-2378

Dear Sirs:

Pursuant to 10CFR50.73, Virginia Electric and Power Company hereby submits the following Licensee Event Report applicable to North Anna Power Station Unit 2.

Report No. 50-339/2009-001-00 This report has been reviewed by the Facility Safety Review Committee and will be forwarded to the Management Safety Review Committee for its review.

Sincerely, Daniel G. Stoddard, P.E.

Site Vice President North Anna Power Station Enclosure Commitments contained in this letter: None cc:

United States Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-8931 NRC Senior Resident Inspector North Anna Power Station

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSIO APPROVED BY OMB NO. 3150-0104 EXPIRES: 8/31/2010 (9-2007)

, the NRC may digits/characters for each block) not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE NORTH ANNA POWER STATION, UNIT 2 05000 339 1 OF 4
4. TITLE Automatic Start of 2H EDG Due To Loss of "B" Reserve Station Service Transformer
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REV MONTH DAY YEAR FACILITY NAME DOCUMENT NUMBER NUMBER NO.

05000 04 28 2009 2009 001 00 06 22 2009 FACILITY NAME DOCUMENT NUMBER 05000

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)

E] 20.2201(b)

[]

20.2203(a)(3)(i)

[F]

50.73(a)(2)(i)(C)

E]

50.73(a)(2)(vii)

[]

20.2201(d)

E] 20.2203(a)(3)(ii)

[3 50.73(a)(2)(ii)(A)

E]

50.73(a)(2)(viii)(A) 1 E] 20.2203(a)(1)

[] 20.2203(a)(4)

E]

50.73(a)(2)(ii)(B)

E]

50.73(a)(2)(viii)(B)

[]

20.2203(a)(2)(i)

[]

50.36(c)(1)(i)(A)

L]

50.73(a)(2)(iii)

E]

50.73(a)(2)(ix)(A)

10. POWER LEVEL

[]

20.2203(a)(2)(ii)

[]

50.36(c)(1)(ii)(A)

[]

50.73(a)(2)(iv)(A)

[I 50.73(a)(2)(x)

F] 20.2203(a)(2)(iii)

[]

50.36(c)(2)

El 50.73(a)(2)(v)(A)

El 73.71(a)(4)

El 20.2203(a)(2)(iv)

E]

50.46(a)(3)(ii)

[]

50.73(a)(2)(v)(B)

[]

73.71(a)(5)

E] 20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

El 50.73(a)(2)(v)(C)

[3 OTHER 100%

El 20.2203(a)(2)(vi)

El 50.73(a)(2)(i)(B)

El 50.73(a)(2)(v)(D)

VOLUNTARY LER

12. LICENSEE CONTACT FOR THIS LER FACILITY NAME TELEPHONE NUMBER (Include Area Code)

E. S. Hendrixson, Director Station Safety and Licensing (540) 894-2108CAUSE SYSTEM COMPONENT MANU-REPORTABLE j CAUSE SYSTEM COMPONENT MANU-REPORTABLE FACTURER TO EPIX FACTURER TO EPIX B

EA CBL K080 Y

14. SUPPLEMENTAL REPORT EXPECTED
15. EXPECTED MONTH DAY YEAR SUBMISSION El YES (If yes, complete 15. EXPECTED SUBMISSION DATE)

EW NO DATE ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)

On April 28, 2009, at 0953 hours0.011 days <br />0.265 hours <br />0.00158 weeks <br />3.626165e-4 months <br />, with North Anna Unit 2 operating at 100% power (Mode 1), Control Room Operations personnel received several annunciators simultaneously that indicated that the "B" Reserve Station Service Transformer (RSST) tripped and locked out.

The Unit 2 "H" Emergency Diesel Generator (EDG) automatically started on a Degraded Voltage/Under Voltage signal due to the loss of the "B" RSST.

The Unit 2 "H" EDG automatically picked up the load of the Unit 2 "H" emergency bus as designed. The "B" Charging/SI pump and "B" Component Cooling pump auto started due to the loss of power.

Operations personnel entered appropriate abnormal procedures and stabilized the plant.

An 8-hour Non-Emergency Report was made to the NRC at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, in accordance with 10 CFR 50.72 (b)(3)(iv)(A), for an event that resulted in the automatic actuation of an EDG and Charging/SI pump. This event posed no significant safety implications since the Unit 2 "H" EDG started as designed and re-energized the emergency bus. The health and safety of the public were not affected by this event.

NRC FORM 366 19-2007)

PRINTED ON RECYCLED PAPER NRC FORM 366 (9-2007)

PRINTED ON RECYCLED PAPER (If more space is required, use additional copies of (If more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17) of the 2H EDG to standby and the clearing of the EDG TS action statements.

5.0 ADDITIONAL CORRECTIVE ACTIONS

Temporary Modification 2009-1809 was initiated to disconnect the 1 B and 2B Station Service Buses from the "B" RSST. A prompt Operability Determination was made with compensatory action to leave the 1B and 2B Station Service Buses disconnected. Visual inspection of the overhead cables along with thermography of the A and C RSS overhead cables was also performed. The "A", "B" and "C" RSS overhead cables will be replaced from the tube bus to normal switchgear.

6.0 ACTIONS TO PREVENT RECURRENCE In addition to the cable replacement, changes are being made to the operating and test procedures along with revisions to the Design/Installation Standards NAS-3014, Specification for Electrical Installation for North Anna Power Station and STD-EEN-0002, Nuclear Electrical Design Standard for Cable.

7.0 SIMILAR EVENTS

LER N2-07-002-01 documents a similar event occurring on March 7, 2007 where the "B" Reserve Station Service Transformer (RSST) tripped and locked out on a phase "B" to ground short.

8.0 ADDITIONAL INFORMATION

At the time of this event, North Anna Unit 1 was operating at 100 percent power.

IPRINTED ON RECYCLED PAPER