05000369/LER-1981-072-03, /03L-0:on 810427,RHR Sys Discovered Isolated from RCS During Mod of Train a Solid State Protection Sys to Include Reactor on Turbine Trip.Caused by de-energized Relay in Logic,Closing Isolation Valve

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/03L-0:on 810427,RHR Sys Discovered Isolated from RCS During Mod of Train a Solid State Protection Sys to Include Reactor on Turbine Trip.Caused by de-energized Relay in Logic,Closing Isolation Valve
ML20009F689
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 05/27/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F683 List:
References
LER-81-072-03L, LER-81-72-3L, NUDOCS 8107310410
Download: ML20009F689 (1)


LER-1981-072, /03L-0:on 810427,RHR Sys Discovered Isolated from RCS During Mod of Train a Solid State Protection Sys to Include Reactor on Turbine Trip.Caused by de-energized Relay in Logic,Closing Isolation Valve
Event date:
Report date:
3691981072R03 - NRC Website

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