05000311/LER-1981-084-03, /03L-0:on 810810,leak Rate Calculation Indicated RCS Leak to Reactor Coolant Drain Tank.Caused by Packing Leakage on Valve 22RC20.Valve Repacked & Leak Rate Reduced

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/03L-0:on 810810,leak Rate Calculation Indicated RCS Leak to Reactor Coolant Drain Tank.Caused by Packing Leakage on Valve 22RC20.Valve Repacked & Leak Rate Reduced
ML20010F279
Person / Time
Site: Salem 
Issue date: 08/28/1981
From: Dickey F
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010F271 List:
References
LER-81-084-03L, LER-81-84-3L, NUDOCS 8109090556
Download: ML20010F279 (1)


LER-1981-084, /03L-0:on 810810,leak Rate Calculation Indicated RCS Leak to Reactor Coolant Drain Tank.Caused by Packing Leakage on Valve 22RC20.Valve Repacked & Leak Rate Reduced
Event date:
Report date:
3111981084R03 - NRC Website

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