ML20009C129

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LER 81-048/03L-0:on 810410,while in Mode 3,wide Range Level Instrument for Steam Generator B Remote Shutdown Monitoring Instrumentation Was Pegged High & Declared Inoperable.Caused by Valved Out Transmitter
ML20009C129
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 05/10/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C120 List:
References
LER-81-048-03L, LER-81-48-3L, NUDOCS 8107200308
Download: ML20009C129 (1)


Text

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ITTM i Steam Generator B Remote Shutdown Monitorine Instrumentation was found peg- I lo 141 l ced hich and declared inoperable. This is in violation of Technical I to tai l Soecification 3.3.3.5 and is reportable per Technical Specification 6.9.1.13; IE I (b). Since redundant instrumentation was available the health and safety i E I of the public were not affected. I tolst i I E E =M can.sonsar caos suecooe su$cos rLo L5J. l II DIO WO Ic l@ l Il NI S lT I RI U l@ l RI@ mU @

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cAuss casemirmon Amo conneenva Ac nous ii io i l The S/G '1B' wide range level @ recorder and indicator were pegged high ,

ITTT1 l because their transmitter was valved out. The root valve of one leg was  ;

m I closed and the equalizine valve was open. The root valve was opened and l L'1.lj l the equalizing valve was closed. The transmitter was t.asted and the , ,,

titai I recorder was calibrated.

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