05000369/LER-1981-046-01, /01T-0:on 810423,insp/leak Detection Measures Assumed for Postulated Breaks in Loop B 10-inch Accumulator Injection Line in Lieu of Structural Restraints to Prevent Unacceptable Interactions.Design Will Be Revised

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/01T-0:on 810423,insp/leak Detection Measures Assumed for Postulated Breaks in Loop B 10-inch Accumulator Injection Line in Lieu of Structural Restraints to Prevent Unacceptable Interactions.Design Will Be Revised
ML20009C231
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 05/07/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C226 List:
References
LER-81-046-01T, NUDOCS 8107200394
Download: ML20009C231 (1)


LER-1981-046, /01T-0:on 810423,insp/leak Detection Measures Assumed for Postulated Breaks in Loop B 10-inch Accumulator Injection Line in Lieu of Structural Restraints to Prevent Unacceptable Interactions.Design Will Be Revised
Event date:
Report date:
3691981046R01 - NRC Website

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EVENT CESCAIPDON ANQ PRQtuSLE CT4 SEQUENCES rasi l Inspection / leak detection measu s were assumed for postulated breaks in Loop B 10-inch Accumulator Injection line in lieu of providing structural r5Tri l restraints or barriers to prevent unacceptable interactions. This is in j

io,s,i violation at the existing Licensing agreement for pipe rupture protection.

Loss of functional integrity of certain Nuclear Sampling or S/G Blowdown o,,

g,,,, lines could eventually result in loss of containment integrity. The g, health and safety of the public have not been affected.

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cAust oEscasPnoN Ano conneenvE ACTIONS gl The inspection / leak detect on program was considered applicable to Loop B lt-inch Accumulator Injection Line contrary to the existing i

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