LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Encl |
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puhtic servlee compimy of Cenomde ve i 16805 Road 19.1/2, Platteville, Colorado 80651-9298 February 5, 1982 Fort St. Vrain Unit No. 1.
P-82032
% R@ R MIR
- FEB 81982 Mr. John T. Collins, Regional Administrator j
Region IV Nuclear Regulatory Commission n
(;7[c ~Qf3 611 Ryan Plaza Drive i
Suite 1000 i
Arlington, Texas 76011
.a. a y g9 Reference: Facility Operating Li e se r/gg I982a I No. DPR-34 nm
- - Lacua[#lft s
Docket No. 50-267 9,
Dec 7
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t
Dear Mr. Collins:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/82-001, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)2.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/82-01.
Very truly yours, W
Don Warembourg Manager, Nuclear Production DW/cis Enclosure cc: Director, MIPC h
82021'60639'820205
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PDR ADOCK 05000267
/ l 0
PDR
REPORT DATE:
February 5,1982 REPORTABLE OCCURRENCE 82-001 ISSUE 0 OCCURRENCE DATE:
January 8, 1982 Page 1 of 6 FORT ST. VRAIN NUCLEAR GENERATING STATION
- - PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298' REPORT NO. 50-267/82-001/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
During Surveillance Testing by plant personnel, while the reactor was in a shutdown / cooled down condition, a total of eighteen Class I hydraulic shock suppressors (snubbers) were found to be inoperable.
Since the reactor had been operated since these snubbers were last successfully tested, the snubbers must be considered to have been inoperable when the reactor was at power.
This is a degraded mode of LC0~4.3.10 and is reportable per Fort'St.
Vrain Technical Specification AC 7.5.2(b)2.
EVENT
DESCRIPTION
With the plant shutdown for a system modification outage, plant personnel conducted a routine Surveillance Test of all-hydraulic shock suppressors (snubbers) to verify their operability. A total of eighteen Class I snubbers were found to be inoperable for various reasons.
The tabulation which follows lists the snubbers by number and their associated event description.
EVENT NUMBER SNUBBER IDENTIFICATION
EVENT DESCRIPTION
1 HRS-281 No visual oil level.
2 HRS-357 No visual oil level.
3 HOS-74 Piston fully extended.
l l
4 H05-88 No visual oil level.
5 HOS-87 Piston fully inserted.
6 MSS-257 Piston fully extended.
t 7
HRS-413 Piston fully inserted.
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REPORTABLE OCCURRENCE'82-001 ISSUE O Page 2 of 6
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EVENT NUMBER ~ SNUBBER IDENTIFICATION
EVENT DESCRIPTION
8 CRS-297 Found disconnected and removed from system.
9
.VSS-116 Piston' fully' extended, no visual oil level 10 HRS-205 Rod shaft unscrewing from rod eye.
11 BFS-399E No visual oil level.
12 BFS-158E No visual oil level.
13 HRS-158 Piston fully extended, no visual oil level.
14 BFS-299E No visual oil level.
15 MSS-149 No visual oil level.
16 CRS-751' uNo visual-oil level.
17 BFS-228E No visual oil level.
18 BFS-534 No visual oil level.
CAUSE
DESCRIPTION:
The following is a listing of cause descriptions associated with each event number.
EVENT NUMBER SNUBBER IDENTIFICATION CAUSE DESCRIPTION 1
HRS-281 Seal / internal leakage caused a loss of reservoir oil.
2 HRS-357 Seal / internal leakage caused a loss of reservoir oil.
3 HOS-74 Thermal pipe contra tion caused snubber to be. fully extended.
4 H05-88 Seal / internal leakage aused a loss of reservoir oil.
5 HOS-87 Thermal pipe contraction caused snubber to be fully inserted.
REPORTABLE OCCURRENCE 82-001 ISSUE 0 Page 3 of 6 EVENT.-
NUMBER SNUBBER IDENTIFICATION-CAUSE DESCRIPTION 6
MSS-257 Thermal pipe contraction caused snubber to be fully inserted.
7 HRS-413 Thermal-pipe contraction caused isnubber to be fully inserted.
8 CRS-297 Exact cause is unknown. May have been disconnected due to mainte-nance in immediate area.
9 VSS-116 Thermal pipe contraction caused snubber to be fully extended, using all available oil in reser-voir.
10 HRS-205 Vibration caused the shaft to ro-tate loose from the rod eye end.
11 BFS-399E Seal / internal leakage caused a loss of reservoir oil.
12 BFS-158E Seal / internal leakage caused a loss of reservoir oil.
13 HRS-158 Thermal pipe contraction and seal leakage caused the snubber to be fully extended, using all remaining oil in reservoir.
14 BFS-229E
- - Seal / internal leakage caused a loss of reservoir oil.
