05000369/LER-1981-048-03, /03L-0:on 810410,while in Mode 3,wide Range Level Instrument for Steam Generator B Remote Shutdown Monitoring Instrumentation Was Pegged High & Declared Inoperable.Caused by Valved Out Transmitter

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/03L-0:on 810410,while in Mode 3,wide Range Level Instrument for Steam Generator B Remote Shutdown Monitoring Instrumentation Was Pegged High & Declared Inoperable.Caused by Valved Out Transmitter
ML20009C129
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 05/10/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C120 List:
References
LER-81-048-03L, LER-81-48-3L, NUDOCS 8107200308
Download: ML20009C129 (1)


LER-1981-048, /03L-0:on 810410,while in Mode 3,wide Range Level Instrument for Steam Generator B Remote Shutdown Monitoring Instrumentation Was Pegged High & Declared Inoperable.Caused by Valved Out Transmitter
Event date:
Report date:
3691981048R03 - NRC Website

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ITTM i Steam Generator B Remote Shutdown Monitorine Instrumentation was found peg-I lo 141 l ced hich and declared inoperable.

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