05000311/LER-1981-082-99, /99X-0:on 810603 & 27,inadvertent Safety Injection Occurred Following Turbine/Reactor Trip.Caused by High Steam Line Flow Conditions Set Up by Steam Driven Auxiliary Feedwater Pump Speed Oscillations

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/99X-0:on 810603 & 27,inadvertent Safety Injection Occurred Following Turbine/Reactor Trip.Caused by High Steam Line Flow Conditions Set Up by Steam Driven Auxiliary Feedwater Pump Speed Oscillations
ML20010E710
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/26/1981
From: Macwatters R
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010E709 List:
References
LER-81-082-99X, LER-81-82-99X, NUDOCS 8109080183
Download: ML20010E710 (1)


LER-1981-082, /99X-0:on 810603 & 27,inadvertent Safety Injection Occurred Following Turbine/Reactor Trip.Caused by High Steam Line Flow Conditions Set Up by Steam Driven Auxiliary Feedwater Pump Speed Oscillations
Event date:
Report date:
3111981082R99 - NRC Website

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