LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl |
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l puhuc Service Company cf OcHersde 16805 ROAD 19%
. _ L.i PLATTEVILLE, COLOR ADO 80651 March 6, 1981 Fort St. Vrain Unit No. 1 P,81087 Mr. Karl V. Seyfrit, Director Nuclear Regulatory Commission Region IV Office of Inspection and Enforcecent 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 Reference: Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Seyfrit:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/
81-015, Final, submitted per the requirenents of Technical Specification AC 7.5.2(b)2.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/81-015.
Very truly yours, h
f7n Don Warembourg Manager, Nuclear Production
- - DW/cis Enclosure cc: Director, MIPC F "'onea4
REPORT DATE:
'" arch 6, 1981 REPORTA3LE CCCURRENCE 81-015 ISSUE O OCCURRENCE DATE:
Februarv 4, 1981 Page 1 of 8 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE CO:f AW OF COLOPADO 16805 WELD COUNTl ROAD 19 1/2 PLATIEVILLE, COLCRADO 80651 REPORT NC. 50-267/81-015/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
During the period from February 4,1981, to February 20, 1981, the plant was operated in a degraded mode of LCO 4.2.10 on nine occasions.
These e' rents are reportable per Fort St. Vrain Technical Specification AC 7.5.2(b) 2.
EVENT
DESCRIPTION
Event 1 (See Figure 1) At about 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on February 4, 1981, while the average core outlet temperature was above 1200*F, the primary coolant total oxidants increased above 10 PPMV, The oxidants remained above 10 ??MV until about 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> on February 4,1981. This event cons titutes operation in a de-graded mode of LC0 4.2.10.
Event 2 (See Figure 1) At about 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on February 4,1981, while the aversge core outlet te=perature was above 1200*F, the total primarf coolant oxidants increased above 10 PPMV. The oxidants remained above 10 ??MV until about 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br /> on February 5,1981. This event constitutes operation in a de-graded mode of LCO 4.2.10.
Event 3 (See Figure 1) At about 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> on February 6,1981, while the average core outlet te=perature was above 1200*F, the total primary coolant oxidants increased above 10 ??MV. The oxidant _: remained above 10 PPMV until about 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on February 8,1981. This event constitutes operation in a de-graded mode of LCO 4.2.10.
REPORTABLE OCCt:RRENCE 31-015 ISSUE O Page 2 of 8 EVENT
DESCRIPTION
(Cont' d)
Event 4 (See Figure 2) At about 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> on February 10, 1981, while the average core outlet temperature was above 1200*F, the pri=ary coolant total oxidants increased above 10 PPMV. The oxidants remained above 10 PPMV until about 1400 hcurs on February 14, 1981. This event constitutes operation in a de-graded mode of LCO 4.2.10.
Event 5 (See Figure 2) At about 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on February 15, 1981, while the average core outlet temperature was above 1200*F, the pri=ary coolant total oxidants increased above 10 PPMV. The oxidants remained above 10 PPMV until about 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on February 15, 1981. This event constitutes operation in a de-graded mode of LCO 4.2.10.
Events 6 and 7 a
(See Figure 2) On February 15, 1981, at about 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> and again at about 1930 hours0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br />, the primary coolant oxidants increased above 10 PPMV for about one hour each time. The average core outlet temperature was above 1200*F on both occasions. These events constitute operation in a degraded = ode of LCO 4.2.10.
Event 8 (See Figures 2 and 3) At about 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on February 16, 1981, while the average core outlet temperature was above 1200*F, the primary coolant total oxidants increased above 10 PPMV. The oxidants remained above 10 PPXV until about 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on February 18, 1981. This event constitutes operation in a degraded mode of LCO 4.2.10.
- - Event 9 (See Figure 3) At about 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on February 21, 1981, while average core
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outlet temperature was above 1200'F, the primary coolant total oxidants in-creased above 10 PPMV. The oxidants remained above 10 PPMV, except for short periods of time, until 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on February 23, 1981. This eveet constf-cutes operation in a degraded mode of LCO 4.2.10.
