05000267/LER-1981-019-03, /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced

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/03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced
ML20008F634
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 03/19/1981
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20008F631 List:
References
LER-81-019-03L, LER-81-19-3L, NUDOCS 8104210413
Download: ML20008F634 (1)


LER-1981-019, /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced
Event date:
Report date:
2671981019R03 - NRC Website

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as> af : Art 43 EVENT OESCRIPT;cN AND PeCS ASL" 00'.SECUENCES h I 4 : 1 1 Cn Februa i 20 and Feb ruct i 23, 1981. the oltnt vss enerated at oewer with e arrenev I I

g gi j feedwater to Loep 1 circulator water turbine drives isolated to repair PV-21243-1.

l o ! 41 [ De;;raded toda of LCO 4.2.2.a).

Reportable per Fort St. Vrain Technical Soecification 1 1, i s ! t AC 7.5.2(b)2.

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13 M i ! operable. No accocpanving_o_ccurrence.

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