ML20009C203

From kanterella
Jump to navigation Jump to search
LER 81-088/03L-0:on 810521,during Calibr of Catalytic Hydrogen Recombiner,While in Mode 5 Initial Fuel Loading, Gaseous Waste Was Released to Environ.Caused When Exhaust Isolation Valve on Hydrogen Inlet Analyzer Was Left Open
ML20009C203
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 06/20/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C197 List:
References
LER-81-088-03L, LER-81-88-3L, NUDOCS 8107200372
Download: ML20009C203 (3)


Text

- . - - , ,

a

. =ac scau ssa u.s. <uct Aa accutArony ceuusssion LICENSEE EVENT REPORT EXHIBIT A CcNTRcL 8 LOCK: l l l l l l l (ptgAsg emINT CR TYPt ALL AtcuenED INFO AMAftoNs i .

8 i *r I c ! v I C !S I1 0 l Ol- I OvCamstnwmetA I O l0 1010 ! -I 01 Ol@t.yCEN64 Il l1l1l1l@l I l F 8 9 WCEMSEE C;ct 14 9 25 .1 TYPt 0 SI OA I 54 @

con'T I, o l ' 'l l'*% LtJ@l 80 n l s f 01 48 010 1 IsioGI01si21 QQCaETNuusam ES 69 11 s i i GIO IfS 612agPCRfDATS EVENT QATI 74 lO l s ! 11@ 44P sveNT caseniericN Ano , ace Asta cousscuer.as @

10 ! 21 1 'Jh41 o in Mode 5. initial fuel loading, during calibration of a catalytic l la62II hvdrneen recembiner. a valve was inadvertent 1v left open. An uncontrolled,  !

Io i A ! t gaseous waste release to the environment was made from a vaste gas tank. ,

t o i s ! ! This violated Technical Specification 4.11.2.1.2 and is reportable per  ;

lo1511 Technieni soeciffention 6.9.1.13(b). Since no radiation above background was ,

A I n,oeane ne daeominod hv Monith Physics analysis, the health and safety of l t o is i i the public were not affected.

(

svfveu cAuse Cause cou, my ,

CCDE CCDE $b5CCCS COMPQNENT OOCE SUSC309 SuSCOCE ioisl 7 s 3 ly i a l@ la_j@ l B l@ Iz 12 I z iz 12 I z r@ l z;@ LZ_J @

10 is 12 13 e 13 ;g

,, SE Cu t nit a L CCCUR.tNCt niecn1

  • EV'SiCN (VEMf vtA8 atPCAT NQ. COCK g o.

W fvet

@ ,"LimraQ

,',a,j a;

_u I s! Ila l-l

=

10 I 818 I 1.

1/1 W l,,-J LO_1

. u n n 2. n E f" " W iJ JISr $"Xan" ou., ..c0l?;2:1, L_G@lFl@ [g,,j@ L2)@ IO '0 : 0 @I Oly_J@ f T.=ls' ,it % ",;",Kf,7 a >. u a v . L n s]@ Iz l@ I Z I 919 ! 91@ ,,

cat.se cesemieTics Ano ccansenvu u ncus @

lifoi1 Tho knflaino exhnust isolation valve on the hydrogen inlet analyzer was in- ,

l' li I I ,dvarrantiv left open. The flow path was realined, the contents of the tank ,

L' u ] I were nnalyzed and the gas volume released was calculated. New procedures ,

1i i 2I I are beine implemented and a design change is being considered. ,

i i 6 41 l }

  • s s e

AT  % POaf R QT1.tM f7 Aft"f. 31 v RY 015CcvamY Ct3CAi871CM i' iI5I W @ lOIOIOl@l "

Mode 5 i L.Aj@l Personnel Observation J

' Jnvory Ccir~r *

  • a l i ! ..m.
  • I L ,_J "_ .... ,v,,v @ "

Lzl @. ln '..u A,. i I NA s CA_ . ..m A, l

..,c ',1,,@,,,s., - * =

l > I 2 I l 01010 !@t?z_j@l,,,C....,.@NA l

.. . e~~ .'s' ,, su'J, . " "

uo. . oiscaime @

li h l. I.nI n i n ..l@lu i

NA I

'rD's***"!s'Cf,*r'ie'."**@* ,,

l 8 i s 1 [.gj@l NA l

. v.ul',ry 8107200372 810618 a

,ssu n o case

  • mea @ PDR ADOCK 0500036cp Nac use cuty L.1 Lo.J 1._NJ@l NA s PDR [;iir;;,;i,,l e 8 9 10 81 49 go