REPORTABLE OCCL*RRENCE 81-016 ISSUE O Page 3 of 8
CAUSE
DESCRIPTION:
Event 1
. The reactor power was increased from 60% to 65% at about 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br /> on Febru-a ry 3, 1981. At this time, the average core outlet temperature increased from about 1235'? to about 1310*F, resulcing in oxidant out-gassing from the core graphite which peaked at about 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on February 4,1981.
Event 2 No specific cause can be associated with this event.
Event 3 During the period prior to and during this event, moisture was intentionally introduced into the primary coolant during scheduled tests of the dewpoint moisture monitor response times.
Event 4 At 0828 hours0.00958 days <br />0.23 hours <br />0.00137 weeks <br />3.15054e-4 months <br /> on February 10, 1981, during scheduled testing of the plant protective system, a spurious trip of both helium circulators in Loop 1 oc-curred. Either the circulator trip or the recovery process resulted in a moisture ingress which caused the very rapid increase in primary coolant oxidants.
Event 5 No ' specific cause can be associated with this event.
Event-6 No specific cause can be associac2d with-this event.
. Event 7
- - No specific' cause can be associated with this avent.
. Even t 8 No' specific cause can be associated with this event.
Event 9-During the period prior to and ddting this event, moisture was intentionally introduced into the primaly.ccolant during scheduled tests 'of the dewpoint moisture monitor response time.
REPORTABLE OCCL"A.RENCE 81-015 ISSUE O Page 4 of S CORRECTIVE ACTION:
The corrective action for all events of operation in a degraded mode of LCO 4.2.10 during the period was to allow the pri=ary coolant purification system to remove the primary coolant oxidants and thereby, bring them below the 10 PPMV limit of the LCO. During event #4, the reactor power level was redaced to lower average core outlet ce=perature and increase the water /
graphite reaction race.
No further corrective action is anticipated or requir?.d for the nine events contained in this report, s
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REPORTABLE OCCL*RRENCE S1-015 ISStlE O Page 8 of 8 Prepared By:
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AL Richard R. Fros:
Technical Services Supervisor Reviewed By:
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.echnical Services Supervisor Reviewed By:
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Frank M. Mathie Operations Manager Approved By:
h MM Don '4arembourg Manager, Nuclear Production f.~m.,_
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| 05000267/LER-1981-001, Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | | | 05000267/LER-1981-001-03, /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | | | 05000267/LER-1981-002-03, /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | | | 05000267/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000267/LER-1981-003-03, /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | | | 05000267/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000267/LER-1981-004-03, /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | | | 05000267/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000267/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000267/LER-1981-005-03, /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | | | 05000267/LER-1981-006-03, During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000267/LER-1981-007, Forwards LER 81-007/03T-0 | Forwards LER 81-007/03T-0 | | | 05000267/LER-1981-007-03, /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | | | 05000267/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000267/LER-1981-008-03, /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | | | 05000267/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-009-03, /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | | | 05000267/LER-1981-010-03, /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | | | 05000267/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000267/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000267/LER-1981-011-03, /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | | | 05000267/LER-1981-012-03, /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | | | 05000267/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000267/LER-1981-013-01, /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | | | 05000267/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Summary Also Encl | Forwards LER 81-014/03L-0.Detailed Summary Also Encl | | | 05000267/LER-1981-014-03, /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | | | 05000267/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-015-03, /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | | | 05000267/LER-1981-016-03, During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000267/LER-1981-017-03, /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | | | 05000267/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000267/LER-1981-018-03, /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | | | 05000267/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019-03, /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | | | 05000267/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-020-03, /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | | | 05000267/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-021-03, /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | | | 05000267/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-022-03, /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | | | 05000267/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-023-03, /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | | | 05000267/LER-1981-024-03, During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | | | 05000267/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025, Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025-03, /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | |
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