05000317/LER-1981-052-03, /03L-0:on 810702,containment RMS Pump Tripped on Low Flow,Resulting in Loss of Gaseous & Particulate Radiation Monitors.Cause Not Determined.Throttle Valve Adjusted

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/03L-0:on 810702,containment RMS Pump Tripped on Low Flow,Resulting in Loss of Gaseous & Particulate Radiation Monitors.Cause Not Determined.Throttle Valve Adjusted
ML20010A354
Person / Time
Site: Calvert Cliffs 
Issue date: 07/31/1981
From: Pavis G, Rizzo P
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010A351 List:
References
LER-81-052-03L, LER-81-52-3L, NUDOCS 8108110346
Download: ML20010A354 (1)


LER-1981-052, /03L-0:on 810702,containment RMS Pump Tripped on Low Flow,Resulting in Loss of Gaseous & Particulate Radiation Monitors.Cause Not Determined.Throttle Valve Adjusted
Event date:
Report date:
3171981052R03 - NRC Website

text

NHC FORM 236 U. S. NUCLE AR REGULATORY COMMISSION (7 771 '

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'S REPORT DATE B0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Io I2l l At 0845 during normal oneration, the containment Radiation Monitoring Sys-1 10131 1 tem (RMS) pump tripped on low flow, resulting in a loss of the caseous l

!al4i I and particulate radiation monitors (T.S. 3.4.6.1).

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