05000254/LER-1981-013-03, /03L-0:on 810717,while Performing High Drywell Pressure Calibr & Functional Test,Pressure Switch PS-1-1001-88C Tripped at 2.03 Psig.Caused by Instrument Setpoint Drift.Pressure Switch Recalibr & Tested

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/03L-0:on 810717,while Performing High Drywell Pressure Calibr & Functional Test,Pressure Switch PS-1-1001-88C Tripped at 2.03 Psig.Caused by Instrument Setpoint Drift.Pressure Switch Recalibr & Tested
ML20010A145
Person / Time
Site: Quad Cities 
Issue date: 07/23/1981
From: Weinfurter E
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20010A143 List:
References
LER-81-013-03L-02, LER-81-13-3L-2, NUDOCS 8108110113
Download: ML20010A145 (1)


LER-1981-013, /03L-0:on 810717,while Performing High Drywell Pressure Calibr & Functional Test,Pressure Switch PS-1-1001-88C Tripped at 2.03 Psig.Caused by Instrument Setpoint Drift.Pressure Switch Recalibr & Tested
Event date:
Report date:
2541981013R03 - NRC Website

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8 o0 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA3LE CONSEQUENCES h While performing QlS-6, High Drywell Pressure Calibration and Functional Test,

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g because protection was provided by the other pressure switches in the one-out-l lO is t I of-two-twice logic, which were all properly calibrated.

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