05000364/LER-1981-027-03, /03L-0:on 810714,during Test,A Train Penetration Room Filtration Sys Was Declared Inoperable When Associated Fan Damper Failed to Open.Caused by Faulty Solenoid Valve. Valve Replaced.Sys Returned to Svc

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/03L-0:on 810714,during Test,A Train Penetration Room Filtration Sys Was Declared Inoperable When Associated Fan Damper Failed to Open.Caused by Faulty Solenoid Valve. Valve Replaced.Sys Returned to Svc
ML20010B036
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/06/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010B034 List:
References
LER-81-027-03L-01, LER-81-27-3L-1, NUDOCS 8108130235
Download: ML20010B036 (1)


LER-1981-027, /03L-0:on 810714,during Test,A Train Penetration Room Filtration Sys Was Declared Inoperable When Associated Fan Damper Failed to Open.Caused by Faulty Solenoid Valve. Valve Replaced.Sys Returned to Svc
Event date:
Report date:
3641981027R03 - NRC Website

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10(3; l Filtration Train A (B) Operability Test), the A Train Penetration Room Filtration System l IoI4I lwas declared inoperable when the associated exhaust fan damper (3356 A) failed to open.

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