LER-1981-046, /03L-0:on 810714,during Normal Operation 120 Ac Vital Bus 3 Was de-energized When Power Was Interrupted at a Inverter.Caused by Station Battery Shorting During Maint Causing a Inverter to Fail |
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60 of DOCK ET NUMBER 68 69 EVENT DATE 14 lb HEPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l o [ 2 l l At 0954 during normal operation 120 A.C. Vital Bus #3A was de-eneroined when power an]
go;3; j interrupted at tha "A" inverter. This created an event contrary to T.S.3.8.2.1.
An QTT] la result of this event.a Reactor / Turbine trip occurred.
Power was restor ed to 1-he l
lol3l l Vital Bus within ten minutes. There was no effect utx>n the health or safety of the 1
[ o lc,1 l general public. This was the first event of this type.and this is the fif t h event-l l 017 l l reported under this specification.
I l O lH ] l 00 7
8 9 SYST E M
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBLODE COMPONENT CODE SUBCODE SUBCODE 1019I I E j C lh ( Ajh [C_j h lB l A lT lT lR lY lh l Z lh (Jd h 7
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10 11 12 13 18 19 20 SEQUE NYl AL OCCURRENCE REPOHT REVISION
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CODE TYPE NO.
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_ 21 22 2J 24 26 27 2H 23 Ju 31 32 ACTION FUTURE EFFECT SHUTDOWN ATT ACHME N T N P R O-4 PRIMF COMP.
COMPONENT TAKEN ACTION ON PL ANT METHOD HOURS 14 SUOMI TT E D FOHM dVB.
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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i j o l lThe cause of this event is attributed to inadvertent shorting of the "A" Station l
[ Battery during maintenance resulting in failure of the "A"
Inverter which was supplying l i i
[ power to the Vital Bus.
THe inverter was repaired. Mainten ce in the battery room l
, j [ij3l lwill utilize tools with insulated handles,and of a length designed to prevent shorting l [and caution signs will be posted at the entran(.e.
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8 9 80 ST S
% POWE H OTER STATUS I C V H DISCOVEHY DESCHIPTION
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i 5 A TlVITY CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTivlTY LOCATION OF RELE ASE l : l 0 l l Z l @ [ Z]@l NA l
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1 N 9 10 11 44 45 80 PE HSONNE L F XPOSUHES NUYHEH TYPf DESCRIPTION '-
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H 9 11 12 13 80 PEHSONNE L INJUHICS NUMBE R DESCnt P flON li la 1 lo lo lo l@l NA l
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8 9 11 12 80 LOSS OF OH DAMAGE TO FAClliTY TYPE DE SC RIP T ION lZl@l NA l
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SUPPIDENTARY INFORMATION.
L Report #50-302/81-046/03Ir0 Facility:
Crystal River Unit 3
' Report Date:
' August '12,1981.
Occurrence Date:
July; 14,1981
- - Identification of. Occurrence:
120 Volt A.C.
Vital Bus #3A was inoperable contrary. to
- Technical Specifica* ion 3 8.2.1.
Conditions Prior to Occurrence:
t 1
Mode 1 - Power Operation (8Q$)
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Description of Occurrence:
At 0954 during normal operation,120 volt A.C._ Vital Bus #3A was de-energized.
- - The "A"
station battery was. shorted during maintenance which blew the output fuse of the "A" inverter which supplied the bus.
As a result of the lost bus the interface' valve for the turbine generator. control 3
fluid opened causing a loss of control fluid resulting in a Turbine / Reactor trip.
Power was restored to the Vital Bus within ten (10) minutes.
Designation of Apparent Cause:
L The cause of. this event is attributed.to a personnel error j
resulting in the short to the battery.
Analysis of Occurrence:
There was no effect upon the health or safety of the general public.
Correctivr, Action:
The "A" Inverter was repaired.
Tools with insulated handles and of a length designed to prevent shorting will be
'obtained for exclusive use in the
_ Battery _ Room.
Additionally, a sign will be installed on the - door to - the Battery Room to.. provide sensitive equipment caution to persons entering.
Failure Data:
L-
' This was the-first event of this type,and this. is the fifth event reported under this specification.
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| 05000302/LER-1981-001-01, /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | | | 05000302/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000302/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000302/LER-1981-002-03, /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | | | 05000302/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000302/LER-1981-003-01, /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | | | 05000302/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000302/LER-1981-004-03, /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | | | 05000302/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000302/LER-1981-005-03, /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | | | 05000302/LER-1981-006-03, /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | | | 05000302/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000302/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000302/LER-1981-007-03, /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | | | 05000302/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000302/LER-1981-008-03, /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | | | 05000302/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000302/LER-1981-009-03, /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | | | 05000302/LER-1981-010-03, /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | | | 05000302/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000302/LER-1981-011, Forwards LER 81-011/01T-1 | Forwards LER 81-011/01T-1 | | | 05000302/LER-1981-011-01, /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | | | 05000302/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000302/LER-1981-012-03, /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | | | 05000302/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000302/LER-1981-013-03, /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. 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