05000348/LER-1981-056-03, /03L-0:on 810817,supply Breaker for 1A Charging Pump Was Inadvertently Racked Out.Caused by Personnel Tagging Unit 2 Pump 2A Instead of Unit 1 Pump 1A.Personnel Counseled

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/03L-0:on 810817,supply Breaker for 1A Charging Pump Was Inadvertently Racked Out.Caused by Personnel Tagging Unit 2 Pump 2A Instead of Unit 1 Pump 1A.Personnel Counseled
ML20010G774
Person / Time
Site: Farley 
Issue date: 09/09/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010G766 List:
References
LER-81-056-03L, LER-81-56-3L, NUDOCS 8109220513
Download: ML20010G774 (1)


LER-1981-056, /03L-0:on 810817,supply Breaker for 1A Charging Pump Was Inadvertently Racked Out.Caused by Personnel Tagging Unit 2 Pump 2A Instead of Unit 1 Pump 1A.Personnel Counseled
Event date:
Report date:
3481981056R03 - NRC Website

text

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