~

NAME C8 PRUAAEn R. W. Ouellette ,wcN E:

l

l l

)

1 McGUllE NUCLEAR STATION INCIDENT REPORT Report Number: 81-88 Report Date: June 18, 1981 j Occurrence Date: May 21, 1981 Facility: McGuire Unit 1, Cornelius, N. C.

Identification of Occurrence: An uncontrolled, gaseous waste release to the environment was made from a Waste Gas (WG) tank via a gas analyzer and out the unit vent.

Conditions Prior to occurrence: Mode 5, cold shutdown, prior to initial criticality.

Descriptic.t of Occurrence: During the calibration of the "B" catalytic hydrogen recombiner (B-CHR), a gh! 9nalyzer valve was inadvertently left open. When the system was placed into service, a pathway existed from Shutdown Decay Tank -B (SDT-B) to the environment. This uncontrolled release constituted a degraded ~

mode of operation and was reportable pursuant to Technical Specification 4.11.

2.1.1.

Apparent Cause: Part 4.2.21 of the procedure "Radwaate Procedure for the Routine Calibration of the Waste Gas System Analyzers (Zero and Span Calibration)" was .

inadvertently omitted during calibration of the analyzer.

, As a result, the Building Exhaust Isolation Valve on the Hydrogen Inlet Analyzer (HARC-1104) was inadvertently lef t open, allowing some of the contents of SDT-B to escape, without being analyzed for radioactivity prior to release.

! Analysis of Occurrence: On the morning of May 21, it was determined, by de-creasing pressure gauge readings, that a small gas leak existed somewhere in the A-train of the Catalytic Hydrogen Recombiner System (A-CHR). It was decided, i

therefore, to remove the A-train from service in order to identify and correct the leak (s). Before the B-train could be placed into service its associated analyzer rack had to be calibrated.

At 1005 the B-analyzer rack was calibrated and placed into service. Between 1100 and 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, it was determined by decreasing pressure gauge readings that a leak also existed somewhere in the B-train 'f this system. Immediately, a team of tschnicians began searching for the leak (s).

At 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> that same day, one of the technicians discovered that the Building Exhaust Isolation Valve was open on HARC-1104. This valve was closed and the RARC-1104 Sample Vent Compressor Suction Isolation Valve was opened to realign the system in its proper mode. The technician then notified Health Physics of the events that had occurred and requested that they analyze a sample of the contents of SDT-B. This was done and the results were reported to the Shift Supervisor at 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />.

i

Report Number 81-88 Page 2 Corrective Action: Once it was suspected that a leak existed somewhere in the B-CHR system, several technicians began tracing out the system, checking for leaks by viv al inspection and by the use of " Snoop" solution (a liquid soap which emits bubbles when applied to a gas leak from a pipe, fitting, or etc.).

When a technician discovered the Building Exhcust Isolation Valve on RARC-1104 open, he realigned the flow path to stop the release. The contents of SDT-B were analyzed and the volume of gas released was calculated.

To avoid an accident of this type in the future: (1) A double verification checklist has been added to all WG analyzer racks. (2) More stringent controls have been added (red tags) to all WG analyzer rack procedures. (3) The valve handles on the CHR's have been painte'd red to make the valve position more visible. (4) An investigation is underway to study the feasability of in-stalling 3-way, six-port valves. The installation of these valves would make it impossible to discharge a WG tank via the analyzer' rack.

Safety Analysis: With the presence of only new, non-irradiated fuel on site at the time of this incident, no radiation above normal back3 round could have been present in the gas released from SDT-B. This was confirmed by the analysis performed on the contents of SDT-B on May 21, 1981.

Had radiation been present in this system, the presence of such a leak may have been detected much sooner, as the gas would be monitored by EHF's 36 and 50.

1 4

I

_ . , . . . _ _ , , _ . . . . _ _ . . . . . . , _ _ .-. - _ _ . - -- .