LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl |
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) public service company of conomde 16805 ROAD 19%
PLATTEVILLE, COLORADO 80651 March 12, 1981 Fort S t.
Vrain Unit No. 1
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Nuclear Regul.atory Commission
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rn' '-/p Office of Inspection and Enforcement 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 Reference: Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Seyfrit:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/
81-018, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)2.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/81-018.
Very truly yours, f
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- Don Warembourg Manager, Nuclear Production DW/cls Enclosure 003 cc: Director, MIPc s
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REPORT DATE:
March 12. 1981 REPORTABLE OCCURRENCE 81-018 ISSUE O OCCURRENCE DATE:
Feb ruary 14, 1981 Page 1 of 4 FORT ST. VRAIN NUCLEAR f'ENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 191/2 PLATTEVILLE, COLORADO 80651 REPORT NO. 50-267/81-018/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
During performance of a scheduled Surveillance Test, the sample flow alam setpoints of three dewpoint moisture monitors were found outside the limits specified by LCO 4.4.1, Table 4.4-1, note (t). This event constitutes oper-ation in a degraded mode of LCO 4.4.1 and is reportable per Fort St. Vrain Technical Spa:ification AC 7.5.2(b)2.
EVENT
DESCRIPTION
While operating at 69% thermal power and 220 !N(e), plant instrument per-sonnel performed the primary c.oolant moisture instrumentation sample flow alarm functional test, SR 5.4.1.1.6e-M.
The test verifies that each of the eight dewpoint moisture monitors will alarm on low and high sample flow.
The limiting condition for operation LCO 4.4.1, Table 4.4-1, note (t) speci-l fies that a dewpoint moisture monitor shall not be considered operable unless the sa=ple flow is alarmed as follows:
l a) A fixed low sample flow alarm set at 1 sec/sec.
b) A fixed high sample flow alarm set at 75 sec/sec.
c) A variable icw sample flow alarm set at 1 to 50 sec/sec as a function of reactor power level.
During performance of the Surveillance Test, two fixed low sample flow alarm setpoints were found below the 1 sec/sec limit, two fixed high sample flow alarm setpoints were found above the 75 sec/see limit, and one variable low sample flow alarm setpoint was found below the 50 sec/sec limit required by the reactor power level at the time the surveillance was performed. Three dewpoint moisture monitors were involved - one high level monitor and one loop monitor in each loop. The actual setpoints found are shown for these three moisture montiors in Table 1.
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REPORTABLE OCCURRENCE 81-018 ISSUE O Page 2 of 4 T.GLE 1 Fixed Low Variable Low Fixed High Moisture Monitor 1 sec/see Alarm 50 sec/sec Alarm 75.sec/see Alarm Monitor Loop Found At Found At Found At h 1117 Loop 1 0.25 sec/sec*
51.7 77.56*
h il19 High 1.36 sec/sec 46.04*
81.86*
Level h 1122 Loop 2 0.25 sec/see*
51.2 73.0
- These values were outside the acceptance criteria.
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PIPORTABLE OCCURRENCE 81-018 ISSUE O Page 3 of 4
CAUSE
DESCRIPTION:
The cause of this event was misadjustment of the alarm setpoints se some time in the past.
It has not been possible to determine the time the mis-adjustmsut occurred or what person was responsible.
CORRECTIVE ACTION:
The alarm setpoints were re-adjusted to the correct value and the Surveil-lance Test completed satisfactorily.
All Results personnel have been informed by memo that unauthori::ed ad-justments are not permitted, and that adjustments may caly be saade within the limits of LCO 4.4.1.
No further corrective action is anticipated or required.
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REPORTABLE OCCURRENCE 81-018 ISSUE O Page 4 of 4 Prepared By:
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AF Richard R. Frost Technical Services Technician Revieved By:
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$/t) /l'),T//, ;.b jh)?yV Frank M. Mathie
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Operaticas Manager l
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Don Ware = bourg g
Manager, Nuclear Production i
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| 05000267/LER-1981-001, Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | | | 05000267/LER-1981-001-03, /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | | | 05000267/LER-1981-002-03, /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | | | 05000267/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000267/LER-1981-003-03, /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | | | 05000267/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000267/LER-1981-004-03, /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | | | 05000267/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000267/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000267/LER-1981-005-03, /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | | | 05000267/LER-1981-006-03, During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000267/LER-1981-007, Forwards LER 81-007/03T-0 | Forwards LER 81-007/03T-0 | | | 05000267/LER-1981-007-03, /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | | | 05000267/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000267/LER-1981-008-03, /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | | | 05000267/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-009-03, /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | | | 05000267/LER-1981-010-03, /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | | | 05000267/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000267/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000267/LER-1981-011-03, /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | | | 05000267/LER-1981-012-03, /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | | | 05000267/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000267/LER-1981-013-01, /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | | | 05000267/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Summary Also Encl | Forwards LER 81-014/03L-0.Detailed Summary Also Encl | | | 05000267/LER-1981-014-03, /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | | | 05000267/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-015-03, /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | | | 05000267/LER-1981-016-03, During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000267/LER-1981-017-03, /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | | | 05000267/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000267/LER-1981-018-03, /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | | | 05000267/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019-03, /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | | | 05000267/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-020-03, /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | | | 05000267/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-021-03, /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | | | 05000267/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-022-03, /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | | | 05000267/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-023-03, /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | | | 05000267/LER-1981-024-03, During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | | | 05000267/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025, Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025-03, /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | |
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