LER-1981-011, /03L-0:on 810608,during Routine Maint,Diesel Generator 1/2 Was Removed from Svc Prior to Demonstrating Diesel Generator 2 Operability,In Violation of Tech Spec. Caused by Personnel Error.Personnel Reinstructed |
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L.lCENSEE EVENT REPORT CONTROL BLOCK: l l
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s 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO S F GA T SS CON'T 101il E Ql0 l5 l0 10. p l 2 l 6 l 5 l@l 0 l6 l0 l8 l 8 l 1 l@l 0 l 7 l 0 l l 18 l1 l@
8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h While performing routine maintenance on the Station Diesel Generators, the 1/2 Diesel l l 012 l l Generator was removed f rom service prior to demonstrating the 2 Diesel Generator l
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operable. This is in violation of Technical Specification 3.9.E.2.
The probable g
,gg,,g consequences are minimat,because the 2 Diesei Generator was fully operable at all g
times while the 1/2 Diesel Generator was out of service.
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10181I 60 SYSTEM
CAUSE
CAUSE COMP.
VAlbE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE l0l9l d l E lh dh l A lh l E l N l G l 1 l N l E lh Wh [Z_] h 7
8 9
10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPOnT REVISION LE R EVENT YEAR REPORT NO.
CODE TYPE NO.
@,ajg/RO 18 l1l L_J 10 11 11 i L(_J 10 13 I l'l I-I
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_ 21 22 23 24 26 27 28 29 30 31 32 AK f ATC ON PL NT 1E HOURS S f IT D FOR1 B.
S PPLIE MAN F TURER
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3 3
40 41 4
43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11101l The cause of this occurrence is oersonnel error.
The monthly maintenance procedure f
i i l
has been reviewec and no changes were deemed necessary. The Operations personnel '
l have been re-inst ructed on this procedure.
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li l4 I I 7
8 9 ST S
% POWER OTHEFt STATUS 1500 RY DISCOVERY DESCRIPTION NA l
l Al@l Operational Event l
W@ l 0l 8l 6l@l i s A TIVITY CO. TENT RELEASEO OF DELEASE AMOUNT OF ACTIVITY LOCATION OF ftELEASE NA l
l NA l
b h Chl i G 83 7
8 9 to is 44 45 PEfh0NNEL EXPOSURES i
NU'NJ E F4 TYPE DESCRIP TION l
10 l 0 l 0 l@LZ_j@l NA i 7 60 7
8 9 11 12 13 PE f tOONN E t. IN JunlES NU?f Mf.It DEscinP TION l
li ln l l 0 l o l 0 J@l E3 NA 7
8 9 tt 17 L 0% OF OH DA*.tAGE TO FACILITY Q TYPE Di e. cit;* TION 0
l Z l@l NA l
1 9 Puoti$iv 8107140699 810701 N " C " 0" '.,
121 ol L"JE. OnonPrioNh PDR ADOCK 05000265 NA S
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1.
LER NUMBER:
LER/R0 81-11/03L-0 ll.
LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station 111.
FACILITY NAME: Unit Two IV.
DOCKET NUMBER: 050-265 V.
EVENT DESCRIPTION
The routine monthly preventive maintenance for the three Standby Diesel Generators was being performed at the time of the occurrence.
On June 8, 1981, the 1/2 Diesel Generator was started and demonstrated to be operable.
This permitted taking I Diesel Generator out of service.
1 Diesel Generator was taken out of service, preventive maintenance was performed, and the Diesel Generator was returned to service. The maintenance team then went to the 1/2 Diesel Generator and had it removed f rom service, it remained out of service for approximately 30 minutes for preventive maintenance. At that time, the limiting condition for operation in Technical Specification 3 9.E.2 was exceeded. The 1/2 Diesel Generator was taken out of service without demonstrating that the 2 Diesel Generator was operable.
The 1/2 Diesel Generator was returned to service, started, and demonstrated to be operable. _Then the 2 Diesel Generator was removed f rom service, preventive maintenance performed, and returned to service, started, and demonstrated to be operable.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
The 2 Diesel Generator had previously been started and loaded on May 26, 1981. There were no operational problems found while the 2 Diesel l
Generator was out of service for preventive maintenance.
Immediately after j
the routine maintenance of 2 Diesel Generator, it was started and
^
demonstrated to be operable.
The 2 Diesel Generator would have started if needed while Diesel Generator 1/2 was out of service. At no time during the maintenance of the Diesel Generators was there more than one Diesel l
Generator out of service. The consequences of this deviation are minimal, and safe operation of the plant was not affected.
