LER-1981-005, /03L-0:on 810202,power Supply to Both Excore Range Monitors Was Interrupted.Caused by Maint Personnel Cutting Off Power to Investigate Steam Generator Status Lights & lo-lo Level Alarms.Personnel Instructed |
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MCGUIRE NUCLEAR STATION ISCIDENT REPORT Report Number:
369/81-05 Report Date: February 11, 1981 Occurrence Date: February 2, 1981 Facility: McGuire Unit 1, Cornelius, North Carolina Identification of Occurrence: Both source range monitors (Excore Instrumentation) were inoperable for 30 seconds.
Conditions Prior to Occurrence:
Initial Fuel Loading, Mode 6 Description of Occurrence:
On February 2, 1981 at 0802 hours0.00928 days <br />0.223 hours <br />0.00133 weeks <br />3.05161e-4 months <br />, the source range monitors' power supplies were interrupted causing the indicating lights associated with the monitors to go of f for approximately 30 seconds and then come back on.
This happened while I&E personnel were perforning maintenance work on steam generators 10-10 level alarms. The 30 second power interruption of these monitors caused a degraded mode of operation and was therefore reportable pursuant to Technical Specification 3.9.2.
Anparent Cause of Occurrence:
ISE personnel were investigating why the status lights on the steam generator A, B, and C lo-lo level alarms were actuated. As a troubleshooting technique, they attempted to completely isolate all input sigrsls that might have actuated the status lights in the Control Room.
Since these signals could be coming from either Train A or B, both ' INPUT ERROR IFHIBIT' switches on the Solid State Protective System (SSPS) panel were inadvertently placed in the ' INHIBIT' position causing power interruption to the source range monitors.
Analysis of Occurrence:
The 30 second power interruption on the source range monitors occurred while there was maintenance work going on at the fuel transfer tube; the air pump that runs the conveyor was being replaced. Since there was no fuel movement at the time the incident occurred, there was no significant effect as to the safety and health of the public.
Corrective Action
Power to the source range monitors were restored after 30 seconds of interrup-tion when I&E personnel placed the ' INPUT ERROR INHIBIT' switch back in the
' NORMAL' position.
I&E personnel were instructed not to perform maintenance work on testing on both trains of the SSPS cabinets at the same time even in Mode 6.
IP/0/A/3010/05, SSPS Safeguard Test, prohibits testing of both trains at the same t ime.
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| 05000369/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000369/LER-1981-001-03, /03L-0:on 810129-0212,several Fire Detection Instruments Were Inoperable for Periods Exceeding 1-h. Caused by Const in Area.Fire Watches & Patrols Established | /03L-0:on 810129-0212,several Fire Detection Instruments Were Inoperable for Periods Exceeding 1-h. 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Valves Repaired & Train a Returned to Svc | /03L-0:on 810203,control Area Ventilation Sys Train a Declared Inoperable.Caused by Draining Essential Header to Repair Leaking Valves in Nuclear Svc Water Sys. Valves Repaired & Train a Returned to Svc | | | 05000369/LER-1981-009-03, /03L-0:on 810205,flow to Reactor Coolant Loops Was Momentarily Lost.Caused by Failure of Throttle Valve to Close Due to Loosening of Nut Holding Linkage to Valve Stem. Linkage Repositioned & Nut Tightened | /03L-0:on 810205,flow to Reactor Coolant Loops Was Momentarily Lost.Caused by Failure of Throttle Valve to Close Due to Loosening of Nut Holding Linkage to Valve Stem. Linkage Repositioned & Nut Tightened | | | 05000369/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000369/LER-1981-010-03, /03L-0:on 810207,total RHR Flow Exceeded Tech Specs.Caused by Air Line Supplying Actuator on RHR Valve Breaking,Allowing Valve to Fail Open.Rhr Flow Reset.Rigid Air Supply Lines to Be Replaced W/Flexible Lines | /03L-0:on 810207,total RHR Flow Exceeded Tech Specs.Caused by Air Line Supplying Actuator on RHR Valve Breaking,Allowing Valve to Fail Open.Rhr Flow Reset.Rigid Air Supply Lines to Be Replaced W/Flexible Lines | | | 05000369/LER-1981-011-03, /03T-0:on 810210,both Pressure Seals on Inner Door of Lower Personnel Air Lock Failed.Caused by Hole in One Seal & Bubble in Other Seal.Seals Replaced & Returned to Manufacturer | /03T-0:on 810210,both Pressure Seals on Inner Door of Lower Personnel Air Lock Failed.Caused by Hole in One Seal & Bubble in Other Seal.Seals Replaced & Returned to Manufacturer | | | 05000369/LER-1981-011, Forwards LER 81-011/03T-0 | Forwards LER 81-011/03T-0 | | | 05000369/LER-1981-012-03, /03T-0:on 801211,isolation Valve NV-250 Found Not Verified Closed Under Administrative Control Per Tech Spec. 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Repairs Performed & EMFs Declared Operable | | | 05000369/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000369/LER-1981-014-03, /03L-0:on 810212,while in Mode 6,control Room Received High Groundwater Alarm.Caused by Localized Temporary High Groundwater Level.Proper Surveillance Conducted & Alarm Was Cleared within 2 Days | /03L-0:on 810212,while in Mode 6,control Room Received High Groundwater Alarm.Caused by Localized Temporary High Groundwater Level.Proper Surveillance Conducted & Alarm Was Cleared within 2 Days | | | 05000369/LER-1981-015-03, /03L-0:on 810213,various Firestops & Fire Doors Rendered Inoperable for Periods Exceeding 1-h from 810213-27.