15 MSS-149 Seal / internal-leakage caused a loss of reservoir oil.
16 CRS-751 Seal / internal leakage caused a loss of reservoir oil.
17 BFS-228E Seal / internal leakage caused a loss of reservoir oil.
18 BFS-534 Seal / internal leakege caused a loss l
of reservoir oil, i
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REPORTABLE OGCURRENCE 82-001 ISSUE O Page 4 of 6 CORRECTIVE ACTION:
The following is a listing of corrective actions taken associated with each event number.
EVENT NUMBER SNUBBER IDENTIFICATION
CORRECTIVE ACTION
1 HRS-281 Cylinder and valve block rebuilt, filled, purged, and tested.
Reser-voir repositioned to ensure maximum oil availability.
Re-installed in system.
2 HRS-357 Filled, purged, and tested.
Re-inst &? led in system.
3 H05-74 Cylinder and valve block rebuilt, filled, purged, and tested.
Re-installed in system.
4 HOS-88 Cylinder and valve block rebuilt, filled, purged, and tested.
Re-installed in system.
5 HOS-87 Filled, purged, and tested.
New bracket made to prevent piston from bottoming out. 'Re-installed in system.
6 MSS-257 Filled, purged, and tested. Ad-justed extension tube. Re-installed in system.
7 HRS-413 Filled, purged, and tested.
'Re-installed in system.
8 CRS-297 Filled, purged, and tested.
Re-installed in system.
9 VSS-116 Adjusted reach rod, filled, purged, and tested.
Re-installed in system.
10 HRS-205 Screwed rod eye tight onto piston rod, filled, purged, and tested.
Re-installed in system.
11 BFS-399E Rebuilt cylinder and valve assembly.
Filled, purged, and tested.
Re-installed in system.
I REPORTABLE OCCURRENCE 82-001 ISSUE O Page 5 of 6 EVENT NUMBER SNUBBER IDENTIFICATION
CORRECTIVE ACTION
12 BFS-158E
- - Rebuilt cylinder and valve block.
Filled, purged, and tested.
Re-installed in system.
13 HRS-158 Rebuilt cylinder and valve block.
Filled, purged, and tested.
Re-installed in system.
Added shim to-end.
14 BFS-299E Rebuilt cylinder and valve block.
Filled, purged, and tested.
Re-installed in system.
15 MSS-149 Rebuilt cylinder.and valve block.
Filled, purged, and tested.
Re-stalled in system.
16 CRS-751 Rebuilt cylinder and valve block.
j Filled, purged,.and tested.
Re-t installed in system.
17 BFS-228E Filled, purged, and tested.
Re-installed in system.
18.
BFS-534 Rebuilt cylinder and orifice block.
Filled, purged, and tested.
Re-installed in system.
In accordance with Surveillance Requirement 5.3.8, the surveillance interval has been adjusted to 31 days + 25%.
No further corrective action is anticipated or required.
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REPORTABLE OCCURRENCE 82-001' ISSUE 0.
.Page 6 of 6-t r
C Prepared By: (!)'toevti ' hh d2 Owen J. C.1tyton-
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Technical ervices Technician.
C/d M /r % u Reviewed By:
Charles Fuller Technical-Services Engineering Supervisor
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s Reviewed By:
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Edw1/(O'. Hill * '
Station Manager Approved By:
Ma,u4 Don Warembourg Manager, Nuclear Production e.
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| 05000267/LER-1982-001-03, /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | | | 05000267/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002-03, /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-003-03, /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | | | 05000267/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-004, Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-004-01, /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | | | 05000267/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005-03, /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | | | 05000267/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-006-03, /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | | | 05000267/LER-1982-007, Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-007-01, /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | | | 05000267/LER-1982-008-03, /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | | | 05000267/LER-1982-009-03, /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | | | 05000267/LER-1982-010-03, /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | | | 05000267/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-011-03, /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | | | 05000267/LER-1982-012-03, /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | | | 05000267/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013-03, /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | | | 05000267/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-014-03, /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | | | 05000267/LER-1982-015-03, /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | | | 05000267/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-016-03, /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | | | 05000267/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-017-03, /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to S | /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to Svc | | | 05000267/LER-1982-018-03, /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | | | 05000267/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-019-03, /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-020-03, /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | | | 05000267/LER-1982-020, Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-021-03, /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | | | 05000267/LER-1982-022-03, /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | | | 05000267/LER-1982-023-03, /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | | | 05000267/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-024, Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | | | 05000267/LER-1982-024-03, /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | | | 05000267/LER-1982-025, Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | | | 05000267/LER-1982-026, Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-026-03, /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | | | 05000267/LER-1982-027, Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-027-03, /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | | | 05000267/LER-1982-028, Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028-03, /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | | | 05000267/LER-1982-029-03, /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | |
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