Vll. CAUSE:
t l
The cause of this-occurrence is personnel error. The Shi f t Engineer made l
an outage report, QOS 6600-04, for the i Diesel Generator at the time of removing the 1/2 Diesel Generator from service, but failed to also specify the 2 Diesel Generator.
l l
Vill. CORRECTIVE ACTION:
This is the first occurrence of failure to demonstrate operability of a Diesel Generator during monthly maintenance. The Unit Two Operating j-Engineer has instructed Operating personnel in the Diesel Generator monthly maintenanc2 p rocedu re.
The Unit One Operating Engineer has reviewed the l
procedure for removing Diesel Generators f rom service wi th the Shi f t Engineer.
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| 05000265/LER-1981-001-03, /03L-0:on 810116,during High Drywell Pressure Calibr & Functional Test,Pressure Switch PS-1-1001-88D Trip Point Found Above Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibr & Tested | /03L-0:on 810116,during High Drywell Pressure Calibr & Functional Test,Pressure Switch PS-1-1001-88D Trip Point Found Above Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibr & Tested | | | 05000254/LER-1981-001-03, /03L-0:on 810105,while Placing Standby Gas Treatment Sys B in Normal Shutdown Lineup,Discharge Valve MO-1/2-7507B Failed to Close When Operated from Control Room.Caused by Worn Breaker Auxiliary Contacts | /03L-0:on 810105,while Placing Standby Gas Treatment Sys B in Normal Shutdown Lineup,Discharge Valve MO-1/2-7507B Failed to Close When Operated from Control Room.Caused by Worn Breaker Auxiliary Contacts | | | 05000254/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000265/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards 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05000265/LER-1981-004-01, /01T-0:on 810220,four Low Condenser Vacuum Switches Tripped in Excess of Tech Specs During Test.Caused by Setpoint Drift.Switches Recalibr | /01T-0:on 810220,four Low Condenser Vacuum Switches Tripped in Excess of Tech Specs During Test.Caused by Setpoint Drift.Switches Recalibr | | | 05000265/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000254/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000254/LER-1981-004-03, /03L-0:on 810116,while Performing Qis 10 Monthly Functional & Quarterly Calibr Test,Reactor Low Level Switch LS-1-263-57A Tripped Above Tech Spec Requirement.Caused by Instrument Setpoint Drift.Switch Recalibr | /03L-0:on 810116,while Performing Qis 10 Monthly Functional & Quarterly Calibr Test,Reactor Low Level Switch LS-1-263-57A Tripped Above Tech Spec Requirement.Caused by Instrument Setpoint Drift.Switch Recalibr | | | 05000265/LER-1981-005-03, /03L-0:on 810224,switch in DPIS-2-1360-1B Failed to Operate While Performing Surveillance Testing.Caused by Failure of High Side Switch in DPIS-2-1360-1B.Switch Adjusted,Recalibr & Satisfactorily Tested | /03L-0:on 810224,switch in DPIS-2-1360-1B Failed to Operate While Performing Surveillance Testing.Caused by Failure of High Side Switch in DPIS-2-1360-1B.Switch Adjusted,Recalibr & Satisfactorily Tested | | | 05000265/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000254/LER-1981-005-01, /01T-0:on 810220,during Testing,Three of Four Condenser Low Vacuum Scram Switches Found Outside Setting Per Tech Spec 3.1-3.Caused by Instrument Setpoint Drift.All Switches Recalibr | /01T-0:on 810220,during Testing,Three of Four Condenser Low Vacuum Scram Switches Found Outside Setting Per Tech Spec 3.1-3.Caused by Instrument Setpoint Drift.All Switches Recalibr | | | 05000254/LER-1981-005, Forwards LER 81-005/01T-0 | Forwards LER 81-005/01T-0 | | | 05000265/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 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| | 05000265/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000265/LER-1981-007-03, /03L-0:on 810322,MSIV AO-2-203-2A Failed to Initiate half-scram in Reactor Protection Sys Channel B. 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Caused by Personnel Error.Personnel Reinstructed | /03L-0:on 810608,during Routine Maint,Diesel Generator 1/2 Was Removed from Svc Prior to Demonstrating Diesel Generator 2 Operability,In Violation of Tech Spec. 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Caused by Instrument Drift.Switch Recalibr & Tested | /03L-0:on 810624,pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Level During Loss of Electrohydraulic Fluid Pressure Calibr & Functional Test. Caused by Instrument Drift.Switch Recalibr & Tested | | | 05000254/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000265/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000254/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000265/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
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