05000364/LER-1981-028-03, /03L-0:on 810717,main Control Board Steam Flow Indicator of FT-474 Instrumentation Loop Failed High.Caused by Transmitter Vent Pipe Break Due to Use of Oversized Valve in Sensing Line.Lighter Valve Installed

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/03L-0:on 810717,main Control Board Steam Flow Indicator of FT-474 Instrumentation Loop Failed High.Caused by Transmitter Vent Pipe Break Due to Use of Oversized Valve in Sensing Line.Lighter Valve Installed
ML20010D218
Person / Time
Site: Farley 
Issue date: 08/18/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010D212 List:
References
LER-81-028-03L-01, LER-81-28-3L-1, NUDOCS 8108240106
Download: ML20010D218 (1)


LER-1981-028, /03L-0:on 810717,main Control Board Steam Flow Indicator of FT-474 Instrumentation Loop Failed High.Caused by Transmitter Vent Pipe Break Due to Use of Oversized Valve in Sensing Line.Lighter Valve Installed
Event date:
Report date:
3641981028R03 - NRC Website

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2 Event o scmPHON AND PRCEA3LE COS.SicuENcES h [3 12j l At 0610 on 7-17-81, the instrumentation loop associated with steam flow transmitter I

j c,3 ; ; FT-474 was declared inoperable when the main control board steam flow indicator failed l

, high due to breakage of a transmitter vent pipe. Tech. spec. 3.3.1 and 3.3.2, in part, j

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! i: i Lto service at 2210 on 7-19-81. All similar instrumentatior, vent lines were also insoected I

and valves replaced. No such similar condition exists in Unit 1 since the heavier valve was [iiai l selected for use in Unit 2 because of an error on a vendor drawing.

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