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrols Established as Required | /03L-0:on 810213,various Firestops & Fire Doors Rendered Inoperable for Periods Exceeding 1-h from 810213-27.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrols Established as Required | | | 05000369/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000369/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000369/LER-1981-016-03, /03L-0:on 810216,several Firestops Inadvertently Left Open W/O Fire Watches Being Posted.Caused by Omission of Stops from Maint List of Those Requiring Seals.Stops Sealed.Seals Will Be Verified Every 18 Months | /03L-0:on 810216,several Firestops Inadvertently Left Open W/O Fire Watches Being Posted.Caused by Omission of Stops from Maint List of Those Requiring Seals.Stops Sealed.Seals Will Be Verified Every 18 Months | | | 05000369/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-018-03, /03L-0:on 810219,annunciator Alarm Indicated Loss of Sample Flow on Radiation Monitor 1-EMF-33.Monitor Vacuum Pump Internally Damaged Due to Water Inside Pump.Pump Vanes & Bearings Replaced & Water Removed | /03L-0:on 810219,annunciator Alarm Indicated Loss of Sample Flow on Radiation Monitor 1-EMF-33.Monitor Vacuum Pump Internally Damaged Due to Water Inside Pump.Pump Vanes & Bearings Replaced & Water Removed | | | 05000369/LER-1981-019-01, /01T-0:on 810306,during ESF Testing,Loss of Ac Power Was Experienced on Half of Station Security Sys.Caused by Blown Security Sys Power Inverter Fuse.Security Procedures Changed to Indicate Info Concerning Power Sys | /01T-0:on 810306,during ESF Testing,Loss of Ac Power Was Experienced on Half of Station Security Sys.Caused by Blown Security Sys Power Inverter Fuse.Security Procedures Changed to Indicate Info Concerning Power Sys | | | 05000369/LER-1981-019, Forwards LER 81-019/01T-0 | Forwards LER 81-019/01T-0 | | | 05000369/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-020-03, /03L-0:on 810219,spurious High Radiation Alarm & Loss of Flow Alarm Sounded in Control Room on EMF-49. Personnel Cleared Radiation Alarm But Overlooked Closed Valve,Causing Loss of Flow Alarm.Monitor Repaired | /03L-0:on 810219,spurious High Radiation Alarm & Loss of Flow Alarm Sounded in Control Room on EMF-49. Personnel Cleared Radiation Alarm But Overlooked Closed Valve,Causing Loss of Flow Alarm.Monitor Repaired | | | 05000369/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-021-03, /03L-0:on 810226,noble Gas Activity Monitor for Condenser Evacuation Sys EMF-33 Not Functioning.Caused by Excessive Amounts of Condensation in Sample Lines.Moisture Removed.Different Type of Moisture Separator to Be Used | /03L-0:on 810226,noble Gas Activity Monitor for Condenser Evacuation Sys EMF-33 Not Functioning.Caused by Excessive Amounts of Condensation in Sample Lines.Moisture Removed.Different Type of Moisture Separator to Be Used | | | 05000369/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000369/LER-1981-022-03, /03L-0:on 810301-16,various Portions of Fire Detection Sys Inoperable for Periods Exceeding 1-h.Caused by Const in Area.Fire Watches & Patrols Established as Required | /03L-0:on 810301-16,various Portions of Fire Detection Sys Inoperable for Periods Exceeding 1-h.Caused by Const in Area.Fire Watches & Patrols Established as Required | | | 05000369/LER-1981-023-03, /03L-0:on 810227-0313,various Firestops & Fire Doors Inoperable for Periods Exceeding 1-h.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrol Established as Required | /03L-0:on 810227-0313,various Firestops & Fire Doors Inoperable for Periods Exceeding 1-h.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrol Established as Required | | | 05000369/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000369/LER-1981-024, Forwards LER 81-024/01T-0 | Forwards LER 81-024/01T-0 | | | 05000369/LER-1981-024-01, /01T-0:on 810316,Unit 1 Wedge Plates Discovered to Be Smaller than Required Size.Cause Not Stated.Calculations Reviewed to Determine Acceptance.Corrective Action Deemed Necessary.Bar Along Length of Washer Plate Added | /01T-0:on 810316,Unit 1 Wedge Plates Discovered to Be Smaller than Required Size.Cause Not Stated.Calculations Reviewed to Determine Acceptance.Corrective Action Deemed Necessary.Bar Along Length of Washer Plate Added | | | 05000369/LER-1981-025-01, /01T-0:on 810319,no Seismic Bracing or Calculations Found for 12 Reactor Bldg safety-related Electrical Cable Tray Hanger Stds.Cause Not Stated.Seismic Calculations Performed on Affected Hangers | /01T-0:on 810319,no Seismic Bracing or Calculations Found for 12 Reactor Bldg safety-related Electrical Cable Tray Hanger Stds.Cause Not Stated.Seismic Calculations Performed on Affected Hangers | | | 05000369/LER-1981-025, Forwards LER 81-025/01T-0 | Forwards LER 81-025/01T-0 | | | 05000369/LER-1981-026-03, /03L-0:on 810305,EMF Sys Panel Alarm in Control Room Indicated Malfunction of EMF-43A.Alarm Could Not Be Cleared & Control Room Outside Air Intake Gaseous Activity Monitor Inoperable.Caused by Broken Bnc Jack | /03L-0:on 810305,EMF Sys Panel Alarm in Control Room Indicated Malfunction of EMF-43A.Alarm Could Not Be Cleared & Control Room Outside Air Intake Gaseous Activity Monitor Inoperable.Caused by Broken Bnc Jack | | | 05000369/LER-1981-026, Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | |
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